IR 05000313/2025004

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Integrated Inspection Report 05000313/2025004 and 05000368/2025004
ML26033A438
Person / Time
Site: Arkansas Nuclear  
Issue date: 02/03/2026
From: John Dixon
NRC/RGN-IV/DORS/PBD
To: Pehrson D
Entergy Operations
References
IR 2025004
Download: ML26033A438 (0)


Text

February 03, 2026

SUBJECT:

ARKANSAS NUCLEAR ONE - INTEGRATED INSPECTION REPORT 05000313/2025004 AND 05000368/2025004

Dear Doug Pehrson:

On December 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Arkansas Nuclear One. On January 15, 2026, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Arkansas Nuclear One.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Arkansas Nuclear One. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, John L. Dixon Jr., Chief Reactor Projects Branch D Division of Operating Reactor Safety Docket Nos. 05000313 and 05000368 License Nos. DPR-51 and NPF-6

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000313 and 05000368

License Numbers:

DPR-51 and NPF-6

Report Numbers:

05000313/2025004 and 05000368/2025004

Enterprise Identifier:

I-2025-004-0002

Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One

Location:

Russellville, AR

Inspection Dates:

October 1, 2025, to December 31, 2025

Inspectors:

J. Drake, Senior Reactor Inspector

N. Greene, Senior Health Physicist

M. Mondou, Resident Inspector

A. Sanchez, Senior Project Engineer

B. Tindell, Senior Resident Inspector

E. Tinger, Acting Senior Resident Inspector

Approved By:

John L. Dixon Jr., Chief

Reactor Projects Branch D

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Include Sufficient Technical Information in an Integrated Control System Work Instruction Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green FIN 05000313/2025004-01 Open/Closed None (NPP)71152A A self-revealed Green finding was identified when the licensee failed to include sufficient technical information in a work order used to calibrate function generators in the Unit 1 integrated control system. Specifically, the calibration work order did not include instructions to periodically calibrate an unused breakpoint for the loop B delta P function generator module. Therefore, the unused breakpoint was not adjusted for acceptable output response leading to an erroneous output signal causing main feedwater pump B to fail to adequately maintain steam generator water level following a reactor trip.

Failure to Maintain Transformer Fire Deluge Pull Stations Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000313/2025004-02 Open/Closed

[P.1] -

Identification 71153 A self-revealed Green finding and associated non-cited violation of Unit 1 License Condition 2.C.(8) was identified when the licensee failed to maintain in effect all provisions of the approved fire protection program. Specifically, the licensees failure to maintain manual actuation stations in the procedurally required configuration resulted in multiple spurious fire suppression deluge actuations and a Unit 1 trip. This event was reported as Licensee Event Report 05000313/2025-001-00 (ML25324A399).

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000313/2025-001-00 Automatic Reactor Trip Due to Fault on the 'B' Main Phase Transformer 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at approximately 70 percent rated thermal power during a coastdown for refueling outage 1R32. On October 10, 2025, the unit was shut down for planned refueling outage 1R32. On November 12, 2025, the reactor was made critical following completion of the refueling outage and returned to full power on November 17, 2025, where it remained for the remainder of the inspection period.

Unit 2 operated at or near full rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk-significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, spent fuel pool cooling during core offload operations during refueling outage 1R32, on October 20, 2025
(2) Unit 1, reactor coolant system pressure, level, and temperature instruments during lowered inventory conditions during refueling outage 1R32, on October 31, 2025
(3) Unit 1, fire water deluge systems following emergency feedwater pump room fire water deluge actuation, on December 17, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 1, north switchgear room, fire area I-2, due to safety-related equipment in the area, on October 3, 2025
(2) Unit 1, reactor building, fire area J, due to safety-related equipment in the area, on October 7, 2025
(3) Unit 2, volume control tank room, motor control center 2B63 room, and various other rooms, fire area HH, due to cables important to safe shutdown in the area, on October 31, 2025 71111.08P - Inservice Inspection Activities (PWR)

Due to the government shutdown, this inspection was completed remotely via in office document review. The inspectors verified that the reactor coolant system boundary, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing documents associated with the following activities in Unit 1 during refueling outage 1R32 from December 11 to December 31, 2025.

PWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01) (1 Sample)

The inspectors verified that the following nondestructive examination and welding activities were performed appropriately:

(1) Ultrasonic Examination

Visual 1 Examination

  • 1-ISI-VT-25-021 high-pressure injection support MU-170
  • 1-ISI-VT-25-040 main steam, MS-144, constant force spring
  • 1-ISI-VT-25-020 high-pressure injection, MU-120 - 1-way restraint Welding Activities

reactor coolant, RCP seal flow transmitters PDT-1282, FW-52, FW-53, FW-54, and FW-55, socket welds PWR Inservice Inspection Activities Sample - Vessel Upper Head Penetration Inspection

Activities (IP Section 03.02) (1 Sample)

The inspectors verified that the licensee conducted the following vessel upper head penetration inspections and addressed any identified defects appropriately:

(1) The licensee performed a Bare-Metal Visual Examination of the RPVCH upper surface with a robotic crawler and remote cameras and supplemented by direct visual examination in accordance with the requirements of ASME Code Case N-729-6 and as directed by CEP-NDE-0955, Visual Examination (VE) of Bare-Metal Surfaces.

One hundred percent of the required RPVCH surface was examined including 360 degrees around each CRDM nozzle annulus where it penetrates the RPVCH.

The inspector reviewed NDE report 1-ISI-VT-25-019, RVH instrumentation nozzles and vent lines.

PWR Inservice Inspection Activities Sample - Boric Acid Corrosion Control Inspection Activities (IP Section 03.03) (1 Sample)

The inspectors verified the licensee is managing the boric acid corrosion control program through a review of the following evaluations:

(1)

  • CZ-12A, entered into corrective action program, cleaned deposits
  • CZ-15, entered into corrective action program, cleaned deposits
  • CZ-17A, entered into corrective action program, cleaned deposits
  • CZ-21, entered into corrective action program, cleaned deposits
  • CZ-22C, entered into corrective action program, cleaned deposits
  • CZ-38A, entered into corrective action program, cleaned deposits
  • CZ-39, entered into corrective action program, cleaned deposits
  • CZ-41A, entered into corrective action program, cleaned deposits
  • CZ-42, entered into corrective action program, cleaned deposits
  • DH-1003, entered into corrective action program, cleaned deposits
  • DH-1409, entered into corrective action program, cleaned deposits
  • DH-1449, entered into corrective action program, cleaned deposits
  • DZ-13B, entered into corrective action program, cleaned deposits
  • MU-22A, entered into corrective action program, cleaned deposits
  • MU-2415A, entered into corrective action program, cleaned deposits
  • P-32D, entered into corrective action program, cleaned deposits
  • P-35B, entered into corrective action program, cleaned deposits
  • PDT-1029, entered into corrective action program, cleaned deposits
  • RBD-12A, entered into corrective action program, cleaned deposits
  • RBD-1002A, entered into corrective action program, cleaned deposits
  • RBD-1003A, entered into corrective action program, cleaned deposits
  • RBD-1004A, entered into corrective action program, cleaned deposits
  • RC-1053A, entered into corrective action program, cleaned deposits
  • YT-78, entered into corrective action program, cleaned deposits PWR Inservice Inspection Activities Sample - Steam Generator Tube Inspection Activities (Section 03.04)

No ASME Code inspection of steam generator tubes was required this outage.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed and evaluated licensed operator performance in the control room during Unit 2, turbine generator valve stroke testing, on October 2, 2025.
(2) The inspectors observed and evaluated licensed operator performance in the control room during the shutdown of Unit 1 for refueling outage 1R32, on October 11, 2025.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed and evaluated Unit 2 continued training simulator activities on December 11, 2025.
(2) The inspectors observed and evaluated Unit 1 continued training simulator activities on December 16, 2025.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 1, reactor building isolation valves due to failures during stroking, on December 9, 2025

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities to ensure the following SSC remains capable of performing its intended function:

(1) Unit 1, main steam isolation valve CV-2692 stem and disk replacement, on November 20, 2025

Aging Management (IP Section 03.03) (1 Sample)

The inspectors evaluated the effectiveness of the aging management program for the following SSCs that did not meet their inspection or test acceptance criteria:

(1) Units 1 and 2, cable jackets cracked due to elevated temperatures and age, on November 21, 2025

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 1, planned elevated and high risk due to refueling outage 1R32, on October 1, 2025
(2) Unit 1, planned elevated risk due to lowered reactor coolant system inventory, on November 13, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 1, polar crane functionality assessment due to missing hardware and controller malfunctions, on October 15, 2025
(2) Unit 1, reactor fuel operability determination due to fuel reconstitution activities, on October 17, 2025
(3) Unit 1, primary coolant sources outside containment functionality assessment due to leakage from the waste gas surge tank, on November 17, 2025
(4) Unit 1, electromatic relief valve operability determination due to failure to close at low reactor coolant system pressure, on November 20, 2025
(5) Unit 1, high-pressure injection train B operability determination due to discharge isolation valve CV-1228 failure to fully close during testing, on November 20, 2025

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 1, permanent modification of emergency diesel generator B governor solenoid, on December 4, 2025

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated the Unit 1 refueling outage 1R32 activities from October 11, 2025, through November 13, 2025.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (3 Samples)

(1) Unit 1, integrated engineered safeguards system test after maintenance on engineered safeguards components, on November 3, 2025
(2) Unit 1, off-site power undervoltage and protective relay test after preventive maintenance, on November 4, 2025
(3) Unit 1, main steam isolation valve CV-2692 test after valve rebuild, on November 20, 2025

Surveillance Testing (IP Section 03.01) (2 Samples)

(1) Unit 1, emergency core cooling sump inspection, on October 30, 2025
(2) Unit 1, startup transformer No. 2 load shedding surveillance test, on November 24, 2025

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1) Unit 1, service water to emergency diesel generator K-4B valve CV-3807 inservice test, on November 24, 2025

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1) Unit 1, equipment hatch local leak rate test, on November 12, 2025

71114.06 - Drill Evaluation

Additional Drill and/or Training Evolution (1 Sample)

The inspectors evaluated:

(1) Unit 2, emergency operating facility drill on failed fuel and reactor coolant system leakage outside containment with safety injection, on December 18, 2025

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (October 1, 2024, through September 30, 2025)
(2) Unit 2 (October 1, 2024, through September 30, 2025)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (October 1, 2024, through September 30, 2025)
(2) Unit 2 (October 1, 2024, through September 30, 2025)

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) July 1, 2024, through September 30, 2025 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
(1) July 1, 2024, through September 30, 2025 71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Unit 1, review of integrated control system card calibrations following failure of main feedwater to automatically control steam generator level after the September 24, 2025, reactor trip, on November 21, 2025

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends that might be indicative of a more significant safety issue. The inspectors performed an in-depth review of the licensee's ability to identify fire water system leakage, evaluate each occurrence, and implement corrective actions. The inspectors determined evidence of an emerging trend in this area, verified the licensee was aware of this trend, and documented an observation. No issues of more than minor significance were identified.

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000313/2025-001-00, Automatic Reactor Trip Due to Fault on the B Main Phase Transformer, (ML25324A399). The inspection conclusions associated with this LER are documented in this report as a non-cited violation under Inspection Results Section 71153. This LER is Closed.

INSPECTION RESULTS

Failure to Include Sufficient Technical Information in an Integrated Control System Work Instruction Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green FIN 05000313/2025004-01 Open/Closed None (NPP)71152A A self-revealed Green finding was identified when the licensee failed to include sufficient technical information in a work order used to calibrate function generators in the Unit 1 integrated control system. Specifically, the calibration work order did not include instructions to periodically calibrate an unused breakpoint for the loop B delta P function generator module. Therefore, the unused breakpoint was not adjusted for acceptable output response leading to an erroneous output signal causing main feedwater pump B to fail to adequately maintain steam generator water level following a reactor trip.

Description:

Following a Unit 1 reactor trip on September 24, 2025, the control room observed lowering steam generator B water level due to main feedwater pump B speed decreasing. Operators opened the feedwater pump discharge crosstie valve so main feedwater pump A could restore steam generator B water level. Investigations determined that the integrated control system (ICS), which controls main feedwater pump speed from a differential pressure error signal, was malfunctioning. Specifically, the ICS loop B delta P function generator module, which controls main feedwater pump B speed, caused an erroneous output signal post-trip due to the module input signal exceeding +10Vdc.

The function generator module normally receives one input signal and produces an output signal which approximates a curve with four straight line segments, each beginning with a breakpoint. The loop B delta P function generator receives a feedwater valve differential pressure error signal and provides an output signal that controls main feedwater pump B speed. The inspectors reviewed Model Work Order 50235594 associated with the calibration of the function generator module and determined that the fourth function generator breakpoint was listed as N/A. Vendor Manual TDB015 0710, Instruction Manual for Integrated Control and Non-Nuclear Instrumentation Systems, Revision 7, states, in part, when calibrating the function generator, the breakpoints must be determined, and all four breakpoints must be adjusted. Since the unused fourth breakpoint was not specified to be calibrated in the work order, the breakpoint was not adjusted to provide an acceptable response when the input signal was greater than +10Vdc. The licensee determined that a total of seven function generator cards for the ICS system, including the loop A delta P function generator module associated with main feedwater pump A, were adversely affected due to the calibration instructions for unused breakpoints. The loop A delta P function generator provided the correct output signal during the Unit 1 reactor trip which allowed the pump to respond properly and maintain steam generator water level.

Entergy Procedure EN-MA-106, Planning, Revision 2, Attachment 9, Work Instruction Development, states, in part, to include vendor technical information in work order instructions. Contrary to EN-MA-106, the licensee did not include the vendor technical manual requirements to periodically adjust all four function generator module breakpoints since the unused fourth breakpoint was not specified to be calibrated in the model work order.

The inadequate work instructions led to the erroneous signal which caused main feedwater pump B to reduce speed post-trip.

Corrective Actions: The licensee updated the work instruction for calibration of the seven ICS function generator modules, and the seven cards were recalibrated.

Corrective Action References: Condition Reports CR-ANO-1-2025-01383, CR-ANO-1-2025-01755

Performance Assessment:

Performance Deficiency: The licensees failure to include sufficient technical information in the ICS function generator calibration work order was a performance deficiency. The performance deficiency was within the licensees ability to foresee and correct because Procedure EN-MA-106, Planning, discusses the requirement to include vendor technical information in work instructions. Specifically, the licensee failed to plan for periodic calibrations of unused breakpoints for function generator modules, which led to main feedwater pump B being unable to maintain steam generator water level following a reactor trip.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inspectors determined the inadequate ICS function generator calibration instructions led to main feedwater pump B reducing speed and lowering steam generator water level when feedwater was required to cool the reactor coolant system following a reactor trip.

Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The finding was determined to be of very low safety significance (Green) because it did not:

(1) represent a deficiency affecting the design or qualification of a mitigating SSC;
(2) represent a loss of the PRA function of a single train TS system;
(3) represent an actual loss of the PRA function of one train of a multi-train TS system for more than its TS allowed outage time or;
(4) two separate safety systems for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />;
(5) represent a loss of a PRA system and/or function as defined in the PRIB or the licensees PRA for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and
(6) represent a loss of a PRA function of one or more non-TS trains of equipment designated as risk-significant in accordance with the licensees maintenance rule program for greater than 3 days. Specifically, ICS is not a safety-related TS system, and the PRA functionality for the main feedwater system was maintained following the reactor trip by main feedwater pump A feeding one steam generator, ensuring continuous cooling was maintained to the reactor coolant system.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance. Specifically, the model work order had not been revised within the last 3 years, and there was not an opportunity to recognize the issue between the last work order update and the present.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Observation: Review of Fire Water System Leakage 71152S The inspectors performed a review of potential adverse trends in the licensees corrective action program with emphasis on fire water system leaks. Records in the sites corrective action program, in addition to other administrative records, showed there has been a negative trend of fire water leaks, including valve leakage and through-wall leakage. During a review of site condition reports over the last year, the inspectors identified 15 condition reports related to fire water valve leakage and 12 condition reports related to fire water piping through-wall leakage across Units 1 and 2. The inspectors identified two fire water leaks that were large enough to decrease fire water system pressure to approximately 110 pounds per square inch gauge (psig) and automatically start the electric fire water pump. These leaks were larger than the capacity of the jockey pump, 50 gallons per minute, which normally maintains system pressure at 118 to 134 psig. The inspectors also performed a review of the site fire impairment database and identified 11 fire impairment forms documented over the last year due to fire water system isolations caused by system leakage. Several fire impairments documented compensatory actions required, such as un-isolating valves to supply fire water and staging fire hoses. These compensatory actions can delay the site fire brigade from responding to fires.

The licensee is aware of the issues relating to the fire water system and recently documented a trend for degraded underground fire system leaks in Condition Report CR-ANO-C-2025-01688. The current state of the site fire water system could indicate the existence of a more significant safety issue caused by an aggregation of small system leaks or large ruptures stressing the system. No more than minor issues were identified.

Failure to Maintain Transformer Fire Deluge Pull Stations Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000313/2025004-02 Open/Closed

[P.1] -

Identification 71153 A self-revealed Green finding and associated non-cited violation of Unit 1 License Condition 2.C.(8) was identified when the licensee failed to maintain in effect all provisions of the approved fire protection program. Specifically, the licensees failure to maintain manual actuation stations in the procedurally required configuration resulted in multiple spurious fire suppression deluge actuations and a Unit 1 trip. This event was reported as Licensee Event Report 05000313/2025-001-00 (ML25324A399).

Description:

On September 24, 2025, Unit 1 automatically tripped from approximately 89.7 percent reactor power on a valid reactor protection system actuation due to a fault on the Unit 1 main transformer B. The cause of the actuation was determined to be a spurious actuation of the Unit 1 main transformer B deluge. The spurious actuation was caused by fire deluge hand switch HS-5636 B, a manual actuation pull station that opens UAV-5636, inadvertently opening allowing fire water to reach the transformer. HS-5636 was found with a failed tamper seal that showed signs of environmental degradation and an incorrectly sized break rod which was not securing the manual actuation station. Unit 1 Procedure OP-1104.032, Fire Protection Systems, Revision 98, includes instructions for installation of the break rod for certain manual actuation pull stations. These procedures are used during manual actuation station resetting and certain tests of the fire protection system, including the transformer deluges, and should have identified and corrected the inadequate condition of the break rods. Following the Unit 1 reactor trip, the licensee identified multiple manual actuation pull stations in Unit 1 and Unit 2 with incorrectly sized break rods. Spurious actuations caused by incorrect break rods for manual actuation pull stations installed in Unit 2 occurred on July 9, 2022, and September 23, 2025.

Corrective Actions: The licensee upgraded manual actuation pull stations on Unit 1 during a planned refueling outage; identical actions are planned for Unit 2 manual actuation pull stations.

Corrective Action References: Condition Report CR-ANO-1-2025-01382

Performance Assessment:

Performance Deficiency: The licensees failure to maintain manual actuation pull stations in the procedurally required configuration was a performance deficiency. Specifically, the licensee failed to correctly perform Procedure OP-1104.032, Fire Protection Systems, Revision 98. Specific portions of this procedure ensure manual pull stations are properly secured via a break rod and a tamper seal. The cause of the issue of concern was reasonably within the licensees ability to foresee and correct because previous spurious deluge actuations on Unit 2 main transformer A on July 9, 2022, and September 23, 2025, with manual actuation pull stations of identical design indicated the correct break rod was not installed and the tamper seal degrades over time.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensees failure to maintain manual actuation pull stations lead to a fault on the Unit 1 main transformer B and an automatic reactor trip.

Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The finding was determined to be of very low safety significance (Green) because it did not cause both a reactor trip and the loss of mitigating equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-Cutting Aspect: P.1 - Identification: The organization implements a corrective action program with a low threshold for identifying issues. Individuals identify issues completely, accurately, and in a timely manner in accordance with the program. Specifically, the licensee failed to identify the manual pull station break rods when addressing spurious deluge actuations or resetting following testing.

Enforcement:

Violation: Arkansas Nuclear One, Unit 1 License Condition 2.C.(8) states, in part, the licensee shall implement and maintain in effect all provisions of the approved fire protection program that comply with 10 CFR 50.48(a) and 10 CFR 50.48(c), as specified in the license amendment request dated January 29, 2014. The license amendment request dated January 29, 2014, Attachment A, Section 3.2.3, Procedures (1), states, in part, procedures are established for inspection, testing, and maintenance of fire protection systems.

Procedure OP-1104.032, Fire Protection Systems, Revision 98, Section 14, Resetting 4-inch and 6-inch Multimatic Deluge Valve, requires manual pull stations for UAV-5619, UAV-5635, UAV-5636, and UAV-5637 have a tamper seal and a break rod installed, with the break rod almost flush with the top of the pull station.

Contrary to the above, prior to September 24, 2025, the licensee failed to maintain in effect all provisions of the approved fire protection program, as specified in the license amendment request dated January 29, 2014, for Unit 1. Specifically, the licensee failed to maintain manual actuation pull stations with a break rod almost flush with the top of the pull station as specified in OP-1104.032, which resulted in spurious deluge actuation on the Unit 1 main transformer B on September 24, 2025, and subsequent Unit 1 automatic trip from a valid reactor protection system actuation.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On December 31, 2025, the inspectors presented the Unit 1 inservice inspection results to Gary Sullins, General Manager of Plant Operations, and other members of the licensee staff.
  • On January 15, 2026, the inspectors presented the integrated inspection results to Doug Pehrson, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Drawings

M-219, Sheet 4

Piping & Instrument Diagram Deluge Valve Trim Details

71111.04

Drawings

M-219, Sheet 5

Piping & Instrument Diagram Deluge Valve Trim Details

71111.04

Drawings

M-232, Sheet 1

Piping & Instrument Diagram Decay Heat Removal System

111

71111.04

Drawings

M-235, Sheet 1

Piping & Instrument Diagram Spent Fuel Cooling System

71111.04

Procedures

OP-1015.002

Decay Heat Removal and LTOP System Control

71111.04

Procedures

OP-1015.048

Shutdown Operations Protection Plan

71111.04

Procedures

OP-1104.006

Spent Fuel Cooling System

71111.04

Procedures

OP-1104.032

Fire Protection Systems

71111.05

Corrective Action

Documents

CR-ANO-

2-2025-01499

71111.05

Miscellaneous

FHA

Fire Hazards Analysis

71111.05

Procedures

PFP-U1

ANO Prefire Plan (Unit 1)

71111.05

Procedures

PFP-U2

ANO Prefire Plan (Unit 2)

71111.08P

Corrective Action

Documents

CR-ANO-

1-2025-01304, 1-2025-01550, 1-2025-01551, 1-2025-01557,

1-2025-01563, 1-2025-01606, 1-2025-01614, 1-2025-01620,

1-2025-01718, 1-2025-01783, 1-2025-01785, 1-2025-01837,

1-2025-01842, 1-2025-01870, 1-2025-01964, 1-2025-02131

71111.08P

Engineering

Changes

EC-0054337820

Pipe Support MS-144 Enhancements

71111.08P

NDE Reports

1-BOP-VT-25-004

  1. 37 Reactor Vessel Stud, Nut and Flange (Stud Hole)

10/21/2025

71111.08P

NDE Reports

1-ISI-VE-21-003

Reactor Vessel Head Examination

04/27/2021

71111.08P

NDE Reports

1-ISI-VE-25-003

Suction Pipe to Safe-End (RCP B)

10/16/2025

71111.08P

NDE Reports

1-ISI-VT-22-002

Cold Leg Drain Nozzle to Safe-End Circ Weld (RCP B)

10/14/2022

71111.08P

NDE Reports

1-ISI-VT-25-019

Reactor Vessel Head Instrumentation Nozzles and Vent Lines

10/18/2025

71111.08P

NDE Reports

1-ISI-VT-25-020

MU-120 - 1-Way Restraint

10/21/2025

71111.08P

NDE Reports

1-ISI-VT-25-021

MU-120, Variable Spring

10/22/2025

71111.08P

NDE Reports

1-ISI-VT-25-040

MS-144, Constant Force Spring

11/12/2025

71111.08P

NDE Reports

1-PT-VT-25-017

P-32D, Reactor Coolant Pump

10/23/2025

71111.08P

NDE Reports

71111.08P

Procedures

CEP-NDE-0955

Visual Examination (VE) of Bare-Metal Surfaces

308

71111.11Q

Miscellaneous

A2SPG-LOR-

260202

EOP-Station Blackout Simulator

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.11Q

Procedures

EN-OP-115

Conduct of Operations

71111.11Q

Procedures

OP-1102.010

Plant Shutdown and Cooldown

71111.11Q

Procedures

OP-1102.016

Power Reduction and Plant Shutdown

71111.11Q

Procedures

OP-1202.006

Tube Rupture

71111.11Q

Procedures

OP-1203.023

Small Steam Generator Tube Leaks

71111.11Q

Procedures

OP-2106.009

Turbine Generator Operations

71111.12

Corrective Action

Documents

CR-ANO-

1-2008-01603, 1-2018-01458, 1-2021-01168, 1-2022-02340,

1-2025-01821, 1-2025-01840, 1-2025-02044

71111.12

Miscellaneous

PO-10462164

QC Inspection for Body to Bonnet Gasket

2/22/2015

71111.12

Miscellaneous

PO-62213913

Purchase Order for Disk/Stm/Stm-Dik/Piston Assy

71111.12

Procedures

EN-DC-308

Safety & Quality Classification of Replacement Parts

71111.12

Procedures

EN-DC-313

Procurement Engineering Process

71111.12

Procedures

EN-DC-346

Cable Reliability Program

71111.12

Procedures

EN-DC-348

Non-EQ Insulated Cables and Connections Inspection

71111.12

Procedures

EN-MA-138

VLF Tan Delta and Withstand Testing of Electrical Power

Cables

71111.12

Procedures

EN-MA-148

Motor Operated Valve Diagnostics

71111.12

Work Orders

WO 53037132

71111.13

Calculations

CALC-09-E-0008-

ANO-1 NFPA 805 Non-Power Operations Assessment

71111.13

Corrective Action

Documents

CR-ANO-

1-2025-01573

71111.13

Miscellaneous

1R32 Outage Risk Assessment Team Report

71111.13

Procedures

EN-OP-119

Protected Equipment Postings

71111.13

Procedures

OP-1015.002

Decay Heat Removal and LTOP System Control

71111.15

Calculations

CALC-27A

Polar Crane Girder

71111.15

Corrective Action

Documents

CR-ANO-

1-2021-01589, 1-2021-01777, 1-2025-01127, 1-2025-01146,

1-2025-01571, 1-2025-01653, 1-2025-01656, 1-2025-01692,

1-2025-01725, 1-2025-01732, 1-2025-01746, 1-2025-01832,

1-2025-02085

71111.15

Engineering

Changes

EC-46557

Provide PSV-1000 Closure Stroke Time Acceptance Criteria

71111.15

Miscellaneous

PMCR-ANO-

Revise the PM Strategy of PSV-1000 IAW RV Program

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2016-00255207

71111.15

Procedures

OP-1202.012

RT-2

03/07/23

71111.15

Procedures

OP-1305.013

Leak Testing the Gaseous Radwaste System

71111.18

Engineering

Changes

EC-0054248561

K-4A&B Governor Run Solenoid Replacements

71111.18

Engineering

Changes

EC-0054248564

Child EC to 0054248561 - Replace K-4B Run Solenoid

71111.18

Procedures

EN-DC-115

Engineering Change Process

71111.18

Work Orders

WO 54319055

71111.20

Calculations

CALC-06-E-0003-

Allowable Void Size Indication for LPI/DH Header

71111.20

Corrective Action

Documents

CR-ANO-

1-2025-01368, 1-2025-02339

71111.20

Miscellaneous

OpESS 2007/03

Crane and Heavy Lift Inspection, Supplemental Guidance to

IP 71111.20 and IP 71111.13

09/01/2018

71111.20

Procedures

COLR

Cycle 33 Core Operating Limits Report

71111.20

Procedures

EN-OP-115.02

Control Room Conduct and Access Control

71111.20

Procedures

EN-OP-115.14

Reactivity Management

71111.20

Procedures

OP-1015.002

Decay Heat Removal and LTOP System Control

71111.20

Procedures

OP-1015.048

Shutdown Operation Protection Plan

71111.20

Procedures

OP-1102.002

Plant Startup

24

71111.20

Procedures

OP-1102.008

Approach to Criticality

71111.20

Procedures

OP-1102.016

Power Reduction and Plant Shutdown

71111.20

Procedures

OP-1102.10

Plant Shutdown and Cooldown

71111.20

Procedures

OP-1103.011

Draining and N2 Blanketing the RCS

71111.20

Procedures

OP-1104.004

Decay Heat Removal Operating Procedure

141

71111.20

Procedures

OP-1504.007

Unit 1 Reactor Vessel Closure Head Removal and Storage

71111.20

Procedures

ORAT

Outage Risk Assessment Team Report

71111.24

Corrective Action

Documents

CR-ANO-

1-2025-01840, 1-2025-01845, 1-2025-01848

71111.24

Engineering

Changes

EC-0000073910

Baseline Reference Values for ANO1 IST Components

71111.24

Procedures

OP-1015.036

Containment Building Closeout

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.24

Procedures

OP-1305.005

SU#2 Transformer Load Shedding Test

71111.24

Procedures

OP-1305.006

Integrated ES System Test

71111.24

Procedures

OP-1305.007

RB Isolation and Miscellaneous Valve Stroke Test

71111.24

Procedures

OP-1305.037

Unit 1 Reactor Building Access & Ventilation Leak Rate

Testing

71111.24

Procedures

OP-1305.059

Off-site Power Undervoltage and Protective Relay Test

71111.24

Procedures

OP-1402.038

Unit 1 Equipment Hatch Opening, Closing, and Maintenance

71111.24

Procedures

OP-1402.069

Main Steam Isolation Valve (MSIV) Disassembly, Inspect.,

Repair & Reassembly

71111.24

Work Orders

WO 54141816, 54165044, 54167396, 54169938, 54174197,

210679

71114.06

Miscellaneous

Red Team 4th Qtr PI Drill

2/18/2025

71151

Calculations

CALC-ANO1-SA-

16-00001

ANO-1 Mitigating System Performance Index Basis

71151

Calculations

CALC-ANO2-SA-

06-00001

ANO-2 Mitigating System Performance Index Basis

71151

Procedures

EN-LI-114

Regulatory Performance Indicator Process

71151

Self-Assessments

LO-ANO-2024-

00052

Radiation Inspection - Performance Indicator Verification -

IP 71151

07/09/2025

71152A

Corrective Action

Documents

CR-ANO-

1-2025-01755, 1-2025-02153

71152A

Engineering

Changes

EC-54338518

Expanding Calibration of Function Generators with Unused

Break Points

71152A

Work Orders

WO 235594

71152S

Corrective Action

Documents

CR-ANO

C-2025-01688

71152S

Procedures

OP-1000.120

ANO Fire Impairment Program

71153

Corrective Action

Documents

CR-ANO-

1-2025-01382

71153

Procedures

OP-1104.032

Fire Protection Systems

98