IR 05000305/2002008
| ML030280288 | |
| Person / Time | |
|---|---|
| Site: | Kewaunee |
| Issue date: | 01/27/2003 |
| From: | Kenneth Riemer NRC/RGN-III/DRP/RPB5 |
| To: | Coutu T Nuclear Management Co |
| References | |
| IR-02-008 | |
| Download: ML030280288 (30) | |
Text
January 27, 2003
SUBJECT:
KEWAUNEE NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION REPORT 50-305/02-08
Dear Mr. Coutu:
On December 28, 2002, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Kewaunee Nuclear Power Plant. The enclosed report documents the inspection findings which were discussed on January 7, 2003, with you and members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
On the basis of the results of this inspection, no findings of significance were identified.
Since the terrorist attacks on September 11, 2001, the NRC has issued two Orders (dated February 25, 2002, and January 7, 2003) and several threat advisories to licensees of commercial power reactors to strengthen licensee capabilities, improve security force readiness, and enhance access authorization. The NRC also issued Temporary Instruction 2515/148 on August 28, 2002, that provided guidance to inspectors to audit and inspect licensee implementation of the interim compensatory measures (ICMs) required by the February 25th Order. Phase 1 of TI 2515/148 was completed at all commercial nuclear power plants during 2002, and the remaining inspections are scheduled for completion in 2003.
Additionally, table-top security drills were conducted at several licensees to evaluate the impact of expanded adversary characteristics and the ICMs on licensee protection and mitigative strategies. Information gained and discrepancies identified during the audits and drills were reviewed and dispositioned by the Office of Nuclear Security and Incident Response. For 2003, the NRC will continue to monitor overall safeguards and security controls, conduct inspections, and resume force-on-force exercises at selected power plants. Should threat conditions change, the NRC may issue additional Orders, advisories, and temporary instructions to ensure adequate safety is being maintained at all commercial power reactors. In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Kenneth Riemer, Chief Branch 5 Division of Reactor Projects Docket No. 50-305 License No. DPR-43
Enclosure:
Inspection Report 50-305/02-08
REGION III==
Docket No:
50-305 License No:
DPR-43 Report No:
50-305/02-08 Licensee:
Nuclear Management Company, LLC Facility:
Kewaunee Nuclear Power Plant Location:
N 490 Highway 42 Kewaunee, WI 54216 Dates:
October 1 through December 28, 2002 Inspectors:
J. Lara, Senior Resident Inspector Z. Dunham, Resident Inspector M. Farber, Reactor Engineer R. Gibbs, Inspector, Office of Nuclear Reactor Regulation T. Madeda, Physical Security Inspector H. Peterson, Senior Operations Engineer T. Ploski, Senior Emergency Preparedness Inspector M. Castanedo, Reactor Engineer Approved By:
Kenneth Riemer, Chief Branch 5 Division of Reactor Projects
SUMMARY OF FINDINGS
IR 05000305-02-08; Nuclear Management Company, LLC; on 10/01-12/28/02; Kewaunee
Nuclear Power Plant; Integrated Inspection Report.
This report covers a 3-month period of baseline resident inspection and announced baseline inspections in emergency preparedness, physical security, maintenance rule program, and licensed operator requalification. The inspections were conducted by the resident inspectors, inspectors from the Region III office, and an inspector from the Office of Nuclear Reactor Regulation. There were no findings identified during this inspection. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.
Inspection Findings No findings of significance were identified.
B.
Licensee-Identified Findings No findings of significance were identified.
REPORT DETAILS
Summary of Plant Status
The plant was operated at approximately 100 percent power for most of the period except for a brief reduction in power to facilitate quarterly scheduled surveillance testing.
REACTOR SAFETY
Cornerstones:
Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
1R01 Adverse Weather Protection
.1 Circulating Water Intake and Forebay Freeze Protection
a. Inspection Scope
On October 28, 2002, the inspectors reviewed the facility design and the licensees procedures to prevent and cope with freezing of the circulating water intake and forebay to ensure that the facilitys ultimate heat sink (Lake Michigan) would remain available during periods of extreme cold weather. In preparation for the walkdown, the inspectors reviewed Procedure E-CW-04, Loss of Circulating Water, Revision T, which prescribed operator actions to take in the event of icing of the forebay traveling water screens, to verify that all operator actions were capable of being performed as written. Additionally, the inspectors evaluated the forebay design to ensure that during a forebay icing event the fire pumps would remain available for use. The inspectors considered fire pump availability important during an icing event because one prescribed operator action was to wash down the traveling water screens using fire hoses to remove slush ice. On December 2, the inspectors verified the circulating water recirculation pump lineup which the licensee had recently started. The circulating water recirculation pump, which the licensee operated when circulating water temperature was below 35 degrees Fahrenheit
(F), provided flow from the circulating water discharge to the intake crib to prevent local icing at the crib.
b. Findings
No findings of significance were identified.
.2 Facility Air Handling Systems
a. Inspection Scope
On October 29, 2002, the inspectors evaluated various air ventilation systems, including the auxiliary building and control room ventilation systems, to ensure that the systems were capable of meeting Updated Safety Analysis Report (USAR) design requirements for maintaining internal building temperatures above 60 F with an outside air temperature of -20 F. The inspectors reviewed various operations, normal and abnormal procedures, system drawings, and the USAR in addition to walking down the ventilation system lineups. The inspectors also reviewed the licensees corrective action database to determine whether there were any historical problems associated with cold weather on the facilitys ventilation systems.
b. Findings
No findings of significance were identified.
.3 Diesel Fuel Oil Storage Tanks
a. Inspection Scope
On November 15, 2002, the inspectors reviewed the design of the stations in-ground diesel fuel oil storage tanks, which provided fuel oil storage for the safety-related diesel generators, to verify that the tanks were adequately protected from freezing weather. In addition to reviewing the design of the tanks, the inspectors reviewed the maintenance history of the fuel oil transfer pumps and their susceptibility to freezing weather to ensure that the pumps would operate as required under extreme weather conditions.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
a. Inspection Scope
The inspectors conducted partial walkdowns of the system trains listed below while the opposite train of equipment was out-of-service to verify that the systems were correctly aligned to perform their design safety function. In preparation for the walkdowns, the inspectors reviewed the system lineup checklists, normal operating procedures, abnormal and emergency operating procedures, and system drawings to verify the correct system lineup. During the walkdowns, the inspectors also examined valve positions and electrical power availability to verify that valve and electrical breaker positions were consistent with, and in accordance with, the licensees procedures and design documentation. The material condition of the equipment was also inspected.
- Service Water (SW) - Train A - October 4, 2002
- Diesel Generator - Train A - November 7
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
The inspectors walked down ten plant areas to assess the overall readiness of fire protection equipment and barriers:
- Auxiliary Building Basement (Waste Handling Area) - October 10, 2002
- Auxiliary Building Basement (Bus 1 and Bus 2) - October 18
- Carbon Dioxide Storage Tank Room - October 24
- Auxiliary Feedwater Pump Train A Room - December 3
- Safeguard Alley Train B - December 3
- Turbine Oil Storage Tank Room - December 6
- Cable Spreading Room - December 12
- Auxiliary Building Fan Floor - December 13
- Screenhouse - December 19
- Technical Support Center and Non-Safeguard Battery Rooms - December 24 Emphasis was placed on the control of transient combustibles and ignition sources, the material condition of fire protection equipment, and the material condition and operational status of fire barriers used to mitigate fire damage or propagation.
Additionally, fire hoses, sprinklers, and portable fire extinguishers were inspected to verify that they were in satisfactory physical condition and were unobstructed. Passive features such as fire doors, fire dampers, and fire zone penetration seals were also inspected to verify that they were in satisfactory condition and capable of providing an adequate fire barrier.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
a. Inspection Scope
On October 22, 2002, the inspectors reviewed Design Change Request 2873, Re-design of Process Piping for Radiation Monitors R-16 and R-20, which was installed in 1998, to determine whether the licensee had adequately addressed potential internal flooding concerns which the design change had introduced. In summary, the design change included routing two 1-inch SW lines which continuously routed water from the SW system returns to an open trench located near electrical bus 1 and bus 2.
The inspectors considered the potential plugging of the trench and subsequent overflow of water into the area to be potentially significant because bus 1 and bus 2, although nonsafety-related, provided 4160-volts alternating current to the main feedwater pumps and reactor coolant pumps, therefore creating an initiating event should the buses become inadvertently grounded.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance
a. Inspection Scope
On October 31, 2002, the licensee conducted heat exchanger performance monitoring on the A train diesel generator jacket water coolers. The inspectors observed portions of the performance monitoring test, reviewed the test procedure, and reviewed the test data to verify that the test was performed as written, that the acceptance criteria were adequate to demonstrate acceptable heat transfer capability of the heat exchanger, and that the test data met the acceptance criteria. Additionally, the inspectors also verified that the test accounted for instrument inaccuracies and that the test frequency was sufficient to provide early detection of heat exchanger degradation prior to any loss of heat removal capabilities below design values.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program
.1 Biennial Written Examination and Annual Operating Test Results
a. Inspection Scope
The inspectors reviewed the overall pass/fail results of individual written tests, Job Performance Measure (JPM) operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee during 2002. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP).
b. Findings
No findings of significance were identified.
.2 Simulator Dynamic Requalification Exam
a. Inspection Scope
On December 9, 2002, the inspectors observed a simulator dynamic requalification exam to evaluate crew performance, formality of communications, and annunciator response. The inspectors reviewed the following licensee procedures and documents to establish the inspection criteria:
- General Nuclear Procedure (GNP) - 03.17.01, Alarm Response Standard, Revision A
- GNP-03.17.02, Briefings Standards, Revision A
- GNP-03.17.04, Communications Standard, Revision A
- Emergency Plan Implementing Procedure AD-02, Emergency Class Determination, Revision AD In addition, the inspectors evaluated the crews implementation of the facilitys abnormal procedures and emergency operating procedures, oversight and direction provided by the shift manager and control room supervisor, and the adequacy of identification and reporting of the event classification in accordance with the facilitys emergency plan.
The inspectors also compared the simulator board configuration with the actual control room board configuration for consistency between the two to verify that the simulator environment matched the actual control room environment as closely as possible. The inspectors observed the post-scenario critique to determine whether performance issues were accurately identified and addressed.
b. Findings
No findings of significance were identified.
==1R12 Maintenance Effectiveness
==
.1 Routine Review of Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the licensee's implementation of the Maintenance Rule, 10 CFR 50.65, for the systems and/or equipment problems listed below. The inspectors observed portions of the licensees troubleshooting and repair efforts to determine the adequacy of the licensees repairs to the affected equipment. The inspectors also reviewed the licensees maintenance practices associated with the failed equipment where applicable to verify that equipment on opposite trains or other systems at the station were not susceptible to maintenance-induced common cause failures.
Additionally, the inspectors reviewed the licensees maintenance rule history and evaluation of each system to verify that they were properly scoped in accordance with 10 CFR 50.65, and that reliability and availability performance criteria were appropriate.
- N-35 Intermediate Range Power Supply Failure - October 9, 2002
- B Train Diesel Generator Speed Response Abnormal During Surveillance Test -
October 11
- Auxiliary Building Ventilation - November 19
b. Findings
No findings of significance were identified.
.2 Biennial Review
Periodic Evaluation
a. Inspection Scope
- Verify that the periodic evaluation was completed within the time restraints defined in 10 CFR 50.65 (once per refueling cycle, not to exceed 2 years).
Ensure that the licensee reviewed its goals, monitored performance of structures, systems, and components (SSCs), reviewed industry operating experience, and made appropriate adjustments to the maintenance rule program as a result of the above activities;
- Verify that the licensee balanced reliability and unavailability during the previous refueling cycle, including a review of safety significant SSCs;
- Verify that (a)(1) goals were met, that corrective action was appropriate to correct the defective condition, including the use of industry operating experience, and that (a)(1) activities and related goals were adjusted as needed; and
- Verify that the licensee has established (a)(2) performance criteria, examined any SSCs that failed to meet their performance criteria, and reviewed any SSCs that have suffered repeated maintenance preventable functional failures including a verification that failed SSCs were considered for (a)(1).
The inspectors examined the Maintenance Rule Periodic Assessments completed for January 1 to December 31, 2001, and February 1, 1999 to January 1, 2001. To evaluate the effectiveness of (a)(1) and (a)(2) activities, the inspector examined a number of Kewaunee Action Requests (ARs) (listed at the end of this report). In addition, ARs were reviewed to verify that the threshold for identification of problems was at an appropriate level and the associated corrective actions were appropriate.
Also, the maintenance rule program documents, audits and self-assessments of the program were reviewed.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessment and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensees evaluation and assessment of plant risk, scheduling, and configuration control during the planned and emergent work activities listed below. In particular, the licensees planning and management of maintenance was evaluated to verify that on-line risk was acceptable and in accordance with the requirements of 10 CFR 50.65(a)(4). Additionally, the inspectors compared the assessed risk configuration against the actual plant conditions and any in-progress evolutions or external events to verify that the assessment was accurate, complete, and appropriate. Licensee actions to address increased on-line risk during these periods were also inspected to verify that actions were in accordance with approved administrative procedures.
- Risk Profile associated with work performed during week ending October 4, 2002
- Risk Profile associated with work performed during week ending October 25
- Risk Profile associated with work performed during week ending November 15
- Risk Profile associated with work performed during week ending November 22
- Risk Profile associated with work performed during week ending December 13
b. Findings
No findings of significance were identified.
1R14 Non-Routine Evolutions
a. Inspection Scope
On December 7, 2002, the unit was reduced to 70 percent power to facilitate quarterly auxiliary feedwater full flow in-service testing and main turbine stop and control valve testing. The inspectors observed selected control room activities and evolutions to evaluate control room staff adherence to plant operating procedures, equipment operation, and communications.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed design basis information and technical specification requirements to verify the technical adequacy of the operability evaluations listed below, to verify that system operability was properly justified, and that the system remained available, such that no unrecognized increase in risk occurred. Where applicable, the inspectors also reviewed calculations and input assumptions to determine the validity of the results.
The inspectors reviewed the following operability evaluations:
- Corrective Action Program (CAP) 13253; B Diesel Generator Speed Response Abnormal When Performing SP 42-312B - October 11, 2002
- CAP 13380; Suspected Water Hammer Following Turbine-Driven Auxiliary Feedwater Pump Start - October 21
- CAP 13507; Non-conservative Assumptions in Determining Motor-Operated Valve Settings - November 1
b. Findings
No findings of significance were identified.
1R16 Operator Workarounds (OWAs)
.1 Control Room Deficiency Tags
a. Inspection Scope
On October 15, 2002, the inspectors reviewed the licensees control room deficiency log, out-of-service control room indicators and equipment, and reviewed posted danger cards located in the control room to determine whether known degraded or out-of-service equipment in the control room would impact operator response to plant transients or emergencies and therefore be considered potential OWAs.
b. Findings
No findings of significance were identified.
.2 Semi-Annual Cumulative Review of OWAs
a. Inspection Scope
On December 4, 2002, the inspectors reviewed all active OWAs to determine whether there were any cumulative effects of the OWAs on the reliability and availability of system equipment, and whether there was any increased impact on operators to respond in a correct and timely manner to plant transients and accidents.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors observed the post-maintenance testing activities associated with the maintenance and emergent work activities listed below to verify that the test was adequate for the scope of the work which had been performed and that the testing acceptance criteria were clear and demonstrated operational readiness consistent with design and licensing basis documents. The inspectors attended pre-job briefings to verify that the impact of the testing had been properly characterized; observed or reviewed the test to verify that the test was performed as written and all testing prerequisites were satisfied; and reviewed the test acceptance criteria. Following the completion of the test, the inspectors conducted walkdowns of the affected equipment, when applicable, to verify that the test equipment was removed and that the equipment was returned to a condition in which it could perform its safety function.
- Motor-Operated Valve RHR-400A Preventative Maintenance - October 18, 2002
- Replacement of Turbine-Driven Auxiliary Feedwater Starting Circuit Relay -
October 21
- Technical Support Center Diesel Generator Preventative Maintenance -
November 27
- Valve RHR-101 Volume Booster Replacement - December 9
- Service Water Pump B2 Replacement - December 10
- Installation of Surge Suppressor on Valve SW-1306A - December 17
- Motor-Operated Valve SW-903B Preventative Maintenance - December 19
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors observed surveillance testing on risk-significant equipment to verify that the equipment was capable of performing its intended safety function and that the surveillance tests satisfied the requirements contained in technical specifications and the licensees procedures, and that the equipment was capable of meeting its design function. During the surveillance tests, the inspectors reviewed the test to verify that it was adequate to demonstrate operational readiness consistent with the design and licensing basis documents, and that the testing acceptance criteria were clear. Portions of the test were observed to verify that the test was performed as written, that all testing prerequisites were satisfied, and that the test data was complete, appropriately verified, and met the requirements of the testing procedure. Following the completion of the test, where applicable, the inspectors conducted walkdowns of the affected equipment to verify that the test equipment was removed and that the equipment was returned to a condition in which it could perform its safety function.
The inspectors observed and reviewed the performance of the following surveillance testing on risk-significant equipment:
- Diesel Generator A Monthly Availability Test - October 4, 2002
- Service Water Train B Pump and Valve Quarterly In-Service Test (IST) -
October 23
- Component Cooling Water Train A Pump and Valve Quarterly IST -
November 8
- Component Cooling Water Train B Pump and Valve Quarterly IST -
November 21
- Containment Spray Train B Pump and Valve Quarterly IST - December 11
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
a. Inspection Scope
On November 19, 2002, the inspectors reviewed Temporary Change Request 02-017, Spool Piece Installed in Place of 1A Spent Fuel Pool Exhaust Fan. Temporary Change Request 02-017 installed a temporary spool piece in the spent fuel pool exhaust ventilation system to maintain a high-energy line break barrier during periods when the exhaust ventilation system boundary would be open for maintenance. The inspectors reviewed the licensees high-energy line break analysis and (USAR) Updated Safety Analysis Report to evaluate the adequacy of the temporary change request.
Additionally, the inspectors evaluated the adequacy of the tagout associated with the installation of the spool piece and observed portions of the maintenance on the associated exhaust fan.
b. Findings
No findings of significance were identified.
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspector reviewed Revision 26 to the Kewaunee Nuclear Power Plants Emergency Plan to determine whether changes identified reduced the effectiveness of the licensees emergency planning, pending onsite inspection of the implementation of these changes.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation
a. Inspection Scope
On December 17, 2002, the licensee performed an emergency planning drill. The drill was designed to exercise the licensees onsite and offsite emergency response organization and emergency plan. The inspectors observed portions of the drill from the control room simulator and the technical support center to evaluate the licensees evaluation, classification, and notification of the simulated event, including development and communication of protective action recommendations. The inspectors also attended the general drill debrief to determine whether the licensee was properly identifying drill weaknesses.
b. Findings
No findings of significance were identified.
SAFEGUARDS
Cornerstone: Physical Protection
3PP4 Security Plan Changes (71130.04)
a. Inspection Scope
The inspectors reviewed Revision 17 to the Kewaunee Nuclear Power Plant Security Manual Plan to verify that the changes did not decrease the effectiveness of the submitted document. The referenced revision was submitted in accordance with 10 CFR 50.54(p)(2) requirements by licensee letters dated October 18, 2002.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed the licensees performance indicator collection process and historical data from the fourth quarter of 2001 through the third quarter of 2002 to verify the accuracy of collected and submitted data for the performance indicators listed below. Additionally, the inspectors reviewed corrective action records, monthly operating reports, control room logs, and licensee event reports to independently verify the data that the licensee had collected.
- Safety System Unavailability - Safety Injection System, October 8, 2002
- Safety System Unavailability - Residual Heat Removal System, October 8
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Review of Identification and Resolution Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action system at an appropriate threshold, that adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Minor issues entered into the licensees corrective action system as a result of inspectors observations are generally denoted in the report.
b.
Issues No issues were identified.
.2 Review of Licensees Re-evaluation of NRC Bulletin 88-04 Response
Introduction and Description As part of the Selected Issue Follow-up Inspection of Inspection Procedure 71152, the inspectors selected CAP 192 (dated January 11, 2002) and an associated corrective action, CA 3209, for review to ensure that the corrective action had been implemented appropriately. Corrective Action Process 192 was written by the licensee to document the dead-heading of a component cooling water (CCW) pump under low flow conditions which occurred on January 10, 2002 (See Inspection Report 50-305/01-17 for additional details). Corrective action 3209, associated with CAP 192, required that the licensee review a previous response to the NRC regarding NRC Bulletin 88-04, Potential Safety-Related Pump Loss, dated May 5, 1988.Bulletin 88-04 documented industry concerns regarding pump miniflow designs. Specifically, one concern involved the potential for the dead-heading of one or more pumps in safety-related systems that have a miniflow line common to two or more pumps or other piping configurations that do not preclude pump-to-pump interaction during miniflow operation. A second concern was whether or not installed miniflow capacity was adequate for single pump operation.
The licensees summarized response to NRC Bulletin 88-04, as it applied to the CCW system, was that the component cooling water system was not vulnerable to this particular type of system failure. Contrary to the bulletin response, the CCW pumps were found to be susceptible to dead-heading during specific flow conditions on January 11, 2002. The inspectors evaluated the licensees review of the bulletin response to ensure that in addition to revisiting potential dead-heading of the CCW pumps that the licensee also re-evaluated their analysis of other safety-related pumps including residual heat removal pumps, auxiliary feedwater pumps, SW pumps, safety injection pumps, and containment spray pumps. The risk significance of this issue was previously evaluated and is documented in Inspection Report 50-305/02-03.
a.
Completion and Resolution of Corrective Actions
- (1) Inspection Scope The inspectors reviewed CAP 192; CA 3209; Root Cause Evaluation (RCE)02-002, Component Cooling Pump Deadheading; NRC Bulletin 88-04; Licensee Event Report 50-305/2002-001-00, Unanalyzed Condition: Strong Pump - Weak Pump Interaction Between Component Cooling Water Pumps; and Wisconsin Public Service Letter NRC-88-91, Initial Response to NRC Bulletin No. 88-04: Potential Safety-Related Pump Loss, dated July 8, 1988. The inspectors also interviewed licensee personnel
- (1) to assess the adequacy of the licensees re-evaluation of their response to Bulletin 88-04 to ensure that the CCW system was properly evaluated for potential miniflow design considerations and
- (2) to ensure that the initial evaluations associated with other safety-related systems were also re-evaluated by the licensee.
- (2) Issues No issues were identified.
.3 RCE 01-058, Failed Feedwater Regulation Valve Booster Causes Plant Trip
Introduction and Description As part of the Selected Issue Follow-up Inspection of Inspection Procedure 71152, the inspectors selected Root Cause Evaluation (RCE)01-058, Failed Feedwater Regulation Valve Booster Causes Plant Trip, for review to verify whether identified corrective actions had been appropriately dispositioned. Root Cause Evaluation 01-058 evaluated a plant trip due to a lowering water level on the B steam generator which occurred on June 20, 2001. The licensee identified that the cause of the lowering steam generator level was due to a failed volume booster associated with the main feedwater regulating valve. The licensee subsequently determined that the root cause for the failure was that there was no regular replacement schedule for volume boosters at the plant and that historically the boosters had only been replaced when they had become problematic or had failed.
a.
Completion and Resolution of Corrective Actions
- (1) Inspection Scope The inspectors reviewed RCE 01-058, Failed Feedwater Regulation Valve Booster Causes Plant Trip, dated August 8, 2001, reviewed the licensees corrective action program database, reviewed the licensees preventative maintenance program regarding volume boosters at the facility, and interviewed maintenance and work control planning personnel to determine the adequacy and dispostion of the corrective actions associated with RCE 01-058.
- (2) Issues No issues were identified.
40A5 Other Activities
.1 Completion of Appendix A to Temporary Inspection 2515/148, Revision 1, Inspection of
Nuclear Reactor Safeguards Interim Compensatory Measures The inspectors completed the pre-inspection audit for interim compensatory measures at nuclear power plants, dated September 13, 2002.
.2 Safeguard Document Request
The inspectors provided to the licensee the NRCs request regarding safeguards information.
.3 Institute of Nuclear Power Operations Training Accreditation Report Review
On December 4, 2002, the inspectors reviewed the most recent Institute of Nuclear Power Operations Training Accreditation Report for the licensees training program.
The report placed the licensees training program on probation.
4OA6 Meetings
Interim Exit Meetings Interim exits were conducted for:
- Safeguards Inspection with Mr. M. Fencl on October 29, 2002;
- Biennial Maintenance Rule Inspection (71111.12B) with Mr. T. Coutu, Site Vice President on December 6; and
- Licensed Operator Requalification (71111.11B) with Mr. Wyatt Godes, Operations Training Supervisor on December 19, via telephone.
Exit Meeting The resident inspectors presented the inspection results to Mr. T. Coutu and other members of licensee management on January 7, 2003. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
KEY POINTS OF CONTACT Nuclear Management Company, LLC L. Armstrong, Engineering Director S. Baker, Manager, Radiation Protection A. Bolyen, Licensing T. Coutu, Site Vice President, Kewaunee Site R. Farrell, Manager, Planning and Scheduling M. Fencl, Security Manager, Kewaunee/Point Beach D. Gauthier, Nuclear Oversight W. Godes, Operations Training Supervisor G. Harrington, Licensing Leader K. Hull, Supervisor, Engineering and Mechanical Design J. Ladewig, Engineering K. McCann, Engineering J. McCarthy, Assistant Plant Manager, Operations P. Miller, Engineering R. Nicolai, Corrective Actions K. Peveler, Nuclear Oversight S. Putman, Assistant Plant Manager, Maintenance R. Repshas, Manager, Site Services K. Schommer, Engineering J. Stafford, Superintendent, Operations C. Steinhardt, Engineering T. Webb, Regulatory Affairs LIST OF ACRONYMS USED AR Action Request CA Corrective Action CAP Corrective Action Process CCW Component Cooling Water CFR Code of Federal Regulations DRP Division of Reactor Projects DRS Division of Reactor Safety GNP General Nuclear Procedure JPM Job Performance Measure IST In-Service Test NOA Nuclear Oversight Assessment NRC Nuclear Regulatory Commission OWA Operator Workaround RCE Root Cause Evaluation SDP Significance Determination Process SSCs Structures, Systems, and Components SW Service Water USAR Updated Safety Analysis Report LIST OF
DOCUMENTS REVIEWED
1R01
Adverse Weather Protection
Relief Request IST-RR-23; IST Plan - Diesel Generator Fuel Oil Transfer Pumps;
Revision O
PMP 04-03; CW Recirculating Pump and Circulating Water Chlorine Monitoring Water
Pump Maintenance (QA-2); Revision H
Operations Department Instruction - Cold Weather Operation; December 13, 2001
NRC Information Notice 98-02; Nuclear Power Plant Cold Weather Problems and
Protective Measures
XK-185-1; Peerless Pump; June 12, 1969
N-ACA-17; Auxiliary Building Ventilation System; Revision Q
N-ACC-25; Control Room Air Conditioning System; Revision V
A-ACC-25; Abnormal Control Room A/C; Revision O
E-ACC-25; Emergency Control Room A/C System Operation; Revision N
USAR Section 9.6.3; Auxiliary Building Ventilation Systems; Revision 17
USAR Section 9.6.4; Control Room Air Conditioning System; Revision 17
OPERM-601; Flow Diagram - Turbine & Aux. Bldg. Ventilation; Revision CH
OPERM-603; Flow Diagram - Air Conditioning Administration Bldg & Control Room;
Revision AT
OPERM-604; Flow Diagram - Aux Building Zone SV Vent & Air Conditioning;
Revision BC
1R04
Equipment Alignment
N-SW-02-CL; Service Water System Prestartup Checklist; Revision AR
M-721; Flow Diagram Service Water System; Revision CP
N-DGM-10-CLA; Diesel Generator A Prestartup Checklist; Revision I
1R05
Fire Protection
PMP 08-14; Fire Protection (FP) Ionization Detector and Pull Station Operational Test -
Safeguards Zones; Revision G
CAP 13948; Problem Discovered with Fire System Impairment Compensatory Actions
FPP-08-17; Impairments to Active Fire Protection Systems; Revision B
Kewaunee Nuclear Power Plant Fire Protection Program Plan; Revision 4
FPP-08-08; Transient Combustibles; Revision A
PMP-08-32; Cable Spreading Area Sprinkler System Inspection; Revision C
PMP-08-33; FP-Penetration Fire Barrier Inspection; Revision D
1R06
Flood Protection Measures
Design Change Request 2873; Re-design of Process Piping for Radiation Monitors R-16
and R-20
CAP 13459; Failure of Turbine Building Pumps Could Result in Loss of Non-safeguards
Buses 1 and 2
1R07
Heat Sink Performance
PMP 1-11; DGM - Diesel Generator Cooling Water Heat Exchanger Performance
Monitoring; Revision B
1R12
Maintenance Effectiveness
Kewaunee Nuclear Power Plant System Health Report; October 2002
NAD-08.20; Maintenance Rule Implementation; Revision C; August 8, 2002
GNP-08.20.04; Maintenance Rule MRFF and MPFF Evaluations; Revision C;
November 26, 2002
FP-PA-ARP-01, Action Request Process; Revision 0; February 27, 2002
CAP003614, N-5000 on Valve Stem of AFW2A Causing Valve to Stick during Travel;
March 15, 2002
CAP011577, AFW2B Not Responding Properly; May 7, 2002
CAP011676, AFW System Discharge Check Valves, May 16, 2002
CAP012616, AFW Pump A Declared OOS Based on Radiography Results; August 16,
2002
CAP013104, CC Surge Tank Level XMTR 24041 Drift and Nonlinearity; September 26,
2002
CAP013517, Component Cooling Surge Tank Level Loop 618 is Not Properly
Calibrated; October 31, 2002
CAP012637, Unplanned LCO Entered Due to Failed Inverters; August 20, 2002
CAP012911, Computer-Inverter BRC109 Static Switch Transferred to Alternate Source
to Load; September 11, 2002
CAP013820, Battery Charger C Failure; September 27, 2002
CAP013440, Delays in Planned Work Stemming from Unplanned Auto Start of TDAFW
Pump; October 24, 2002
CAP013854, NRC Maintenance Rule Inspection Identified Procedure Problem;
December 4, 2002
CAP013855, NRC Maintenance Rule Inspection Identified Procedure Problem;
December 4, 2002
CAP013861, Significant NRC Observation: Kewaunee CA Deferral Appears Similar to
Davis-Besse
CAP013864, Maintenance Rule Procedure (GNP08.20.04) Deficient
CAP013893, MRE Determination for CAP011577; December 5, 2002
CAP013894, MRE Determination for CAP012011; December 5, 2002
CAP013896, MRE Determination for CAP013517; December 5, 2002
CAP013898, CAP Not Written for Condition Identified in CWO 02-0106443;
December 5, 2002
CAP013899, CAP Not Written for Condition Identified in CWOs 02-15491 and
2-15492; December 5, 2001
KSA-ENG-0202, Maintenance Rule Periodic Assessment - January 1, 2001 to
December 31, 2001; March 19, 2002
Maintenance Rule Periodic Assessment; Revision 2; February 1, 1999 to January 1,
2001; June 22, 2001
Maintenance Rule Quarterly Review; January 1 to March 31, 2001
Maintenance Rule Quarterly Review; April 1 to June 30, 2001
Maintenance Rule Quarterly Review; July 1 to September 30, 2001
Maintenance Rule Quarterly Report; January 1 to March 31, 2002
Maintenance Rule Quarterly Report; April 1 to June 30, 2002
Maintenance Rule Quarterly Report; July 1 to September 30, 2002
Audit 01-002, Maintenance Summary Second Quarter 2001
2002-004-2-037, Nuclear Oversight Observation Report - Engineering Programs;
December 5, 2002
Service Water Pump 75-TU-1719 Shaft Failure Investigation; February 1, 2001
Service Water Pump Inspection Action Plan; February 13, 2001
Service Water Pump Inspection Action Plan; May 1, 2001
Service Water Pump Inspection Action Plan; April 23, 2002
Maintenance Rule System Basis - Nuclear Instrumentation; Revision 1
KAP WO 02-15465; N-35 IR Channel Failed
SP 48-287A-2; Source Range N31 and Intermediate Range N35 Wide Range Amplifier
and Opto Isolator Calibration; Revision C
SSC Performance Criteria Sheet - Nuclear Instrumentation; Revision 2
Maintenance Rule Scoping Questions - Nuclear Instrumentation; Revision 2
E-2051-1; Integrated Logic Diagram Power Range Nuclear Instrumentation; Revision N
E-2051-2; Integrated Logic Diagram Source and Intermediate Range Nuclear
Instrumentation; Revision O
KAP WO 00-750; Receiving Annunciator 47033 SR/IR Non-Operate In Numerous
Repeated Bouts Causing a Control Room Distraction
N-DGM-10A; Diesel Generator A Manual Operation; Revision I
SP 42-312B; Diesel Generator B Availability Test; Revision Q
SP 42-047B; Diesel Generator B Operational Test; Revision U
CAP 11748; Auxiliary Building Basement FCU B Has Broken Belts
CAP 258; Auxiliary Building Mezzanine Fan Coil A Failed Its Performance Monitoring
1R14
Non-Routine Evolutions
N-0-03; Plant Operation Greater Than 35 percent Power; Revision AM
SP-54-086; Turbine Stop and Governor Valve Operability Test; Revision AE
SP-05B-284; Turbine Driven AFW Pump Full Flow Test - IST; Revision O.
1R15
Operability Evaluations
CAP 13380; Suspected Water Hammer Following TDAFW Pump Start
WR 02-2748; B Diesel Generator Speed Response Abnormal
USAR Section 8.2.3; Emergency Power; Revision 17
E-1621; Integrated Logic Diagram - Diesel Generator Mechanical System; Revision AL
E-1622; Integrated Logic Diagram - Diesel Generator Mechanical System; Revision V
E-1588; Schematic Diagram - Diesel Generator B Shutdown, Governor Control &
Auxiliary Relays; Revision AM
GMP-238; MOV Thrust and Torque Evaluations; Revision E
1R16
Operator Workarounds
OWA 01-08; AFW-4A(B) Often Leak Past Seat When Stopping AFW Following a Plant
Startup
OWA 01-16; Tagout 99-253. NRC Generic Letter 96-06 Valves Must Remain Open
When at or Above Hot Shutdown
OWA 01-22; SW-1306A(B) Fail Open on Power Supply Perturbations
OWA 02-01; Component Cooling Pump Overheating Concern in Two Pump Operation
with Normal At-Power Flows
1R19
Post-Maintenance Testing
XK414-1; Dimension Drawing Vacuum Breaker; Revision K
XK-414-11; Installation, Operating and Maintenance Instructions for Model LD-240-140
Vacuum Breaker; March 30, 1972
ICP-34-02; RHR - Heat Exchangers Bypass Control Loop 626 Calibration; Revision K
SP-34-099A; Train A RHR Pump and Valve Test - IST; Revision A
KAP WO 02-10237; Inspect/Clean Motor Starter
KNP Tagout Control Sheet 02-001157; RHR-400A - Perform Actuator Maintenance;
October 18, 2002
PMP 23-02; Containment Spray (ICS) QA-1 Motor Operated Valve Maintenance;
Revision K
Corrective Repair Procedure 05B-016497; Revision A
E-1490; Schematic Diagram 125 VDC CAB BRA-104 Motor 1-036; Revision V
E-1602; Integrated Logic Diagram - Auxiliary Feedwater; Revision AY
XK-100-147; Logic Diagram - Primary Coolant System Signals; Revision 4D
CAP 13380; Suspected Water Hammer Following TD AFW Pump Start
CAP 13376; TD AFW Pump Low Lube Oil Pressure Alarm
CAP 13374; Invalid TD AFW Pump Start
RT-DGM-10-TSC; Technical Support Center Diesel Generator; Revision V
GMP 236-03; Motor Operated Valve Diagnostic Testing Using the Universal Diagnostic
System; Revision B
GMP 238; MOV Thrust and Torque Evaluations; Revision E
GMP 236-02; Diagnostic Test Analysis and Acceptability Determination; Revision B
DCR 3205-1; Controller Surge Suppressors for SW-1306A
ICP-02-21; SW - Component Cooling Heat Exchanger 1A Temperature Control Loop;
Revision I
DC/PM 3205-1; Controller Surge Suppressors for SW1306A
E-2492; Schematic Diagram - Control valves CV-31406, 31407; Revision H
E-1632; Integrated Logic Diagram - Service Water System; Revision AH
E-1531; Wiring Diagram External Connection Solenoid & Control Valves TBs 1357,
1358, 1360, & 1391; Revision AJ
1R22
Surveillance Testing
CAP 13676; ICS-8A Operability Determination
SP-02-128B; Train B Service Water Pump and Valve Test - IST; Original Revision
SP-34-099A; Train A RHR Pump and Valve Test - IST; Revision A
PMP 23-02; Containment Spray (ICS) QA-1 Motor Operated Valve Maintenance;
Revision K
CAP 11902; Surveillance Procedure Conflict
SP 02-292; Service Water Pump Reference Values Determination; Revision F
SP-42-312A; Diesel Generator A Availability Test; Revision R
PMP 42-03; Train "A" Auto Sequencing Test with Diesel A; Revision N
USAR Section 8.2.3; Emergency Power; June 01, 2002
CAP 013181; Engine Water Temp (55003) Elevated during Performance of SP-47-312A
SP-02-138B; Train B Service Water Pump and Valve Test - IST; Original Revision
ASME Section XI; Rules for Inservice Inspection of Nuclear Power Plant Components;
1989 Edition
OMa-1988 Part 6; Inservice Testing of Pumps in Light-Water Reactor Power Plants
OMa-1988 Part 10; Inservice Testing of Valves in Light-Water Reactor Power Plants
SP-31-168A; Train A CC Pump and Valve Test - IST; Revision A
USAR Section 9.3; Auxiliary Coolant System; Revision 17
OPERXK-100-19; Flow Diagram - Auxiliary Coolant System; Revision AE
OPERM-202-2; Flow Diagram - Service Water; Revision CH
1EP4
Emergency Action Level and Emergency Plan Changes
Kewaunee Nuclear Power Plant Emergency Plan; Revision 26
1EP6
Drill Evaluation
Preliminary Drill Critique Report; December 17, 2002
EPIP-AD-02; Emergency Class Determination; Revision AE
EPIP-AD-07; Initial Emergency Notifications; Revision AR
EPIP-AD-19; Protective Action Guidelines; Revision R
3PP4
Physical Protection - Security Plan Change
Kewaunee Nuclear Power Plant Security Manual; Revision 17, dated October 18, 2002
4OA1 Performance Indicator Verification
NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 2
CAP 3217; Unavailability of Safety Injection and Residual Heat Removal Due to
Potential Unavailability of Component Cooling Water
Safety System Unavailability - Safety Injection System Data Sheets; 4th Quarter 2001
through 3rd Quarter 2002
Safety System Unavailability - Residual Heat Removal System Data Sheets; 4th
Quarter 2001 through 3rd Quarter 2002
Control Room Logs; 4th Quarter 2001 through 3rd Quarter 2002
4OA2 Identification and Resolution of Problems
ES-1.3; Transfer to Containment Sump Recirculation; Revision S
LER 2002-001-00; Unanalyzed Condition: Strong Pump - Weak Pump Interaction
Between Component Cooling Water Pumps; March 11, 2002
RCE000002; Investigate Cause of CCW Pump 1B Heating Up When Two Pump
Operation in Progress
RCE 02-002; Component Cooling Pump Deadheading; April 15, 2002
CA 3209; Perform and Document a Revised Evaluation of Bulletin 888-04
NRC Bulletin No. 88-04; Potential Safety-Related Pump Loss; May 5, 1988