IR 05000289/2018004
ML19036A887 | |
Person / Time | |
---|---|
Site: | Three Mile Island |
Issue date: | 01/31/2019 |
From: | Matt Young NRC/RGN-I/DRP/PB6 |
To: | Bryan Hanson Exelon Generation Co, Exelon Nuclear |
Young M | |
References | |
IR 2018004 | |
Download: ML19036A887 (13) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION ary 31, 2019
SUBJECT:
THREE MILE ISLAND NUCLEAR GENERATING STATION, UNIT 1 -
INTEGRATED INSPECTION REPORT 5000289/2018004
Dear Mr. Hanson:
On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Three Mile Island, Unit 1 (TMI). On January 11, 2019, the NRC inspectors discussed the results of this inspection with Ed Callan, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR ) Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Matthew R. Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket No. 50-289 License No. DPR-50
Enclosure:
Inspection Report 05000289/2018004 w/Attachment: Supplementary Information
Inspection Report
Docket Number: 50-289 License Number: DPR-50 Report Number: 05000289/2018004 Enterprise Identifier: I-2018-004-0079 Licensee: Exelon Generation Company Facility: Three Mile Island Station, Unit 1 Location: Middletown, PA 17057 Inspection Dates: October 1 through December 31, 2018 Inspectors: Z. Hollcraft, Senior Resident Inspector B. Lin, Resident Inspector J. Ambrosini, Senior Emergency Preparedness Inspector J. Bridge, Nuclear Systems Engineer R. Rolph, Health Physicist C. Hobbs, Reactor Inspector C. Safouri, Project Engineer Approved By: M. Young, Chief Reactor Projects Branch 6 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at
Three Mile Island, Unit 1 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
No findings or more-than-minor violations were identified.
PLANT STATUS
Unit 1 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Exelons performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04 - Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Protected system lineup during A train engineered safeguards 480V under voltage trip testing on October 2, 2018
- (2) Fire service piping during piping repairs downstream of valve FS-V-237 on October 2, 2018
- (3) Reactor building emergency cooling water system during testing of backpressure regulation valves RR-V-5 and RR-V-6 on November 28, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the decay heat river water system on November 14, 2018.
71111.05AQ - Fire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Fire Zone FH-FZ-5, Control Building Patio Area, 322 elevation on October 2, 2018
- (2) Fire Zone FH-FZ-5, Fuel Handling Building 380 elevation on November 1, 2018
- (3) Fire Zone AB-FA-2, B Decay Heat Vault on October 9, 2018
- (4) Fire Area DG-FA-2, Diesel Generator B Building on December 3, 2018
- (5) Fire Area CB-FA-2D, Control Building East Battery Charger Room on December 4, 2018
71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator requalification training on October 16, 2018.
71111.12 - Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Auxiliary building and heat exchanger vault on December 11, 2018
Quality Control (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
- (1) Decay river discharge valve DH-V-1A motor-operated valve (MOV) testing on October 30, 2018
71111.13 - Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unplanned maintenance on the fire service piping requiring excavation on October 2, 2018
- (2) Elevated risk for reactor coolant dropline isolation valve DH-V-3 breaker testing on October 9, 2018
- (3) A decay heat system outage window on October 30, 2018
71111.15 - Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Operability evaluation of B train nuclear service closed cooling pump NS-P-1B on October 1, 2018
- (2) Operability evaluation of A train decay closed cooling suction relieve valve DC-V-18A on October 11, 2018
- (3) Operability evaluation of fuel handling building supply fan AH-E-10 discharge boot on October 30, 2018
71111.18 - Plant Modifications
The inspectors evaluated the following plant modification:
- (1) Alternate reactor coolant system sampling with closure of CA-V-24
71111.19 - Post Maintenance Testing
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
- (1) A emergency diesel generator ventilation AH-D-17 maintenance on October 2, 2018
- (2) Reactor coolant drop line valve DH-V-3 circuit breaker testing on October 9, 2018
- (3) A decay river pump and discharge valve testing and maintenance on October 30, 2018
- (4) A building spray pump system outage window on November 10, 2018
- (5) B emergency feedwater pump planned maintenance on December 11, 2018
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: Routine
- (1) C reactor protection system functional testing on October 1, 2018
- (2) Reactor coolant dropline valve DH-V-3 breaker testing on October 9, 2018
- (3) B decay heat pump DH-P-1B on October 9, 2018
71114.04 - Emergency Action Level and Emergency Plan Changes
The inspectors verified that the changes made to the emergency plan were done in accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action Levels, Emergency Plan, and its lower-tier implementing procedures, had not resulted in any reduction in effectiveness of the Plan. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation Emergency Planning Drill
The inspectors evaluated the conduct of a routine Exelon emergency planning drill on October 16,
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls Contamination and Radioactive Material Control
The inspectors observed personnel and material exiting the radiologically controlled area at the Unit 1 control point. The inspectors observed personnel monitor alarm responses. The inspectors ensured Nationally Tracked Sources were accounted for and reported as required.
71124.03 - In-Plant Airborne Radioactivity Control and Mitigation
Self-Contained Breathing Apparatus (SCBA) for Emergency Use
The inspectors evaluated Exelons self-contained breathing apparatus program at Three Mile Island by reviewing maintenance records, observing control room operators, and observing the inspection an SCBA ready for issue.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
- (1) OR01: Occupational Exposure Control Effectiveness, October 2017 through October 2018
71152 - Problem Identification and Resolution Semiannual Trend Review
The inspectors reviewed the licensees corrective action program for trends that might be indicative of a more significant safety issue.
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Issue Report 4061160, corrective actions to prevent recurrence following a rod drop event
INSPECTION RESULTS
Observation 71152 Semi-Annual Trend Review The inspectors evaluated a sample of condition reports generated over the course of the past two quarters by departments that provide input to the quarterly trend reports. The inspectors determined that issues were appropriately evaluated by licensee staff for potential trends and resolved within the scope of the corrective action program. Inspectors noted an increase in the number of redundant rod control power supply failures during recent testing. The licensee also noted this increase and as an action for IR 4199429, determined that since infant mortality ended, on average one power supply has failed per year, but in 2018 four failed.
The licensee is working with the vendor to determine any possible cause for this increase.
The inspectors agreed with these actions and will review the results of the vendor determination.
Observation 71152 Follow-up of selected issues On October 10, 2017, during an ascension to full power following a refueling outage, control rod 5-7 dropped resulting in an immediate downpower and eventual shutdown for troubleshooting and repair. The root cause was determined to be inadequately addressed long term degradation of neoprene insulation on the control rod cable connections in the reactor building. The specific failed connector was replaced as an immediate corrective action and the plant restarted. A corrective action to replace seven connectors with a history of potential degradation was planned for the next forced or refueling outage. As a corrective action to prevent reoccurrence, the licensee would develop and implement inspection and testing to accurately assess the health of the cables and connectors. Due to the corrective action being to develop a program, inspectors selected it for a focused follow up problem identification and resolution (PI&R) sample to review the final plan.
The licensee developed three new testing protocols to be completed on all cables during every outage:
- A phase to phase and phase to neutral megger test of the control rod drive mechanism power cables from the output cabinet breakers to the connectors
- Connector phase to neutral phase resistance measurements of the connectors
- Durometer testing of the neoprene insulation to check hardness and indications of degradation Inspectors reviewed these new procedures and discussed plans for implementation with engineering staff. Based on the approval of these procedures, inspectors determined that the intent of the original corrective action to prevent reoccurrence appears to have been met.
The inspectors also noted the licensee has implemented other contingencies to replace the connectors if the original action is not effective.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 11, 2019, the inspector presented the quarterly resident inspector inspection results to Ed Callan, Site Vice President and other members of the licensee staff.
DOCUMENTS REVIEWED
71111.04: Equipment Alignment
Procedures
1104-45B, Fire Service Water System, Revision 107
OP-TM108-117-1001, TMI Protected System Equipment Program, Revision 4
OP-TM-534-901, Reactor Building Emergency Cooling Operations, Revision 14
OP-TM-534-000, Reactor Building Emergency Cooling Water System, Revision 5
OP-TM-534-210, IST of RR-V-5 and RR-V-6, Revision 2
Issue Report
4199723
Work Orders
4833884 4824286
Miscellaneous
IE-534-28-001, Reactor Building Emergency Cooling Water System Diagram, Revision 2
71111.05: Fire Protection
Procedures
AB-FZ-2, Aux. Building Elevation 261, B DH Vault & B BS Vault Pre-Fire Plan, Revision 2
FH-FZ-5, Fuel Handing Building Elevation 322; Control Building Patio Area, Revision 7
FH-FZ-5, Fuel Handling Building Elevation 380 Pre-Fire Plan, Revision 3
FH-FZ-5A, Fuel Handling Building Elevation 380 Pre-Fire Plan, Revision 3
FH-FZ-5B, Fuel Handling Building Elevation 380 Pre-Fire Plan, Revision 3
DG-FA-2, Diesel Generator Building EG-Y-1B Pre-Fire Plan, Revision 6
CB-FA-2D, Control Building Elevation 322 A Inverter Room Pre-Fire Plan, Revision 7
Issue Report
4184153
Miscellaneous
990-1745, Three Mile Island Unit No. 1 Fire Hazards Analysis Report, Revision 28
ESDS #: 2007-002, Equipment Storage Data Sheet for Scaffold Material Storage for EG-Y-1B
Maintenance, Revision 1
1-FHA-035, Fire Area Layout for Control Room Tower El. 322 and 338, Revision 17
1-FHA-044, Fire Area Layout for Diesel Generator Building, Revision 1
1-FHA-045, Fire Area Layout for Diesel Generator Building, Revision 1
71111.11: Licensed Operator Requalification Program
Miscellaneous
TQ-TM-104EP-2018, EP Drill 2018, October 9, 2018
71111.12: Maintenance Effectiveness
Miscellaneous
2705855-05, Internal Flooding Design Review, Revision 1
Topical Report 160, Maintenance Rule Structures In-Scope Inspection Report for Auxiliary
Building and Heat Exchanger Vault - CMT 614975, Revision 2
71111.13: Maintenance Risk Assessments and Emergent Work Control
Miscellaneous
Excavation Permit for FS-V-237 and piping repairs and replacement
71111.15: Operability Determinations and Functionality Assessments
Procedures
OP-TM- 543-000, Decay Heat Closed System, Revision
SM-AA-300-1001, Procurement Engineering Process and Responsibilities, Revision 23
Issue Reports
4180725 2453613 0175850 4189938
Miscellaneous
Operability Evaluation for Decay Closed Valve 18A, Decay Closed Pump 1A Suction Relief
Valve, Revision 1
CGD-T1-99-0001, Commercial Grade Dedication, Revision 1
MD-H168-001, Replacement of Relief Valve Numbers Dc-V-0018A, Revision 0
990-1536, Three Mile Island Pump Head Curves, Revision 17
71111.18: Plant Modifications
Procedure
N1807.1, Reactor Coolant & Pressurizer Sampling, Revision 20A
Miscellaneous
Engineering Change # 0000626546, RCS Additional Sample Path, Revision 0
Drawing # 302-671, Liquid Sampling
Drawing # 302-660, Makeup & Purification
71111.19: Post-Maintenance Testing
Procedures
OP-TM- 212-201, IST of DH-P-1B and Valves from ES Standby Mode, Revision 16
Work Orders
195919 4352176 4817669
71111.22: Surveillance Testing
Procedures
1303-4.2C, RPS Chanel C CRD Breaker and Test Module Testing, Revision 25
E-21, Thermal Overload Device Inspection and Testing, Revision 43
E-62.2, Molded Case Circuit Breaker and Replacement, Revision 6
OP-TM-543-202, IST of DC-P-1B, Revision 4
OP-TM-642-241, ES 480V UV Trip Test - Train A, Revision 4
Issue Report
4179109
Work Orders
4770133 195919
71114.06: Drill Evaluation
Miscellaneous
TQ-TM-104EP-2018, EP Drill 2018, October 9, 2018
71114.04: Emergency Action Level and Emergency Plan Changes
Evaluation 18-02, EP-AA-111/EP-CE-111, Emergency Classification and Protective Action
Recommendations, Revision 21-04
Evaluation 18-09, Drill and Exercise Procedure Changes
EP-AA-122-100, Drill and Exercise Planning and Scheduling, Revision 008
EP-AA-122-100-F-08, Pre-Exercise and NRC Exercise Checklist, Revision F
EP-AA-122-100-F-09, Off-Year Exercise Checklist, Revision D
EP-AA-122-100-F-10, Focus Area or Station Only Drill Checklist, Revision E
EP-AA-122-100-F-12, Hostile Action Based Exercise Checklist, Revision D
EP-AA-122-100-F-13, Call in Drill (CID) Checklist, Revision F
EP-AA-122-100-F-14, Drive in Drill (DID) Checklist, Revision F
EP-AA-122-300-F-01, Drill and Exercise Evaluation Criteria, Revision J
EP-AA-122-300-F-02, Drill and Exercise Objective Evaluation Summary, Revision F
Evaluation 18-75, TQ-AA-113, ERO Training and Qualification, Revision 34
71124.01: Radiological Hazard Assessment and Exposure Controls
Procedures
NISP-RP-007, Control of Radioactive Material, Revision 0
RP-AA-503-F-01, Unconditional Release Instructions Using the Small Articles Monitor (SAM) for
Personal Items Used in the Radiologically Controlled Area (RCA) and in a Contaminated
Area, Revision 004
Issue Reports
4147377 4168750 4175170 4186607
71124.03: In-Plant Airborne Radioactivity Control and Mitigation
Procedures
NISP-RP-003, Radiological Air Sampling, Revision 0
RP-AA-301, Radiological Air Sampling Program, Revision 11
RP-AA-825, Maintenance, Care and Inspection of Respiratory Protection Equipment, Revision 8
RP-AA-825-101, Monthly Inspection and Maintenance of MSA Firehawk Mask Mounted
Regulator SCBAs, Revision 0
RP-AA-825-101-1001, Operation and Use of the MSA Firehawk Self-Contained Breathing
Apparatus, Revision 0
Issue Reports
4167532 4179512
71152: Problem Identification and Resolution
Procedures
20-CRD-2, CRD Stator or Power Cable Troubleshooting and Repair, Revision 14
E-11, CRDM Resistance and Megger Readings, Revision 18
PI-AA-125, Corrective Action Program (CAP) Procedure, Revision 4
Issue Reports
4061160 4189938 4199429