IR 05000289/1976004
| ML19276H199 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 03/04/1976 |
| From: | Davis A, Kellogg P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML19276H198 | List: |
| References | |
| 50-289-76-04, 50-289-76-4, NUDOCS 7910150429 | |
| Download: ML19276H199 (5) | |
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- U. S. NUCLEAR REGULATORY CCMMISSION
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OFFICE OF INSPECTION AND ENFORCEMET
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REGION I
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u; IE Inspection Repcre No:
50-289/76- 04 Docket No:
50-289
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Licensee:
Metropolitan Edisen Ccacany License No:
DPR-50 P.O. Box 542 Priority:
C Reading. Pennsv1vania 19603 Category:
Safeguards Group:
Location: Middletown, Pennsv1vania (Three Mile Island 1)
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Type of Licensee:
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ype of Inspection:
Management Meeting Dates of Inspection:
March 2, 1976 Dates of Previous Inspection:
February 10-20, 1976 W
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Reporting Inspector:
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P.* J/
. vgg, R6 actor Inspector
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None Acco=panying Inspectors:
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Other Accompanying Personnel:
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See Meeting Attendees
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O Reviewed By:
i A. B. Davis, Section Chief, Reactor Projects gj+
Section No. 1 gi
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O S M.ARY OF FINDINGS
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Enforcement Action
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None
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Other Significant Finding s
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A.
Current Findings Not Applicable
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B.
Management Meeting
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T'ie =anage ent meeting required by the Trial Inspection Program was conducted at the Three Mile Island 1 site on March 2, 1976.
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The following personnel were in attendance:
Metrocolitan Edison Cenpany G
Mr. J. Colitz, Unit 1 Superintendent
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Mr. J. Herbein, Manager, Generation Operations - Nuclear
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Mr. J. Moran, Licensing Engineer ifr. C. S=yth, Licensing Engineer Nuclear Reculatory Cennission Mr. A. Davis, Section Chief, Reactor Projects Section 1 M..
P. Kellogg, Reactor Inspector Mr. F. Nolan, Senior Reactor Insp..: tion Specialist Sanida taberatories Mr. N. Brisbin. Project Manager Purpose and Score A =eeting was held with Met-Ed management to discuss the affect of the
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Trial Inspection Progran on the facility.
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Discussion Ite=s
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Specific ite=s discussed are su==arized below:
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Trial Inspection Program affect en the facility co= pared to pre-vious inspection efforts.
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1.
Met-Ed indicated that inspection frequency at first appeared f""
to be abnormally high.
Inspection frequency now has decreased
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to more nor=al levels.
2.
Met-Ed indicated that key personnel were involved in the Trial
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Inspection Program efforts on about the sa=e level as the previous inspection program.
Clerical personnel appeared to be expending more ti=e in supporting the Trial Program than in the previous inspection program.
A comparison of licensee manhours to support the Trial Inspection Program and the Routine Inspection Program was cuggested as a meaningful method of evaluating the Trial Inspection Program affect on
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the facility.
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Met-Ed indicated the diverse inspectors now conducting inspec-tions under the Trial Inspection Program were causing additional e__
time to be expended in retracing areas that had previously been resolved under the Routine Program.
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Trial Inspection Program effectiveness campared to previous inspec-
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tion efforts.
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Met-Ed indicated that it was premature at this point to state the effectiveness of the Trial Program co= pared to the Routine Program.
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An opinion was expressed that the Trial Program apparently removed some inspector lattitude with respect to judgement as compared to tie Routine Program.
The licensee was advised that his ce==ents/ concerns would be evaluated.
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PHILADELFEIA ELECT?.IC COMPA5Y Peach Hotto: Ato=ic Pever Station G
Delta. Pennsylvania l~* 31k Harch k,1976 Mr.
a=es P.
C'P.eilly, Director
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jffice of Inspectico and Enforce =ent
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'30 ited States Nuclea: Resulatory-Co==ission 2 t / e m h a d.
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631 Park Avenue AG-a-
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X. i n g c f Prus sia, Penssylxan ia.
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SU BJ EC7:
?EP037A3LE OCCURRINCT - PROMP7 5077FICAT*0N
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Confir= int W.
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Ullrich's phone conversation vith Mr. Vait 2aun a:k,
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negicn 1 United St at es, Ucclear Regulat ery Cc==i s s ion on March 3, 1776.
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?eferecce:
Docket. Su=her 350-277 Unit No. 2 Technical.3pecification Reference:
3.3.C.1 Report No.:
2-76-14/1P
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Oeeurr nce-Late: March 2/3, 1976
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identificatics of Occurrence:
Tots 1. airborne. activity release race exceeded. Technical Specification ifcits.
Jonditices Prior to Occurrence:
Unit 2 at 1005 power.
Steady state gaseous release rate of 32% of i Tech Sp e e li=it.
- Jescript.on of Occurrence:
On 3/2/T6., at 9:00 a.=..,
operation of the 23 =echanical co= pressor
assceinted vith the. Unit 2 reco=biner caused an increase in see Unit 3 Reactor Zuildd=t ve=tilstiew st ack releace rate.
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stack. activity was caused
'e y leaks frc= various c0=pe=ects s: 0:inted with the 23 =echanical.co= pressor.
The ce= pressor was i==ediately s h ut d own.
The =azi=a= release rate observed durist this period was 151% of Tec6 Epee li=it. Release. rates in excess of tce Teet spee:
, lasted fer approxi=ately tes.=i=utes.
Total curies relessed as a
.',r e s u.I t of the operatior. of this co= pressor at this ti=e was approx 1=ately*
+ 5 0Ls curies,
A Icah test vasiperfes.ed-en the co=pr.essor a=d several leati=g. gaskets replacei.
At.approri= ate 17 ',: 30 a.=.
ca.3/3/76 the e== press:r was agai=
placed i=. service..
This rescited in a=other i= crease in gaseous release rate i= excess of the Te c h c ic al Specifications.
Fest release rate a-
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this ti=e was 1975 of the "echnical Specification it=1t.
Release rate stove the Technical Specification li=it. lasted for approxi=ately 15 cinutes with a total activity release of 9.7 curies.
The 23 cc= presser was aEsin leak tested.
Severci additienni leats were identified a=1 corrected a=d the : =;ressor again returned te service.
Sta:t radiatio: 11 d so i=:rease,. and as a result of re=evi=g the 2A
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ce= press =r fr== service, actually decreaced to approxtcately :=e-quarte.-
of its original value.
Stesdy state gaseous release rate folleving repair o f this ::= pressor var 19% of : Tech Spee li=it.
Apparest Cause of Oc curre=ce:
Sa=ercus =i= r leaks associated with 2B =e:hanical ec= pressor.
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(Continued er,page 2)
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locjr #wmd Mr. Jsses P.
C'3eiL17, Director
.ce of *ccpection and Enforcement.
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Unitei States suelear P.cgulatory Co==ission Es 6 31 Farir. Avenue Fl2 King of Prussia. Pennsylrania 19L06
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SUBJECT:
P.EFOP.TABTE COCURP.E50E - PROMPT 507IFICATIC5
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?.e p c r t No. 2-76-14/IP
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A= a ly s is of the Occurrences Bas ed en the short duration of the activity relesse and the fact that h;
the caf, o r activi-ty was. Noble Gas es, the effects of this occurrence should be minicaL.
yf Ccrrective Action:
Corrective setice has.been effected as described abeve by correcting
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the lesks ide=tified.
. e ry truly yours, j
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Ullrich, S u p e rin t e n de n.c.
Peach Ec*tc= Atonic Power Statici
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