IR 05000320/1976019
| ML19220B806 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 12/27/1976 |
| From: | Finkel A, Keimig R, Narrow L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML19220B803 | List: |
| References | |
| 50-320-76-19, NUDOCS 7904270391 | |
| Download: ML19220B806 (13) | |
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Torn 12
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Osn 75) (Rev)
NO DEc 2 81976
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U. S. NUCLEAR RECUL\\TCRY CC:CIISSION
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OFFICE OF INSPECTION AND ENFORCD1ENT
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REGION I
'II Inspec tion Report No: _
Docket No.
50-320 50-32.0/76-19
- Licensee:
}fetropolitan Edison Cc=pany
License No:
CPPR-56
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Eca: 542 Priority:
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Reading, Pennsylvania 19603
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. Ca tegory:
i Safeguards
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Location:
Middletown, Pennsylvania (TMI-2)
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Type of Licensee:
Pk'R 959 }Ne f.B&'J)
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,6y, of Inspection: _
Routine, Unannounced
.; Dates of Inspection:
November 29 - Decenber 2, 1976
i Dates of Previous Inspection:
Nove=ber 15, 1976 i
Reporting Inspector:
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/78[4 L. Narrow, Reaq r Inspector
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Accompanying Inspectors:
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21hel, neJCtor inspeCLQr
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Other Accompanying Personnel:
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DATE Rmrieved B : /
R. R. reimigQ ef, Construction ProjectsSection I'LI'L'7 /'? b f
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/ *, Reactor Const tion and Engineering Scpport Branch,
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SU?^'ARY OF FIT INGS Enforcement Action Tte=s of Noncountiance Infraction 76-19-01 - Yailure to control specification and procedure changes.
Contrary to 10 CFR 50, Appendix B, Criterion V and General Construction Procedure GCP-1-2, construction depart =et :
and QC did not audit specifications and procedures and the velding department did not properly maintain and control these documents.
(Details, Paragraph 3)
t I.icensee Action on Previousiv Identified Enforce =ent Items i
None.
Desfun Changes
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None.
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Unusual Occurrences
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None.
Other Significant Findings
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A.
Current Findings 1.
Unresolved Items
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76-19-02 - Cable and Raceway installation.
(Details, Paragraph 4)
76-19-03 - Temporary rces of safety related cable.
(Details
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Paragraph 5)
76-19-03 - Fire in 'ITE notur control center.
(Details,
Paragraph 6)
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76-19-C5 - Chort. circuit in GE notor control center.
(Details,
Paragraph ?)
2.
Accentable Items GPU audits of electrical installation.
(Details, Paragraph 8)
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B.
Previously Reoorted Unresolved Items The following itens have been resolved:
1.
Engagenent of bolt threads in flanged piping connections.
(Details, Paragraph 4)
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2.
Hydrostatic test of condensate storage tank.
(De tails,
Paragraph 10)
3.
Inspection of rainforcing steel for da= age during concrete chipping.
(Details, Paragraph 11)
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. Inconplete records of preventive maintenance for electrical equipnent.
(Details, Paragraph 12)
5.
Battery room viring and lighting.
(Details, Paragraph 13)
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Deviations None (
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Exit Interview An exit interview was held at the site on Dece=ber 2, 1976.
Persens Present
_Ceneral Public Utilities Service Corporation R. P. Tenti, QA Auditor P. Karish. Electrical Engineer P. A. Levine, QA Auditor J. R. Stout, Electrical Resident Engineer M. J. Stromberg, Senior Site Auditor
E. J. Vermann, QA Engineer L. M. Zubey, Mechasiical Engineer
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United Engineers and Constructors
S. Abbott, Welding Supervisor i
J. J. Carrabba, Construction /QC Superintendent l
L. A. Dick, QC Ingineer, Electrical
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J. J. Karn, Piping Enginee:
D. C. Lanbert, Field Supervisor, QC D. S, Long, III, QC Electrical Coordinator T. M. Polen, Electrical Checker J. C. Spinak, Lead QC Engineer
_ Burns & Ree G. T. Harper, Jr., Site Proj ect Engineer E. M. Curry, QA Site Group Supervisor A.
Scone of Insoection The inspector stated that the inspection was conducted tc reviev
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the status of outstanding items and the QC program for electrical
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Inscection Findin g
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The inspector sarized the results of the inspect 1on as listed in the Su= mary of Findings. * In each case the licensee acknowledged i
the information.
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D_ETAILS 1.
Persons Contacted General Public Utilities Service Corporation R. 7. Fenti, QA Auditor S. Levin, Project Engineer F..L Levine, QA Auditor M. A. Nelson, Technical Engineer J. R. S tout, Electrical Resident Eogineer H. J.
tronberg, Senior Site Auditor J. R. Toole, Test Superintendent E. J. Wermann, QA Engineer United Engineers and Constructors
S. Abbott, Velding Supervisor D. Barker, Mecha: teal Technician B. A. Bozarth, QC Engineer J. Carrabba, Construction /QA Superintendent i,
R. Crofton, QC Engineer L. A. Dick, QC Engineer
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G. Edwards, Welding Supervisor M. Hocker Drawing and Docunent Control Clerk i
S. Kakarla, Lead Start-up Engineer J. Karn, Piping Engineer F. Kovalik, Office Engineer D. Lanbert, QC Supervisor
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D. Long, III, Electrical Coordinator J. Matthews, Office Engineer, Electrical J. Sch=1dt, Records Supervisor M. Shaw, Welding. Clerk R. Snith, Drauing Control Clerk J. Walck, Assistant Office Engineer Burns & Roe
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G. T. Harper, Site Project Engineer
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V. Burbure, Site Elec::rical and Liaison Engineer 2.
General i
At a pre-inspection neeting with the licensee's representatives, the inspector discussed the scope of the inspection. The status
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of outstanding '.tems was reviewed and the licensee's representative identified the ite=s which had been corrected.
The licensee's representative discussed the nreviously reported problems with the GE and ITE motor control centu 's.
The investigations were continu-ing and he stated that addditio.2al infor=ation would be furnished to the inspector as it became available.
The licensee's representa-tive also discussed progress of the work and s cated that the second shif t would be started during the week of December 6.1976 rathar than in January, 1977 as previously planned.
3.
Control of Soecifications and Procedures The inspector examined records of receipt, distribution and control of specifications and procedures by the organizations shown belov for conformance to the requirements of UE&C General Construction
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3, Procedure CCP-1-2, Rev.
Control."
42 " Drawing, Specification and Document
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Eneineering Deoartmen**
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i The inspector oranined record cards showing specifications and I
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procedures received and compare.d these with the Drawinb/
Specification and Revision Status list.
The inspector also
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avmined the docu=ent transmittal forms showing documents
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distributed to on-site organizations and noted selecte.d docu-ments for comparison with records of those organizations.
j records conformed to the requirenents of GCP-1-2.
The Start-Up Department
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The inspector armined copies of the document transmittal forms, j
logs of specifications and procedures, copies of the twice
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monthly audits perfomed and selacted copies of the specifications and procedures.
The records and documents selected conformed to
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Engineering records of documents distributed to this depart =ent.
The records and audits conformed to the requirements of GCP-1-2.
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Mechanical-Department i
I The inspector armined copies of specifications and procedures
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l trar.suittal forms and twice monthly audits as well as the card
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file of such documents received by the depart =ent.
The records
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I audits conformed to the requirements of GCP-1-2. The records and I
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Piping Denartment The inspector ami ed copies of the transmittal forms showing documents issued to this department by Engineering and the card file of documents maintained by the Piping Depart-
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.ecords of audits of specifications and procedures were not available and the inspector was informed that such audits were not conducted althougn drawing audits were conducted.
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This is contrary to Paragraph VIII.E.2 of GCP-1-2 which states
" Auditing in the Piping Departusc and Piping Pield Offi vill be performed at least once monthly, by the randam sa=nling ces
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method."
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Electrical Decartment
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The inspector examined copies of the transmittal forms, copies I
of selected specifications and procedures and the card file of j
these documents maintained by the department.
Records of audits of these documents by the depart =ent were not available and the inspector was informed that audits were conducted of
drawings only but not of. other docu=ents.
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Paragraph V.C.2 of GCP-1-2 which states "The Draving Control"his is contr
g clerk shall, audit all areas / personnel on the Interdepartmental
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Distribution Schedule by random sampling method at least once j
monthly."
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Welding Department i
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Records of specifications and procedures includ'ed the Quarterly
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j Index issued by Engineering and the Annual Status of Latest Approved Revision of Welding Procedures.
Neither current records of spe.ifications and procedures nor a copy of the
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transmittal form of such documents for the period June thru Fovember,1976 was available for review by the inspector.
i Specification No. 2555-134
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j Engineering records as furnishedAmendz'ent 1 which was listed on to the Welding Department and signed for as having been received was available in that department.
In addition recorda of audits of specifications
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and procedures by the Welding Depannt were not available
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for review by the inspector.
II.A.2 and II.C.1 of GCP-1-2 which state, ~respectively "A"These copy of transmittals " file vill be kept in the velding office..."
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"The Drawing Clerk shall perform a minimum of twice monthly ant"
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audits on a v,ndom sampling basis."
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OC Deeartment The inspector n mined records of audits by the QC Department of drawings, specifications and other technical docu=ents assigned to department offices and field drawing locations of
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the Piping and Electrical Departments. The inspector observed that audits of the Piping Department and the Welding Depart =ent had not been conducted on a monthly basis as required by GCP-1-2, Addendum A. Paragraph 2, Section C and that random sa=pling audits of the Electrical Department field drawing locations had not been conducted on a weekly basis as required by GCP-1-2, Addendum A, Paragraph 2, Section D.
Failure to perfor= audits of document control and to m2intain docu-ment control as required by GCP-1-2 is considered to be a noncon-I pliance of 10 CFR 50. Appendiz 3, Criterion V.
(76-19-01)
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cable and Racevav Installation During inspection of cable and raceway installation the inspector identified the following nonconfor=ing conditions:
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a.
Cable Installation
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During the inspection of the Cable Room and Control Room, the inspector found that the separation criteria insice Control Room cabinets and cable cross over areas were not being met.
The inspector also noted that barrier naterial used to maintain separation within cable trays carrying instrumentation and control cables did not pass through tees or around bends. Review of the
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'QC checklist showed that the t:
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2rovide a complete barrier am required by the separation cra.._
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.Racevwv Installation l
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During the inspection of the cable tray hangers, the inspector found that the installed hardware was not in accordance with
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the.equirements of UE&C drawing 9459.02-102474-E, Revision I.
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Engineering Instructions The Burns and Roe pull slips for cable pulls do not define the
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cable routing for " dropouts" from the point of'" dropout" to the
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equipment or next tray location.
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Cable Identification
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Cables leaving raceways and at intersections within racevays were not identified as required by Procedure ECP-3-2.
The inspector was informed that these nonconforming conditions had been identified during a licensee audit of electrical activities and confirned that they were included as findings
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in GPU Audit Report 76-14.
This item (76-1902) is unresolved pending review of corrective action by an NRC inspector.
Tecuerarv Runs of Safety Related Cabh
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During inspection of the cable room, the inspector rnted four safety-related cables, HH108C, EH1210, HH97C and HRlf.2C tied under a cable tray and tagged with a te=porary installation notice on the bundle. There is no procedure for pulling te=porary safety related cables and no controls to assure that no damage was done to the cable while in a temporary configuration. This fi'nding was t
identified during a licensee audit.
This item (76-19-03) is unresolved pending review of corrective
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action by an NRC inspector.
Fire in ITE Motor Control Center - Series 5600
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The licensee had reported a fire in ITE motor control center (MCC)
No. 11E3 on Nove=ber 22. 1976. Invesd.gation of thir fire indicates that during inserting of the combination st'arter/cf.re'u'it bisakeilidii a unit compartment one of the bifurcated" copper stiabs was misallised -
n1 ring a high resistance contact with the vertical bus bar. The copper stabs of the starter / circuit breaker module connects to the bus bars of the cabinet through slots in a fiber-glass polyester
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'~~ sate-1 1 ithin the unit compartment.~
The heat generated at the
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ar contact was sufficien't' to ignite the fiberglass polysster ma: -
rithin the unit compartment. This fire also caused a cover
over the horizontal bus bars of the MCC to ignite and bers.
mater
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i The MC contir_ued burning, even though the power to the center was l
trippe.1 out by the circuit breakers associated with this unit.
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- 9-The licensee is pr.esently taking the c.llowing action:
Inspect all Motor Control Centers Series $600 stab / bus bar a.
connections.
b.
Establish extent of cable da= age of safety related cables to MCC.
Esta*alish characteristics of materials used in the MCC.
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Establish schedule for installation of replacement MCC.
This item (76-19-04) remains unresolved pendi'rg review by an NRC inspector of installation of replacement MCC and associated safety related cables.
7.
Short Circuit in GE MCC - 7700 Line
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The licensee had reported a short circuit in GE MCC No. 21E3 on November 17, 1976.
- At the time of this inspection, the investigation was not co=plete i
but the following are considered to have contributed to the short circuit:
The power cables connect to the horizontal bus bars of the a.
cabinet through the top entry position. During connection of the power cables t3 the bus bar connectore within the
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cabinet, one of the esanectors was bent toweds t' a rear of
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the cabinet, thus reducing the air gap.
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Cors drilling of the floor above the MCC had been completed recently an ' a water / cement slurry had run down the conduits
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and into tia bus bar conpartment of the MCC.
k h two workmen vere tagging wires within MCC 21EB, a third c.
. man working on cable trays nearby stepped on top of a cabinet
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adjacent to the MCC. The weight of this nan on top of the cabinet apparently caused a slight move =ent of the vall of
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Cabinet 21E3.
This movem'ent in conbination with the reduced air gap is considered to have been sufficient te have caused a short he'veen one of the bus bars and the metal cabinet.
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short melted the vertical bus bar and the viring within the cabinet and also injured the two men working in front of the
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cabinet.
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The main breakers to the MCC vere tripped and power was removed from the MCC.
It was noted that the. ground fault relay was not in the circuit due to a -construction related condition.
g This iten (76-19-05) is unresolved pending review of the report and corrective action plan by an NRC inspector.
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B.
GPU Audits of Electrical Installation The inspector revie.e4 tha. records of the last two QA audits (Audit Reports 75-32 and 76-14) associated with electric cable installation, cable tray and conduit. These records confir=ed that the audits were performed and that deficiencies identified during these audits were documented and corrective action either was completed or in process c,f being acted on.
No discrepancies were identified.
9.
Bolt Thrend Enragement Insufficient engagement of bolt threads on flanged connectionn in the Decay Heat (DH) system had been identified as an unresolved iten.
(Inspection Report 50-320/76-01)
Engineering Change Memo (ECM) Ho.1552, Rev. I dated February 23,
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1976 which reviced specifications 2555-64 and 2555-72 to read
" Length (of thread) shall be sufficient to expose any visible portion of thread beyond the b maring surface of. the nut af ter
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each assembly."
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Quality Control Final Accept.tuce Inspection Check List (for
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piping systems) which had been revised August 3,1976 ti. add a requirement that proper thread engagement of bolted connections be verified.
Quality Control Inspection Report (QCIR) No. W-2372 which c.
verified t. hat thread engagement of DH flanges met the require-
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ments of specification 2555-72 and ECM 1552 af ter corrective action.
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QCIE No. W-2583 which verified thread engagement for systes which had been inspected prior to revision of the final acceptance check list.
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slso audited selected bolted connections in the Nuclear Service Closed Cooling System and the Nuclear Service River Water The inspecto-System and observed that threaded connections met the require::lents of ECM No. 1552.
This item is resolved.
Evdrostatic Test of Condensate Storage Tank _
10.
2555-72 with resweet to field testing Discrepancies in specificationof the condensate storage tank had been ide it e:1.
(Inspection Report 50-320/76-08)
2555-72
..ich The inspector examined revision 52 to specification corrected the test requirements to identify Paragtaph ND-61J.O of ASME Section III, Winter 1971 Addenda as the appropriate requirement.
This paragraph in turn invokes the requirements of NC-6500 of the B&R memo dated September 16, 1976 statc. that the ASME III Code.
hydrostatic test was performed in accordance with the requirements of ASME Section IIT., Winter 1971 Addenda using the test procedure of NC-6540.
This item is resolved.
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Insuection of Reinforcing Steel for Damage 11.
Minoc damage to reinforcing steel during chipping of concrete and i
lack of a requirement for inspection of the steel had been identi-fled as an une..olved item.
(Inspection Report 50-320/76-15)
The inspector examined the following documents:
Deviation Report (DR) No. 0605 with Supplements 2 and 3 docu-menting an inspection of the rebar in the fuel transfer tube a.
blockout and identifying the marks to be generally less than 1/16 inch deep vich seme da= age up to 1/8 inch.
Attached to the DR was Test Report No. P6.5549 by Pittsburgh Testing Laboratory (FIL) of a test on No.11 rebar with nicks
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All of the bars net the specification of 1/16, 1/8 and 3/16 inch.
requirements of the cat
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based on the results of the PTL test.
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Field Change No. QC-218 to OC Procedure QC-1-2 for General
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Construction and Structural Concrete adds an inspection
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point for da= aged rebar to the inspector's concrete check sheet.
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The check sheet has added an item requiring that rebar be free
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of surface defects.*
This item is resolved.
Incenolete Records of Preventive Maintenance Waiving of pre entive maintenance checks folleving turnover to test v
and startup group had been identified as an uneasolved item.
(Inspec-tion Report 50-32C/76-15)
Preventive Maintenance Specification SP-4 has been revised (TCN-2)
to add Paragraph 5.5 which requires that the date of operation shall be shown on the Preventive Maintena ce Card as a record of the equip-ment having been operated during the period.
This item is resolved.
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Batterv Rocm Wiring and Lighting
Review of a possible requirement for use of explosion proof equipment l
in the battery rooms had been identified as an unresolved item.
(Inspection Report 30.-320/76-12)
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By memo dated October 7,1976, B&R states that H7AC calculations indicate that during normal operation a minimum of 2 efs of fresh air is required tn eliminate a potentially hazardous atmosphere and that even under completely ait tight conditions a potentially hazardous atmosphere vould not be present until 12 days af ter cessation of all ventilation. Examination of the HVAC flow diagram showed that
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the battery room ventilation system includes two, supply fans and an i
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, exhaust fan.
This meets the dasign criteria.
i This item is resolved.
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