IR 05000282/2001018

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IR 05000282/2001-018 & IR 05000306/2001-018, Prairie Island, Inspection on 11/16-12/29/2001 Re Resident Inspector & Licensed Operator Requalification Program. No Violations Noted
ML020170480
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 01/17/2002
From: Lanksbury R
Division Reactor Projects III
To: Nazar M
Nuclear Management Co
Ray S
References
IR-01-018
Download: ML020170480 (25)


Text

January 17, 2002

SUBJECT:

PRAIRIE ISLAND NUCLEAR GENERATING PLANT NRC INSPECTION REPORT 50-282/01-18; 50-306/01-18

Dear Mr. Nazar:

On December 29, 2001, the NRC completed an inspection at your Prairie Island Nuclear Generating Plant. The enclosed report documents the inspection findings which were discussed on December 27, 2001, with Mike Werner and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

No findings of significance were identified.

Immediately following the terrorist attacks on the World Trade Center and the Pentagon, the NRC issued an advisory recommending that nuclear power plant licensees go to the highest level of security, and all promptly did so. With continued uncertainty about the possibility of additional terrorist activities, the Nation's nuclear power plants remain at the highest level of security and the NRC continues to monitor the situation. This advisory was followed by additional advisories, and although the specific actions are not releasable to the public, they generally include increased patrols, augmented security forces and capabilities, additional security posts, heightened coordination with law enforcement and military authorities, and more limited access of personnel and vehicles to the sites. The NRC has conducted various audits of your response to these advisories and your ability to respond to terrorist attacks with the capabilities of the current design basis threat (DBT). From these audits, the NRC has concluded that your security program is adequate at this time. In accordance with 10 CFR 2.790 of the NRC's Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/NRC/ADAMS/index.html (the Public Electronic Reading Room).

Sincerely, Original signed by Roger D. Lanksbury Roger D. Lanksbury, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-282; 50-306 License Nos. DPR-42; DPR-60

Enclosure:

Inspection Report 50-282/01-18; 50-306/01-18

REGION III==

Docket Nos:

50-282, 50-306 License Nos:

DPR-42, DPR-60 Report No:

50-282/01-18; 50-306/01-18 Licensee:

Nuclear Management Company, LLC Facility:

Prairie Island Nuclear Generating Plant Location:

1717 Wakonade Drive East Welch, MN 55089 Dates:

November 16 through December 29, 2001 Inspectors:

S. Ray, Senior Resident Inspector S. Thomas, Resident Inspector D. Karjala, Resident Inspector D. McNeil, Senior Operations Specialist Approved by:

Roger D. Lanksbury, Chief Branch 5 Division of Reactor Projects

SUMMARY OF FINDINGS IR 05000282-01-18; IR 05000306-01-18, on 11/16-12/29/2001; Nuclear Management Company, Prairie Island Nuclear Generating Plant, Units 1 & 2, Resident Inspector and Licensed Operator Requalification Program Report.

This report covers a 6-week routine resident inspection and an inspection of the licensed operator requalification program. The inspections were conducted by resident inspectors and a senior operations specialist. No findings of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described at its Reactor Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/index.html. Findings for which the SDP does not apply are indicated by No Color or by the severity level of the applicable violation.

A.

Inspector-Identified Findings No findings of significance were identified.

B.

Licensee-Identified Findings No findings of significance were identified.

Report Details Summary of Plant Status Unit 1 was operated at or near full power for the entire inspection period except that power was reduced to about 40 percent on December 2-3, 2001, for quarterly turbine valve testing. Unit 2 was operated at or near full power for the entire inspection period.

1.

REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness 1R01 Adverse Weather Protection (71111.01)

a.

Inspection Scope The inspectors conducted plant walkdowns and document reviews to verify that the risk significant systems were adequately protected against impending cold weather. The residents concentrated on the condensate storage tank (CST) heating system, the instrument air compressor cooling system, and the ventilation systems for the emergency and security diesel generator rooms. The inspectors used the licensee checklists and procedures listed at the end of this inspection report to verify that the systems were lined up as required. In addition, the inspectors reviewed the condition reports (CRs) and work orders (WOs) listed at the end of this report to verify that the licensee had entered problems identified with cold weather operations into the corrective action system and was taking the appropriate compensatory actions.

b.

Findings No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a.

Inspection Scope The inspectors performed a walkdown of the 21 shield building ventilation train to verify that the redundant train was in the correct lineup while the 22 shield building ventilation train was inoperable due to a failed surveillance test. The inspectors used the checklist and drawing listed at the end of this report to determine the correct lineup. The inspectors also reviewed outstanding WOs and CRs associated with the 21 train to verify that these documents did not reveal issues that could affect train function.

Significant WOs and CRs reviewed are listed at the end of this report. The inspectors used the information in the sections of the Updated Safety Analysis Report (USAR) and Technical Specifications (TSs) listed at the end of this report to determine the functional requirements of the system. During the walkdown, the inspectors also observed the

material condition of the equipment to verify that there were no significant conditions not already in the licensees work control system.

b.

Findings No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Area Walkdowns a.

Inspection Scope The inspectors conducted walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events (IPEEE), their potential to impact equipment which could initiate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed at the end of this report, the inspectors walked down the areas to verify that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The following areas were inspected:

!

Fire Area 41: screenhouse ground floor, elevation 670';

!

Fire Area 41: plant screenhouse, elevation 695';

!

Fire Area 35: 21 battery room, elevation 695'; and

!

Fire Area 36: 22 battery room, elevation 695'.

b.

Findings No findings of significance were identified.

.2 Fire Brigade Drill a.

Inspection Scope The inspectors observed the performance of a fire brigade drill in the Unit 1 hydrogen seal oil area. This area was considered risk significant because a fire could cause a unit trip initiating event. The inspectors observed the initial response of the control room operators to the fire alarm, the brigade turnout and organization in the brigade dressing area, and the establishment of communications between the brigade and the control room. The inspectors also observed the fire brigades response to the simulated fire, the brigade leaders command and control, and the brigades use of fire fighting

equipment. At the conclusion of the drill, the inspectors observed the licensees drill critique to ensure that any weaknesses noted during the drill were addressed and/or entered into the licensees corrective action system. In addition to the NRC inspection procedure listed above, the inspectors used the licensees Fire Drill Criteria Checklist and other documents listed at the end of this report for the evaluation.

b.

Findings No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1 Facility Operating History a.

Inspection Scope The inspectors reviewed the plants operating history from January 2000 through November 2001, to assess whether the Licensed Operator Requalification Training (LORT) program had addressed operator performance deficiencies noted at the plant.

b.

Findings No findings of significance were identified.

.2 Licensee Requalification Examinations a.

Inspection Scope The inspectors performed a biennial inspection of the licensees LORT program. The inspectors reviewed the annual requalification operating and written examination material to evaluate general quality, construction, and difficulty level. The operating portion of the examination was inspected during December 3 - 7, 2001. The operating examination material consisted of two dynamic simulator scenarios and five job performance measures (JPMs). The biennial written examination was administered between September 28 and November 2, 2001. The biennial written examination material included approximately 35 open reference, multiple-choice questions on each examination. The inspectors reviewed the methodology for developing the examinations, including the LORT program two-year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications. The inspectors assessed the level of examination material duplication during the current year annual examinations with last years annual examinations. The inspectors also interviewed members of the licensees management and training staff and discussed various aspects of the examination development.

b.

Findings No findings of significance were identified.

.3 Licensee Administration of Requalification Examinations a.

Inspection Scope The inspectors observed the administration of the requalification operating test to assess the licensees effectiveness in conducting the test and to assess the facility evaluators ability to determine adequate performance using objective, measurable performance standards. The inspectors evaluated the performance of one operating shift crew and one administrative crew during two dynamic simulator scenarios and five JPMs in parallel with the facility evaluators. The inspectors observed the training staff personnel administering the operating test, including pre-examination briefings, observations of operator performance, individual and crew evaluations after dynamic scenarios, techniques for JPM cuing, and the final evaluation briefing for licensed operators. The inspectors noted the performance of the simulator to support the examinations. The inspectors also reviewed the licensees overall examination security program.

b.

Findings No findings of significance were identified.

.4 Licensee Training Feedback System a.

Inspection Scope The inspectors assessed the methods and effectiveness of the licensees processes for revising and maintaining its LORT program up-to-date, including the use of feedback from plant events and industry experience information. The inspectors interviewed licensee personnel (operators, instructors, training management, and operations management) and reviewed the applicable licensees procedures. In addition, the inspectors reviewed the licensees quality assurance/quality control oversight activities, including the licensees training department self-assessment reports, to evaluate the licensees ability to assess the effectiveness of its LORT program and to implement appropriate corrective actions.

b.

Findings No findings of significance were identified.

.5 Licensee Remedial Training Program a.

Inspection Scope The inspectors assessed the adequacy and effectiveness of the remedial training conducted during the annual requalification examinations to ensure that the training addressed weaknesses identified in licensed operator performance. The inspectors reviewed the licensees current examination cycle remediation packages for unsatisfactory operator performance on the written examination to ensure that

remediation and subsequent re-evaluations were completed prior to returning individuals to licensed duties.

b.

Findings No findings of significance were identified.

.6 Conformance with Operator License Conditions a.

Inspection Scope The inspectors evaluated the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensees program for maintaining active operator licenses to assess compliance with 10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance for tracking on-shift hours for licensed operators and designating which control room positions were granted credit for maintaining active operator licenses. The inspectors also reviewed 20 licensed operators medical records maintained by the facility to ensure the medical fitness of its licensed operators and to assess compliance with medical standards delineated in ANSI/ANS-3.4 and with 10 CFR 55.21 and 10 CFR 55.25. In addition, the inspectors reviewed the licensees LORT program to assess compliance with the requalification program requirements as described by 10 CFR 55.59(c).

b.

Findings No findings of significance were identified.

.7 Written Examination and Operating Test Results a.

Inspection Scope The inspectors reviewed the pass/fail results of individual written tests, operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2))

administered by the licensee during calender year 2001.

b.

Findings No findings of significance were identified.

1R12 Maintenance Rule Implementation (71111.12)

a.

Inspection Scope The inspectors reviewed systems to verify that the licensee properly implemented the maintenance rule for structures, systems, or components (SSCs) with performance problems. This evaluation included the following aspects:

!

whether the SSC was scoped in accordance with 10 CFR 50.65;

!

whether the performance problem constituted a maintenance rule functional failure;

!

the proper safety significance classification;

!

the proper 10 CFR 50.65(a)(1) or (a)(2) classification for the SSC; and

!

the appropriateness of the performance criteria for SSCs classified as (a)(2) or the appropriateness of goals and corrective actions for SSCs classified as (a)(1).

The above aspects were evaluated by using the maintenance rule scoping and report documents listed at the end of this report. For each SSC reviewed, the inspectors also reviewed significant WOs and CRs listed at the end of this report to verify that failures were properly identified, classified, and corrected and that unavailable time had been properly calculated. In addition, the inspectors reviewed CRs to verify that minor deficiencies identified during these inspections were entered in the licensees corrective action system.

The inspectors reviewed the licensees implementation of the maintenance rule requirements for the following SSCs:

!

circulating water system, and

!

D1 and D2 emergency diesel generators.

b.

Findings No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or activities during a time when more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety significant equipment. The inspection was conducted to verify that evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration, where practical, and that contingency plans were in place, where appropriate. The licensees daily configuration risk assessments, observations of shift turnover meetings, observations of daily plant status meetings, and the documents listed at the end of this report were used by the inspectors to verify that the equipment configurations had been properly listed, that protected equipment had been identified and was being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel.

The inspectors reviewed the following maintenance activities:

!

planning and actions to monitor and increase the seal leakoff flow from the 22 reactor coolant pump, and

!

planning and work control associated with the work on breaker for MV-32238.

b.

Findings No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope The inspectors selected CRs for risk significant components and systems in which the operability issues were discussed. These CRs were evaluated to determine whether the operability of the components and systems was justified. The inspectors compared the operability and design criteria in the appropriate sections of the TSs and USAR to the licensees evaluations presented in the CRs below and documents listed at the end of this report to verify that the components or systems were operable. Where compensatory measures were necessary to maintain operability, the inspectors reviewed of the documents listed at the end of the report to verify that the measures were in place, would work as intended, and were properly controlled.

The CRs evaluated were:

!

CR 200186696, Lineshaft and Suction Bell Float Switches for the 12 Diesel-Driven Cooling Water Pump Are Stuck in the 90-100 Percent Flow Position - No Alarm Will Sound on Loss of Flow, and

!

CR 200186163, Evaluate Westinghouse 9 November 01 Letter for Effect on Plant.

b.

Findings No findings of significance were identified.

1R16 Operator Workarounds (71111.16)

.1 Review of Selected Workarounds a.

Inspection Scope The inspectors reviewed an operator workaround associated with the safety injection mini recirculation line flowmeters being out-of-service. This review was performed to determine whether a mitigating system function of the operators ability to implement abnormal operating procedures was affected. This workaround was selected because with the flowmeters out-of service, the safety injection mini-recirculation line Lo/No flow alarms were also out-of-service. This workaround represented a potential increase in the possibility of safety injection pump damage because of the resultant increased reliance on operator actions to identify that adequate pump discharge or bypass flow existed, subsequent to a pump start, and to secure the pump before pump damage occurred.

b.

Findings No findings of significance were identified.

.2 Cumulative Effects of Operator Workarounds a.

Inspection Scope The inspectors reviewed the cumulative effect of all identified operator workarounds to determine whether the cumulative conditions had a significant impact on plant risk or on the operators ability to respond to a transient or an accident.

b.

Findings No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a.

Inspection Scope The inspectors reviewed post-maintenance testing activities associated with maintenance on important mitigating and support systems to ensure that the testing adequately verified system operability and functional capability with consideration of the actual maintenance performed. The inspectors used the appropriate sections of the TSs and the USAR, as well as the documents listed at the end of this report, to evaluate the scope of the maintenance and verify that the post-maintenance testing performed adequately demonstrated that the maintenance was successful and that operability was restored. In addition, the inspectors reviewed CRs to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system.

Testing subsequent to the following activities was observed and evaluated:

!

2RX bus fault repair; and

!

operational testing of MV-32085 [Motor-Operated Valve for Refueling Water Storage Tank to 12 Residual Heat Removal Pump] subsequent to planned maintenance on its electrical supply breaker.

b.

Findings No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope The inspectors witnessed selected surveillance testing and/or reviewed test data to verify that the equipment tested using the surveillance procedures (SPs) met TSs, the

USAR, and licensee procedural requirements, and also demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in verifying mitigating systems capability. The inspectors used the documents listed at the end of this report to verify that the testing met the TS frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. In addition, the inspectors conducted reviews to verify that minor deficiencies identified during these inspections were entered into the licensees corrective action system.

The following tests were observed and evaluated:

!

SP 1112, Steam Exclusion Monthly Damper Test, and

!

SP 2088B, Train B Safety Injection Quarterly Test.

b.

Findings No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope On December 4, 2001, the inspectors observed licensee requalification examinations in the control room simulator. During the examinations, the inspectors observed the licensee make three event classifications and three notifications. Protective action recommendations were not required nor made. The inspectors attended the licensee evaluators critique of the examinations to ensure that any weaknesses were documented and addressed.

b.

Findings No findings of significance were identified.

4.

OTHER ACTIVITIES 4OA1 Performance Indicator (PI) Verification (71151)

a.

Inspection Scope The inspectors reviewed for completeness and accuracy the PI data submitted by the licensee for the Emergency AC [alternating current] Power Systems PI in the Mitigating Systems cornerstone. The inspectors compared the data reported by the licensee to the definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 1. The inspectors reviewed the computerized Limiting Conditions for Operation Log, Control Room Log, and Hold and Secure Card Log to gather information regarding unavailable times for the

emergency diesel generators, and compared those times to the data reported by the licensee.

b.

Findings No findings of significance were identified.

4OA3 Event Followup (71153)

.1 (Closed) Licensee Event Report (LER) 2-01-03, Revision 1 and (Closed) LER 2-01-03, Revision 2: Technical Specification Required Shutdown of Unit 2 Due to Declared Inoperability of Both Emergency Diesel Generators.

This event was discussed in Special Inspection Report 50-306/01-13. The event is considered to be of very low risk significance based on the results of a Regulatory Conference documented in NRC letter to Mr. Mano Nazar dated December 11, 2001.

.2 (Closed) LER 1-01-03: Plant In Unanalyzed Condition Due to Flood Panel Deficiencies.

This event report described a licensee-identified condition where 16 of 17 flood panels, which are installed during a flood condition where water level crest is predicted to exceed 692' elevation, were degraded. The issues included not having the correct gasket materials, inadequate anchor bolt installation capabilities, and the inability to install the panels in a timely manner.

The SDP Phase 1 screening assumed the loss of long-term reactor heat removal capability. Since the plant-specific SDP Phase 2 worksheets do not currently include initiating events related to the licensees Individual Plant Examination of External Events analysis (i.e., external flooding), a Phase 3 risk assessment was completed using information from the IPEEE.

Based on the assessment, it was determined that the issue was of very low risk significance (Green) due to the low probability of an external flooding event that reached the 695' elevation, the use of existing procedures that monitored areas vital to critical plant equipment, and the sufficient amount of time (five days) the licensee had after the external flooding conditions began to successfully complete compensatory actions prior to reaching the 695' elevation. The licensee entered the issue into its corrective action system as CR 20015571.

4OA6 Meeting(s)

Exit Meeting The resident inspectors presented the inspection results to Mr. M. Werner and other members of licensee management on December 27, 2001. The licensee acknowledged the findings presented. No proprietary information was identified.

Interim Exit Meeting Senior Official at Exit:

Mano Nazar, Site Vice President Date:

December 7, 2001 Proprietary (explain yes)

No Subject:

Results of an inspection of the licensees licensed operator requalification program Change to Inspection Findings:

No

KEY POINTS OF CONTACT Licensee T. Allen, General Superintendent Plant Operations T. Amundson, General Superintendent Engineering T. Breene, Manager Nuclear Performance Assessment B. Jefferson, Director Site Operations A. Johnson, General Superintendent Radiation Protection and Chemistry L. Meyer, General Superintendent Plant Maintenance M. Nazar, Site Vice President J. Waddell, Superintendent Security M. Werner, Plant Manager L. Williams, Director Site Engineering NRC S. Ray, Senior Resident Inspector, Prairie Island LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED Opened None.

Closed 2-01-03 Revision 1 LER Technical Specification Required Shutdown of Unit 2 Due to Declared Inoperability of Both Emergency Diesel Generators (Section 4OA3.1)

2-01-03 Revision 2 LER Technical Specification Required Shutdown of Unit 2 Due to Declared Inoperability of Both Emergency Diesel Generators (Section 4OA3.1)

1-01-03 LER Plant In Unanalyzed Condition Due to Flood Panel Deficiencies (Section 4OA3.2)

Discussed None.

LIST OF ACRONYMS USES AC Alternating Current ADAMS Agencywide Documents Access and Management System ANS American National Standard ARP Annunciator Response Procedure CFR Code of Federal Regulations CR Condition Report CST Condensate Storage Tank DRS Division of Reactor Safety DRP Division of Reactor Projects ICPM Instrumentation and Controls Preventive Maintenance IMC Inspection Manual Chapter IPEEE Individual Plant Examination of External Events IR

Inspection Report

JPM

Job Performance Measure

LER

Licensee Event Report

LORT

Licensed Operator Requalification Training

LOCA

Loss of Coolant Accident

NCV

Non-Cited Violation

NOMS

Nuclear Operations Management System

NEI

Nuclear Energy Institute

NRC

Nuclear Regulatory Commission

PARS

Publicly Available Records

PI

Performance Indicator

PINGP

Prairie Island Nuclear Generating Plant

PITC

Prairie Island Training Center

RCP

Reactor Coolant Pump

SAT

Systems Approach to Training

SBLOCA

Small-Break Loss of Coolant Accident

SDP

Significance Determination Process

SP

Surveillance Procedure

SRO

Senior Reactor Operator

SSC

Structure, System, or Component

TC

Temperature Controller

TCN

Temporary Change Notice

TP

Test Procedure

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

USAR

Updated Safety Analysis Report

WO

Work Order

LIST OF DOCUMENTS REVIEWED

1R01

Adverse Weather Protection

TP [Test Procedure] 1637

Winter Plant Operation

Revision 28

System Prestart Checklist

C28-11

CST Winter Operation

Revision 8

Operating Procedure

C28.6

Condensate Storage Tank Freeze

Protection System

Revision 9

WO 0115191

TC [temperature controller]-26300 is not

Working

WO 0100026

121 Spent Fuel Pool Makeup Air Handler

Snow Buildup

WO 0100266

Fabricate Metal Cover for Control Switch

CR 20010134

11 Condensate Recycle Pump Found in

Auto/Off Rendering CST Freeze Protection

Out-of-Service

CR 20011227

C28.6 Condensate Storage Tank Freeze

Protection System Does Not Address Unit

1/Unit 2 CST Temperature Control Valves

CV-31959 and 31957

CR 20010022

Auxiliary Building and Spent Fuel Pool

Makeup Air Handlers Regularly Build Up

With Snow During Winter and No

Procedures for Dealing With It

1R04

Equipment Alignment

Integrated Checklist

C19.2-6

Shield Building Ventilation System Unit 2

Revision 9

Drawing NF-39602-2

Reactor Building Unit 2 Ventilation Flow

Diagram

Revision AP

Operating Procedure

2C19.2

Containment System Ventilation Unit 2

Revision 7

Operations Manual B19

Containment Systems

Revision 5

USAR Section 5.3

Secondary Containment System

Revision 22

TS 3.6.H

Shield Building Ventilation System

Revision 91

TS 4.4.B

Emergency Charcoal Filter Systems

Revision 126

WO 0114057

Humidity Sensor Not Working

WO 0115017

Status Panel Lights Lit Unexpectedly

CR 20001580

Auxiliary Building and Shield Building

Ventilation System Charcoal Ignition

Temperature Stated in the USAR is

Incorrect

CR 200185163

During lCPM [Instrumentation and Controls

Preventive Maintenance] 2-018 Found the

Unit 2 Shield Building Ventilation Particulate

and Charcoal Filter Humidity Sensor Not

Working - No Spares - They Are Obsolete

1R05

Fire Protection

Area Walkdowns

Plant Safety Procedure

F5

Fire Fighting

Revision 25

Plant Safety Procedure

F5 Appendix F

Fire Hazard Analysis

Revision 12

Plant Safety Procedure

F5 Appendix A

Fire Strategies

Revision 8

IPEEE NSPLMI-96001

Appendix B

Internal Fires Analysis

Revision 2

F5 Appendix D

Impact of Fire Outside Control/Relay Room

Revision 6

Fire Brigade Drill

Fire Drill 2001-04

Unit 1 Hydrogen Seal Oil Area

Plant Safety Procedure

F5

Appendix J

Fire Drills

Revision 7

Plant Safety Procedure

F5

Appendix A

Fire Detection Zone 4

Revision 7

CR 200186895

Conduct of Fire Drill

1R11

Licensed Operator Requalification

PITC Q-96

Job Performance Measure Summary Sheets

(10 Operators)

Revision 7

PITC Q-203

Training Cycle Simulator Team Evaluation

(2 Crews) plan

Revision 1

Meeting Minutes

Operations PAC Committee Meeting Notes

Various

Simulator Guide

NIS Failure/Charging Pump Trip/RCP Seal

Failure/RPS Failure/SBLOCA

Revision 13

Simulator Guide

Steam Generator Tube Rupture w/Loss of

1R Transformer

Revision 0

Simulator Guide

Loss of Bus Duct Cooling/Accumulator

Inleakage/Loss of All AC/SBLOCA

Revision 4

Job Performance

Measures

Thirty Job Performance Measures of

Various Titles Used for this Examination

Various

Written Examinations

Written Examinations Administered to All

Licensed Operators During Examination

Weeks

Various

Medical Records

Medical Records for Twenty Randomly

Selected Operators

Various

UFSAR

Prairie Island Updated Final Safety Analysis

Report, Section 14.5.4, Steam Generator

Tube Rupture

Revision 22

SWI-0-43

Operator Qualification Program

Revision 1

SWI 0-39

Operations Training Plan

Revision 6

CR 20000885

Perform a Self-Assessment of Operations

Training

March 31, 2000

Self-Evaluation

INPO Accreditation Renewal Self-Evaluation

Report

September 6,

2001

P9100

Program Description for License

Requalification Training

Revision 17

Training Procedure

NRC Exam Security Training Procedure

3.10

Revision 8

PITC 3.7

License Requalification Examination

Development and Administration

Revision 10

1R12

Maintenance Rule Implementation

General

2000 Equipment Performance Annual

Report

April 20, 2001

Maintenance Rule System Basis Document,

Volume 1A

Revision 3

Quarterly Equipment Performance Report -

3nd Quarter 2001

November 13,

2001

NUMARC 93-01

Nuclear Energy Institute Industry Guideline

for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants

Revision 2

Regulatory Guide 1.160

Monitoring the Effectiveness of Maintenance

at Nuclear Power Plants

Revision 2

Circulating Water

CR 20017973

Intake Approach Canal Indicates Canal Is

Slowly Filling In With Silt That May Affect

Water Intake to the Plant

CR 20017497

MV-32001, 11 Circulating Pump Discharge

Valve Operation

CR 20002892

Problems Identified During Surveillance

Procedure 1293, Flood Preparation Flood

Control Panel Inspection/Installation

WO 0101630

24 Traveling Screen Does Not Rotate

WO 0104411

Repair Control Valve for 22 Traveling

Screen

WO 0101591

Traveling Screens Start and Stop

Independent of Control Switch Position

WO 0101586

23 Traveling Screen Making Abnormal

Noises

WO 0101222

24 Traveling Screen Wash Water Control

Valve Leaking By

WO 0101172

Instrument Block Valve for 13 Traveling

Screen Spray Wash Pressure Switch Needs

Rebuild

WO 0010754

Adjust Limit Switches on MV-32005 [1B

Condenser Circulating Water Crossover

Motor Valve], Inspect Seats

WO 0008664

21 Traveling Screen Noise

WO 0008663

23 Traveling Screen Making Noise

WO 0000300

Repair SV-33140 [22 Traveling Screen

Spray Wash Solenoid Valve]

D1 and D2 Emergency Diesel Generators

CR 200186961

D1 Air Start Regulator Diaphragm Seems

To Have Failed When Valved In

CR 20018377

Removal Of Maintenance Resources During

D1 18 Month Planned Maintenance Caused

4 to 5 Hour Delay In Restoration For This

LCO Job

CR 20018181

Eddy Current Testing Located Tubes To Be

Plugged In D1 Oil Cooler And Jacket

Coolant Heat Exchanger

CR 20017414

SP 1093 Completed Unsat Due To Failure

Of Ventilation Fans To Start

CR 20015360

Parts Traceability to End Use Lost Because

They Were Charged To The Wrong Work

Order

CR 20012100

SP 1093 Interrupted Due To Smoke From

Penetration 472 Flammastic On Asbestos

Insulation Smouldered Due To Exhaust

Heat

CR 20003871

Installed New Seals On The Pumps For

Both D1 and D2 Standby Coolant

Recirculation Pumps

1R13

Maintenance Risk Assessment and Emergent Work Control

Prairie Island Action Plan

Actions To Mitigate Reactor Coolant Pump

Seal Leak Off Rate For 22 RCP

Revision 2

Temporary Instruction 01-

101

Unit 2 Volume Control Alternate Dilute Path

Instructions

Abnormal Operating

Procedure 2C3 AOP3

Failure Of A Reactor Coolant Pump Seal

Revision 8

Operating Procedure

C12.1

Letdown, Charging, And Seal Water

Injection

Revision 27

1R15

Operability Evaluations

CR 200186696

Lineshaft and Suction Bell Float Switches

for the 12 Diesel-Driven Cooling Water

Pump are Stuck in the 90-100 Percent Flow

Position - No Alarm Will Sound on Loss of

Flow

USAR Section 10.4.1

Cooling Water System

Revision 22

TS 3.3.D

Cooling Water System

Revision 131

Temporary Instruction 01-

105

Unit 1 Cooling Water

December 4, 2001

Temporary Change

Notice (TCN) 2001-2010

to Annunciator Response

Procedure (ARP) 47020-

0207

12 Cooling Water Pump (Diesel) Running

Revision 27

TCN 2001-2011 to

Operating Procedure C35

Cooling Water System

Revision 43

TCN 2001-2012 to Prairie

Island Nuclear Generating

Plant (PINGP)195

Turbine Building Data - Unit 1

Revision 62

ARP 47020-0608

12 Cooling Water Pump (Diesel) Loss of

Bearing Water Flow

Revision 30

CR 200186163

Evaluate Westinghouse 9 November 01

Letter for Effect on Plant

CR 200186164

Review Need for Changing Annunciator

Response Procedure/Setpoints for

Accumulator High/Low Pressure Based on

Results of CR 200186163

CR 200186166

Implement Interim Controls to Ensure

Accumulator Pressures are Maintained 740

+/- 20 Vice 740 +/- 30 as Allowed by TS

CR 200186167

Review Need to Revise TSs Based Upon

Results of CR 200186163

CR 200186168

Review Past Operating History for

Reportability Due to New Accumulator

Pressure Limits in CR 200186163 Letter and

TS Nonconservatism

TS 3.3.A

Safety Injection and Residual Heat Removal

Systems

Revision 161

USAR Section 6.2

Safety Injection System

Revision 22

USAR Section 14.6

Large Break LOCA [Loss of Coolant

Accident] Analysis

Revision 22

1R16

Operator Workarounds

CR 20003741

Safety Injection Mini Recirculation Flow

Failure

CR 20010354

Equipment Problems Were Encountered

During Installation of the Safety Injection

Mini Recirculation Flow Meters

WO 0003335

Install New Safety Injection Recirculation

Flowmeters

WO 0003399

Install New Safety Injection Mini

Recirculation Line Flowmeters

WO 0104180

Replace Safety Injection Miniflow

Transducers

Temporary Instruction

01-08

Safety Injection Mini Recirculation Line

LO/NO Flow Out-Of-Service

The 4th Quarter of 2001 Report on Operator

Workarounds and Aggregate Assessment of

Operator Workarounds

1R19

Post-Maintenance Testing

CR 200185959

Investigation of 2RX Bus Duct Following

Lockout of 2RX Transformer Revealed Fault

and Raises Questions on 2RY Bus Duct

CR 200185890

2RX Transformer Locked Out

CR 200186230

Re-insulate the Outdoor Portion of 2RX Bus

With 15 KV Insulating Sleeve.

CR 200186232

Ensure Moisture Abatement Systems Are

Properly Installed and Functioning on 2RX

Bus Duct

CR 200186233

Ensure Good Electrical Connection at the

Splice Points of 2 RX Bus That Had Been

Disassembled for Insulation System Repair

CR 200186234

Perform Inservice Testing of Plant Busses

Using Radio Frequency Monitoring

Technique

WO 0115052

2RX/300 Bus Duct Inspection

WO 0115183

2RX Transformer and Bus Duct Post

Maintenance Testing

WO 0115131

Test Operability of the 2 RX Bus Duct

Heater

WO 0013308

PE-121J-4, Breaker Electrical 5 Year

Planned Maintenance, MV-32085

WO 0107577

P32085 12 Residual Heat Removal Pump

Suction From Refueling Water Storage

Tank D70 Inspection

1R22

Surveillance Testing

SP 1112

Steam Exclusion Monthly Damper Test

Revision 40

SP 1117

Monthly Steam Exclusion Check Damper

Test

Revision 8

TS 4.8.C

Steam Exclusion System

Revision 91

TS Table 4.1-1C

Miscellaneous Instrumentation Surveillance

Requirements

Revision 121

TS 3.4.C

Steam Exclusion System

Revision 91

TS Table 3.5-1

Engineered Safety Features Initiation

Instrument Limiting Set Points

Revision 44

Administrative Work

Instruction 5AWI 8.7.0

Foreign Material Exclusion Program

Description

Revision 3

USAR Appendix I,

Section 4.2

Steam Exclusion Boundaries

Revision 23

CR 19992037

Damper Gear Integrity

SP 2088B

Train B Safety Injection Quarterly Test

Revision 0

TCN 2001-2036

Train B Safety Injection Quarterly Test

Revision 0

4OA1 Performance Indicator Verification

NEI 99-02

Regulatory Assessment Performance

Indicator Guideline

Revision 1

4OA3 Event Followup

LER 2-01-03

Technical Specification Required Shutdown

of Unit 2 Due to Declared Inoperability of

Both Emergency Diesel Generators

Revision 1

LER 2-01-03

Technical Specification Required Shutdown

of Unit 2 Due to Declared Inoperability of

Both Emergency Diesel Generators

Revision 2

NRC Letter from G. Grant

to Final Significance Determination for

Preliminary White Finding; (NRC Inspection

Report 50-306/01-13) (Prairie Island Nuclear

Generating Plant, Unit 2)

November 11,

2001

LER 1-01-03

Plant In Unanalyzed Condition Due to Flood

Panel Deficiencies