IR 05000271/2006002

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IR 05000271-06-002; 01/01/06 - 03/31/06; Vermont Yankee Nuclear Power Station; Routine Integrated Report
ML061290083
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 05/09/2006
From: Anderson C
NRC/RGN-I/DRP/PB5
To: Thayer J
Entergy Nuclear Operations
References
IR-06-002
Download: ML061290083 (30)


Text

May 5, 2006

SUBJECT:

VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000271/2006002

Dear Mr. Thayer:

On March 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vermont Yankee Nuclear Power Station. The enclosed report documents the inspection findings which were discussed on April 13, 2006, with members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Clifford J. Anderson, Chief Projects Branch 5 Division of Reactor Projects Docket No. 50-271 License No. DPR-28 Enclosure: Inspection Report 05000271/2006002 w/Attachment: Supplemental Information

M

SUMMARY OF FINDINGS

IR 05000271/2006002; 01/01/06 - 03/31/06; Vermont Yankee Nuclear Power Station; Routine

Integrated Report.

This report covered a 13-week period of inspection by resident inspectors and announced inspections by regional engineering, health physics, operations, and emergency preparedness inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings

No findings of significance were identified.

B.

Licensee Identified Findings None.

REPORT DETAILS

Summary of Plant Status

Vermont Yankee (VY) Nuclear Power Station began the inspection period operating at or near full power. On February 2, 2006, Entergy performed a planned reactor power reduction to approximately 50% to support control rod pattern adjustment and feedwater regulating valve (FRV) maintenance then returned to full power. On March 2, the NRC granted Entergy a license amendment increasing VYs licensed maximum power level from 1593 megawatts thermal (MWth) to 1912 MWth. On March 4, operators increased power to approximately 105%

of VYs original licensed limit in accordance with the approved power ascension test procedure.

This equated to a reactor power of approximately 87% of the newly-licensed power level.

Power was maintained at approximately 87% for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

.1 Readiness for Seasonal Susceptibilities

a. Inspection Scope

(one sample)

The inspectors reviewed measures established by Entergy for ensuring cold weather availability and operability of the alternate cooling system (ACS) including inspections of the accessible portions of the ACS piping heat tracing and system alignment used to de-ice the West cooling tower deep basin. The inspectors performed walkdowns of the accessible portions of these systems and compared the current system alignments and operation to the requirements of Vermont Yankee Operating Procedure (OP) 2196, Preparations for Cold Weather Operations, OP 3127, Natural Phenomena, OP 0150, Conduct of Operations and Operator Rounds, OP 2181, Service Water/Alternate Cooling Operating Procedure, OP 2180, Circulating Water/Cooling Tower Operation, and Technical Specifications (TS). Additionally, the inspectors reviewed condition reports (CRs) related to cold weather to ensure issues associated with ACS piping heat tracing and the West cooling tower deep basin were properly addressed for resolution.

b. Findings

No findings of significance were identified.

.2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

(two samples)

On February 17, the inspectors reviewed actions taken by Entergy following the receipt of switchyard annunciator alarms coincident with high winds and thunderstorm activity in the vicinity of the plant. During this weather event, control room operators observed seven alarms related to a disturbance on the Northfield 345 kilovolt (KV) off-site power line and entered OP 3127, Natural Phenomena, Appendices B, Lightning Damage Indicator Walkdown Check Sheet, and E, Considerations When Severe Natural Phenomena is Imminent. The inspectors performed independent walkdowns of the switchyard and 345 KV relay house.

On February 28, the inspectors reviewed actions taken by Entergy due to severe cold weather in the vicinity of the plant. The inspectors reviewed procedure OP 3127, Appendix D, Extreme Low Temperature Walkdown Check Sheet, and performed independent walkdowns of systems listed in Appendix D, including the high pressure coolant injection (HPCI), reactor core isolation cooling (RCIC), and the emergency diesel generator (EDG) systems, to determine the impact of severe cold weather on these systems. The inspectors also performed a walkdown of the condensate storage tank (CST) enclosure to verify the temperature in the vicinity of the CST level instrumentation and associated HPCI and RCIC suction automatic transfer instrumentation remained above the temperature required by the environmental qualification program.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Equipment Alignment

a. Inspection Scope

(four samples)

The inspectors performed four partial system walkdowns of risk-significant systems to verify system alignment and to identify any discrepancies that could impact system operability. Observed plant conditions were compared to the standby alignment of equipment specified in Entergys system operating procedures. The inspectors also observed valve positions, the availability of power supplies, and the general condition of selected components to verify there were no obvious deficiencies. The inspectors verified the alignment of the following systems:

  • The safety-related portions of the service water (SW) system while the C SW pump was out of service for planned maintenance;
  • The HPCI system while the RCIC system was out of service for planned maintenance;
  • The A train of the standby liquid control (SLC) system and the alternate rod insertion system during emergent repair of the B SLC pump suction isolation valve, SLC-12B.

b. Findings

No findings of significance were identified.

.2 Complete Equipment Alignment

a. Inspection Scope

(one sample)

The inspectors performed a complete equipment alignment inspection of the accessible portions of the RCIC system. The inspectors walked down the RCIC system and compared actual equipment alignment to approved piping and instrumentation drawings (P&IDs), the updated final safety analysis report (UFSAR), the RCIC design basis document (DBD), and operating procedures. The inspectors reviewed RCIC system health reports, open corrective maintenance and modification work orders, and a sample of CRs related to the RCIC system.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Quarterly Fire Area Inspections

a. Inspection Scope

(nine samples)

The inspectors identified fire areas important to plant risk based on a review of Entergys Vermont Yankee Safe Shutdown Capability Analysis, the Fire Hazards Analysis, and the Individual Plant Examination External Events (IPEEE). The inspectors toured plant areas important to safety in order to verify the suitability of Entergys control of transient combustibles and ignition sources, and the material condition and operational status of fire protection systems, equipment, and barriers. The following combustion free zones (CFZs), fire areas (FAs) and fire zones (FZs) were inspected.

  • Torus Room, 213 foot elevation, North (FZ RB1);
  • Torus Room, 213 foot elevation, South (FZ RB2);
  • Reactor Building, 252 foot elevation, North (FZ RB3);
  • Reactor Building, 252 foot elevation, South (FZ RB4);
  • Reactor Building, 252 foot elevation, S1 cable trays (CFZ 3/4);
  • Reactor Building, 252 foot elevation, S2 cable trays (CFZ 3/4);
  • Reactor Building, 280 foot elevation, recirculation motor generator area (SZ RB-MG);
  • Reactor Building, 303 foot elevation (FZ RB7); and
  • Turbine Building, all areas (FA TB).

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill Observation

a. Inspection Scope

(one sample)

On February 7, the inspectors observed the performance of a fire drill involving simulated smoke and arcing in the cable vault nuclear instrumentation battery room.

Also simulated was an injured, non-ambulatory individual at the same location. The inspectors evaluated the readiness of the fire brigade against the drill objectives and acceptance criteria established within the drill scenario including:

  • Donning of protective clothing;
  • Use of self-contained breathing apparatus equipment;
  • Fire brigade control of the affected area;
  • Use and availability of fire fighting equipment; and
  • Communications between the fire brigade, the main control room, and security personnel.

The inspectors also observed debriefing activities between the drill evaluators and the fire brigade to ensure lessons learned were communicated to fire brigade members.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

(one sample)

The inspectors reviewed Entergys established flood protection barriers for coping with internal flooding on the 252 foot elevation of the reactor building. The inspectors reviewed internal flooding design information contained in Entergys IPEEE, the UFSAR, and in the Internal Flooding DBD. The inspectors also performed a walkdown of accessible portions of the area to ensure equipment and structures needed to mitigate an internal flooding event were as described in the IPEEE and the DBD.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Requalification Activities Review by Resident Staff

a. Inspection Scope

(one sample)

The inspectors observed a simulator as-found evaluation for one operating crew to assess the performance of the licensed operators and the ability of Entergys Training and Operations Department staff to evaluate licensed operator performance. Crew performance was evaluated during simulated events involving a main steam line break and a loss of both startup transformers under extended power uprate conditions. The inspectors evaluated the crews performance in the following areas:

  • Clarity and formality of communications
  • Ability to take timely actions
  • Prioritization, interpretation, and verification of alarms
  • Procedure use
  • Control board manipulations
  • Oversight and direction from supervisors
  • Command and control Crew performance in these areas was compared to Entergy management expectations and guidelines as presented in Vermont Yankee Administrative Procedure (AP) 0151, Responsibilities and Authorities of Operations Department Personnel, AP 0153, Operations Department Communication and Log Maintenance, and Vermont Yankee Department Procedure (DP) 0166, Operations Department Standards. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed Entergy evaluators to verify that they also noted the issues to be discussed with the crew.

b. Findings

No findings of significance were identified.

.2 Training Provided to Licensed Operators Regarding Plant Response to a Condensate

Pump Trip

a. Inspection Scope

(one sample)

The inspectors observed just in time (JIT) training provided to licensed operators on the expected plant response to a trip of either a feedwater pump or a condensate pump from the new 100% reactor power level (following implementation of the extended power uprate). Training included a discussion of expected plant response(s) and a series of simulator scenarios requiring operators to respond to simulated condensate pump and feedwater pump trips. The inspectors compared the operators response to expected operator actions contained in the applicable operational transient procedures and Operations Department standards. Additionally, the inspectors observed the fidelity of the plant-specific simulator and compared it to the plant response that had been predicted by Reactor Engineering and to the requirements of American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, Nuclear Power Plant Simulators for Use in Operator Training and Examination.

b. Findings

During the observation of training provided to licensed operators on the expected plant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulated plant response differed from the predicted plant response indicated in Reactor Engineerings analysis for this event. The difference was in the final values of core thermal power and core flow immediately following the pump trip. This issue was of particular interest because the VY Extended Power Uprate Safety Evaluation Report requires Entergy to perform a condensate pump trip test once they reach the new extended power uprate 100% power level.

Following a trip of a condensate pump from 100% power, expected plant automatic responses include (but are not limited to) the trip of one of the three running feedwater pumps (in anticipation of reduced pump suction pressure due to the tripped condensate pump) and a recirculation pump runback (to reduce core flow and thus core thermal power to a point consistent with continued operation with two feedwater pumps running).

Entergy Reactor Engineering personnel had performed an analysis to predict the values for core thermal power and core flow immediately following a condensate pump trip from 100% power. This analysis indicated that the combination of final core thermal power and core flow would place the plant on a point on the power-to-flow map slightly above the established power-to-flow limit line which, by procedure, would require operators to insert control rods to reduce reactor power below the power-to-flow limit line.

While observing licensed operator training on the expected plant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulator response differed from Reactor Engineerings predicted plant response in that the combination of final core thermal power and core flow placed the plant on a point on the power-to-flow map below the established power-to-flow limit line, thus no rod insertion was required.

The inspectors discussed this issue with Entergy who then entered it into the corrective action program (CR 2006-0603). Additional actions taken by Entergy at that time included a memorandum, issued by the Operations Department, to alert operators to the results of Reactor Engineerings analysis and expected plant response to a condensate pump trip and plans by the Training Department to provide additional condensate pump trip training during upcoming licensed operator requalification training (LORT). This training will be in addition to existing plans to perform JIT training prior to the performance of the required condensate pump trip test.

In accordance with ANSI/ANS 3.5-1998, Entergy is expected to maintain the plant-specific simulator such that it accurately reflects actual plant response(s) to transients.

This ensures that the simulator training provided to licensed operators best prepares them to respond to an event such as a trip of a condensate pump. To determine if the initial condensate pump trip training provided to licensed operators met the guidance outlined in ANSI/ANS-3.5-1998, the inspectors plan to observe the planned condensate pump trip training to be provided during upcoming LORT, observe the JIT training provided prior to the performance of the required condensate pump trip test, and observe the performance of the actual condensate pump trip test. This issue is considered to be an unresolved item (URI) pending determination of whether the training provided to the operators met the guidance outlined in ANSI/ANS-3.5-1998: URI 05000271/2006002-01, Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip.

1R12 Maintenance Effectiveness

a. Inspection Scope

(two samples)

The inspectors performed one issue/problem-oriented inspection of actions taken by Entergy in response to the failure of the A RHR/Core Spray (CS) system power monitoring relay, 10A-K3A. The inspectors also performed one system/function performance history-oriented inspection of the ACS freeze protection system, a system currently designated as a Maintenance Rule a(1). These inspections included a review of work practices that may have contributed to degraded system performance, Entergys ability to identify and address common cause failures, the applicable maintenance rule scoping document for each system, the current classification of these systems in accordance 10 CFR 50.65 (a)(1) or (a)(2), and the appropriateness of the performance criteria and goals established for each system.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Evaluation

a. Inspection Scope

(five samples)

The inspectors evaluated online risk management for three planned maintenance activities and two emergent repair activities. The inspectors reviewed maintenance risk evaluations, work schedules, recent corrective actions, and control room logs to verify that other concurrent or emergent maintenance activities did not significantly increase plant risk. The inspectors compared reviewed items and activities to requirements listed in AP 0125, "Plant Equipment" and AP 0172, "Work Schedule Risk Management -

Online." The inspectors reviewed the following work activities:

  • Planned maintenance on the B train of the RHR system;
  • Planned maintenance on the C SW system pump;
  • Planned maintenance on the RCIC system;
  • Emergent repair of SLC system valve SLC-12B; and
  • Emergent repair of the A RHR/CS system power monitoring relay, 10A-K3A.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions

a. Inspection Scope

(three samples)

The inspectors directly observed and assessed control room operator performance during the following non-routine evolutions:

  • Power reduction to approximately 50% to support a planned control rod sequence exchange and FRV maintenance on February 2, 2006; and
  • The first 5% power increase for the extended power uprate on March 4, 2006.

The adequacy of personnel performance, procedure compliance, and use of the corrective action process for all non-routine evolutions were evaluated against the requirements and expectations contained in TS and the following station procedures, as applicable:

  • AP 0151, Responsibilities and Authorities of Operations Department Personnel;
  • AP 0153, Operations Department Communication and Log Maintenance;
  • DP 0166, Operations Department Standards;
  • Engineering Request Special Test Instruction (ERSTI) 04-VY1-1409, Power Ascension Test Procedure for Extended Power Conditions 1593 to 1912 MWth;
  • OP 0105, Reactor Operations; and
  • OP 2403, Control Rod Sequence Exchange with the Reactor Online.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

(four samples)

The inspectors reviewed four operability determinations prepared by Entergy. The inspectors evaluated the operability determinations against the guidance contained in NRC Inspection Manual, Part 9900, Technical Guidance, Operability Determinations and Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety, as well as Entergy procedure ENN-OP-104, Operability Determinations. The inspectors verified the adequacy of the following evaluations of degraded or non-conforming conditions:

  • Observed voltage increase on motor control center 89B;
  • The D RHR pump breaker charging spring indicator did not indicate fully charged as expected;
  • A CST low level signal to the logic for RCIC containment isolation valve V13-41 would override the ability of the valve to be manually closed from the main control room as described in the UFSAR; and
  • Issues identified with RHRSW system piping while performing a system high flow test.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

(one sample)

The inspectors reviewed the permanent replacement of the RCIC system cooling water line pressure control valve to verify that the design bases, licensing bases, and performance capability of the RCIC system had not been degraded. The inspectors reviewed the modification package Engineering Request (ER) 04-1222, Replace RCIC PCV-13-23 with One Direct Acting Pressure Control Valve and Install Restriction Orifice. This modification was also selected to verify that the corrective actions taken by Entergy to address issues previously identified in NCV 05000271/2004008-05, Cooling Water Supply Portion of RCIC Not Installed per Design Basis and NCV 05000271/2004008-06, Failure to Correct Non-Conforming RCIC Pressure Control Valve, had been completed and were appropriate. The inspection also included a walkdown of the RCIC system, interviews with plant staff, and review of applicable documents including the modification package, procedures, calculations, drawings, and the UFSAR. A listing of documents reviewed is provided in the attachment to this report.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

b. Inspection Scope

(seven samples)

The inspectors reviewed seven post-maintenance testing (PMT) activities on risk-significant systems. The inspectors either directly observed the testing or reviewed completed PMT documentation to verify that the test data met the required acceptance criteria contained in the TS, UFSAR, and inservice testing program. Where testing was directly observed, the inspectors verified that installed test equipment was appropriate and controlled and that the test was performed in accordance with applicable station procedures. The inspectors also ensured that the test activities were adequate to ensure system operability and functional capability following maintenance, systems were properly restored following testing, and any discrepancies were appropriately documented in the corrective action program. The inspectors reviewed the PMTs performed for the following maintenance activities:

  • Disassembly and inspection of B RHR pump discharge check valve V10- 48B, PMT in accordance with work order (WO) 05-3565 and OP 4124;
  • Installation of new RCIC system oil cooler pressure control valve and orifice assembly, PMT in accordance with ERT-04012222-01;
  • Testing of RHR/CS system power monitoring relay following repair and replacement;
  • RCIC system turbine overspeed trip testing following planned maintenance on the trip mechanism in accordance with OP-5296;
  • A FRV positioner replacement, PMT per OP-4172; and
  • Repair of SLC system valve SLC-12B, PMT per OP-4114.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

(seven samples)

The inspectors observed surveillance testing to verify that the test acceptance criteria specified for each test was consistent with TS and UFSAR requirements, the test was performed in accordance with the written procedure, the test data was complete and met procedural requirements, and the system was properly returned to service following testing. The inspectors observed selected pre-job briefs for the test activities. The inspectors also verified that discrepancies were appropriately documented in the corrective action program. The inspectors verified that the following surveillance testing activities met the above requirements:

  • A EDG monthly surveillance testing (routine test) in accordance with OP 4126, Section B;
  • A RHR system quarterly surveillance testing (in-service test) in accordance with OP 4124, Section H;
  • A RHRSW system quarterly surveillance testing (in-service test) in accordance with OP 4124, Section G;
  • RHR system valves RHR-26A and 26B accumulator pressure test (routine test)in accordance with OP 4124, Section C;
  • Drywell equipment and floor drain testing and drywell leakage calculation (reactor coolant system leak detection test) in accordance with OP 4152, Section A;
  • HPCI system quarterly surveillance testing (routine test) in accordance with OP 4120, Section A; and
  • Six Month EDG Fast Start Operability Test (routine test) in accordance with OP 4126, Section F.

b. Findings

No findings of significance were identified

1R23 Temporary Plant Modifications

z.

Inspection Scope (one sample)

The inspectors reviewed a temporary alteration (TA) made to the position indication probe for control rod 26-07 to ensure that this alteration did not adversely affect the availability, reliability, or functional capability of any risk-significant structures, systems, or components. The inspectors compared the information in the TA package to Entergys TA requirements contained in ENN-DC-136, Temporary Alterations. The inspectors observed the installation of the TA and verified that required tags were applied and that the alteration was being properly maintained.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

(one sample)

The NRC received and acknowledged the changes made to the Vermont Yankee Emergency Plan and implementing procedures. Entergy made the changes in accordance with 10 CFR 50.54(q) and determined that the changes did not result in a decrease in effectiveness to the Plan and concluded that the changes continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. During this in-office inspection on January 30 and March 6, 2006, the inspectors conducted a sampling review of the changes which could potentially result in a decrease in effectiveness. This review does not constitute an approval of the changes and, as such, the changes are subject to future NRC inspection. The requirements in 10 CFR 50.54(q) were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a. Inspection Scope

(one sample)

On January 26, 2006, the inspectors observed an operating crew respond to a simulator-based event during licensed operator requalification training activities. The inspectors discussed the performance expectations and results with the lead instructor.

The inspectors focused on the ability of licensed operators to perform event classifications and make proper notifications in accordance with the following station procedures and industry guidance:

  • AP 0153, Operations Department Communications and Log Maintenance;
  • AP 0156, Notification of Significant Events;
  • DP 0093, Emergency Planning Data Management;
  • OP 3540, Control Room Actions During an Emergency; and

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

(twelve samples)

The inspectors reviewed the effectiveness of Entergys program to maintain occupational radiation exposure as low as reasonably achievable (ALARA). The inspectors performed a selective examination of documents (as cited in the List of Documents Reviewed section) for regulatory compliance and for adequacy of control of radiation exposure. The review was against criteria contained in 10 CFR 20.1101 (Radiation Protection Programs), 10 CFR 20.1701 (Use of Process or Other Engineering Controls), and Entergy procedural requirements.

This inspection activity represents the completion of twelve

(12) samples relative to this inspection area (i.e., inspection procedure sections 02.01.a, c, and d, 02.02.a thru c, and e*, f*, and I*, 02.03.a and 02.08.a and b*) in partial fulfillment of the biennial inspection requirements.

Planning (02.01.a, c, and d)

The inspectors reviewed pertinent information regarding plant collective exposure history, current exposure trends, and ongoing or planned activities in order to assess current performance and exposure challenges. The inspectors reviewed the site specific trends in collective exposures and source-term (i.e., average contact dose rates with reactor coolant piping) measurements. The inspectors also reviewed the site specific procedures associated with maintaining occupational exposures ALARA. This review included a review of processes used to estimate and track work activity specific exposures. The review was against criteria contained in 10 CFR 20.1101 (Radiation Protection Programs).

Radiological Work Planning (02.02.a thru c, e*, f*, and I*)

The inspectors obtained a list of twenty-one ALARA refueling outage work activity packages with their exposure summaries, including the original exposure estimates and actual exposures. The inspectors reviewed the post-job ALARA reviews for six activities with actual exposures that were greater than five rem and exceeded the original exposure estimates by fifty percent. For these outage work activities, the inspector reviewed the pre-job ALARA work activity evaluations, exposure estimates, exposure mitigation requirements, radiation work permits, in-progress ALARA reviews, and revised exposure estimates based on the in-progress ALARA reviews. The inspectors reviewed grouping of the radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances. The inspectors compared the results achieved (i.e., dose rate reductions, person-rem used) with the intended dose established in Entergys ALARA planning for these work activities.

The inspectors reviewed the integration of ALARA requirements into the radiation work permit documents. While examining selected post-job ALARA review documents, the inspectors compared the person-hour estimates provided by maintenance planning and other groups to the radiation protection group with the actual work activity time requirements and evaluated the accuracy of these time estimates. During the review of selected post-job (work activity) review documents, the inspectors confirmed that identified problems and items for improvement were entered into Entergys corrective action program.

Verification of Dose Estimates and Exposure Tracking Systems (02.03.a)

The inspectors reviewed the current annual collective exposure estimate for 2006 and the assumptions and basis for the estimate. The inspectors discussed the methodology used for estimating work activity-specific exposures and the intended dose outcome with the radiation protection manager and the ALARA supervisor. The review was against criteria contained in 10 CFR 20.1101 (Radiation Protection Programs).

Problem Identification and Resolution (02.08.a and b*)

The inspectors reviewed Entergys last self-assessment of ALARA which was conducted in 2005 and the post-job ALARA reviews for six work activities in the 2005 refueling outage. The inspectors reviewed their methodology for meeting the requirements of 10 CFR 20.1101 to review the content and implementation of the radiation protection program on at least an annual basis. The inspectors discussed this requirement with the radiation protection manager and with a radiation protection support supervisor. The inspectors also reviewed Entergys procedure used to implement this requirement.

During the review of dose-significant post-job (work activity) reviews of exposure performance, the inspectors evaluated those identified problems that were entered into the corrective action program for resolution.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

(three samples)

The inspectors sampled Entergy submittals for the performance indicators (PIs) listed below for the period from January 2004 to December 2005. The inspectors reviewed selected operator logs, plant process computer data, CRs, and monthly operating reports. The PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Indicator Guideline, and AP 0094, NRC Performance Indicator Reporting, were used to verify the accuracy and completeness of the PI data reported during this period.

Initiating Events Cornerstone

  • Unplanned Scrams per 7000 Critical Hours
  • Scrams with Loss of Normal Heat Removal

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

a. Inspection Scope

The inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into Entergys corrective action program at an appropriate threshold and that adequate attention was being given to timely corrective actions. Additionally, in order to identify repetitive equipment failures and/or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into Entergys corrective action program. This review was accomplished by reviewing the description of each new CR and/or by attending daily CR screening meetings. A listing of CRs and other documents reviewed is included in the attachment to this report.

b. Findings

No findings of significance were identified.

.2 Annual Sample Review - Operator Workarounds

a. Inspection Scope

(one sample)

The inspectors reviewed the cumulative effect of operator workarounds on the reliability, availability, and potential mis-operation of systems with particular focus on issues that had the potential to affect the ability of operators to respond to plant transients and events. The inspectors reviewed the Operator Aggregate Impact Index and Operations Performance Indicators for February 2006, as well as the related operator burdens, control room deficiencies, system lineup deviations, and disabled or illuminated control room alarms. For selected issues, the inspectors reviewed CRs and discussed the issues with responsible operations personnel to ensure they were appropriately categorized and tracked for resolution. In addition, control panel and in-plant walkdowns were performed to identify any potential workarounds that had not been previously identified in accordance with procedures DP 0166, Operations Department Standards, and AP 0047, Work Requests.

b. Findings and Observations

No findings of significance were identified. The inspectors found that Entergy ensured that appropriate attention was placed on conditions that could impact operator actions, including conditions that would require compensatory actions (workarounds and burdens), control room deficiencies and alarms, components tagged out-of-service or with caution tags, and component deviations, through periodic management review of performance indicators. At the time of the inspection, there were no open operator workarounds and corrective actions for other items were scheduled for completion commensurate with each items significance.

4OA3 Event Followup

.1 (Closed) Licensee Event Report (LER) 05000271/2005002-00 Primary Containment

Leak Rate Testing Program Second Barrier Valve Found Mis-Positioned On October 4, 2005, Entergy identified that a 3/4 inch manual globe valve in a RHR system sample line (valve V10-198A) was found to be open verses its required position of closed. V10-198A is a second barrier that supports Entergys primary containment integrity and is required to be closed per TS Surveillance Requirement 4.7.A.2 and Entergys Primary Containment Leakage Rate Testing Program. Upon discovery, operators closed V10-198A, placed it under administrative control by applying a danger tag indicating the valves required closed position, and entered the issue into their corrective action program (CR 2005-2879). Although V10-198A was open, Entergy verified that primary containment integrity was maintained by two normally-closed, air-operated chemistry sampling valves and an additional normally-closed, manually operated valve located downstream of V10-198A. Entergy determined that the root cause of this condition was the application of an inadequate design control process in 1996 during the implementation of the Qualified Closed Loop Outside Primary Containment modification. The process that was used lacked sufficient documentation and reviews to effectively implement required changes including changes to procedures and drawings. As a result, the valve lineups included in the RHR system operating procedure and the RHR P&ID were not updated to reflect the required closed position of V10-198A versus open. Corrective actions included improvements to the design control process, completion of required revisions to the RHR system operating procedure and P&ID, and the performance of extent of condition reviews. Although the fact that V10-198A was open with the reactor plant critical was a condition prohibited by TS, the inspectors concluded that this issue constituted a violation of minor significance. The inspectors based their conclusion on the fact that Entergy was able to verify that primary containment integrity was maintained regardless of the position of V10-198A and the fact that no new findings were identified during their review. As such, this finding is not subject to enforcement action in accordance with Section IV of the NRCs Enforcement Policy. This LER is closed.

4OA5 Other Activities

.1 Power Uprate: Power Ascension Testing

a. Inspection Scope

The inspectors observed selected plant testing performed in accordance with attachments to test procedure ERSTI-04-VY1-1409, Power Ascension Test Procedure for Extended Power Conditions 1593 to 1912 MWth, following Entergys initial 5 percent power increase to approximately 87% of the newly-licensed power level on March 4, 2006. The following activities were observed to ensure operators performed the tests in accordance with the approved procedures and plant TS, test results were appropriately evaluated, and plant systems were restored following testing.

  • 8A, MHC [mechanical hydraulic control, i.e., pressure]

Demonstration 1673 MWth.

Following the power increase to 87%, the inspectors observed Entergys actions when they determined that a Level 2 Hold criterion was reached for strain gauge data on the A main steam line. CR 2006-0650 was written to document the condition.

b. Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

Resident Exit On April 13, the resident inspectors presented the inspection results to Mr. Bill Maguire and other members of the VY staff. The inspectors asked whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

J. Devincentis, Licensing Manager
J. Dreyfuss, Director of Engineering
M. Hamer, Licensing
W. Maguire, General Manager of Plant Operations
K. Pushee, Radiation Protection Manager
N. Rademacher, Director of Nuclear Safety
J. Thayer, Site Vice President

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000271/2006002-01 URI Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip (Section 1R11.2)

Closed

05000271/2005002-00 LER Primary Containment Leak Rate Testing Program Second Barrier Isolation Valve Found Mis-Positioned (Section 4OA3)

Discussed

05000271/2004008-05 NCV Cooling Water Supply Portion of RCIC not Installed per Design Basis (Section 1R17)
05000271/2004008-06 NCV Failure to Correct Non-Conforming RCIC Pressure Control Valve (Section 1R17)

LIST OF DOCUMENTS REVIEWED