IR 05000269/1992027

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Insp Repts 50-269/92-27,50-270/92-27 & 50-287/92-27 on 921101-28.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maintenance Activities & Low Pressure Injection Sys Walkdown
ML16148A723
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 12/15/1992
From: Belisle G, Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A722 List:
References
50-269-92-27, 50-270-92-27, 50-287-92-27, NUDOCS 9301150255
Download: ML16148A723 (8)


Text

SREG(

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, ATLANTA, GEORGIA 30323 Report Nos.:

50-269/92-27, 50-270/92-27 and 50-287/92-27 Licensee:

Duke Power Company 422 South Church Street Charlotte, NC 28242-0001 Docket Nos.: 50-269, 50-270, 50-287, 72-4 License Nos.: DPR-38, DPR-47, DPR-55, SNM-2503 Facility Name: Oconee Nuclear Station Inspection Conduct d:

ovember1 - November 28, 1992 Inspectors:

-

___

___

SP. E. Hirmon, nior e Inspector Date Signed B. Desai esident n c r Date Signed W. K. Poertner, Res' ent Inspe tor Date Signed Approved by: A. Belisle, ection Chief Dat6 Signed SUMMARY Scope:

This routine, resident inspection was conducted in the areas of plant operations, surveillance testing, maintenance activities, low pressure injection system walkdown, and inspection of ope item Results:

No violations or deviations were identified. However, one Unresolved Item (URI) concerning the acceptability of non-safety power supplies to the Low Pressure Injection (LPI) throttle valves was identified (paragraph 5).

9301150255 921217 PDR ADOCK 05000269 Q

PDR

REPORT DETAILS Persons Contacted Licensee Employees

  • H. Barron, Station Manager
  • S. Benesole, Safety Review D. Coyle, Systems Engineering
  • J. Davis, Safety Assurance Manager D. Deatherage, Operations-Support Manager B. Dolan, Manager, Mechanical/Nuclear Engineering (Design)

W. Foster, Superintendent, Mechanical Maintenance J. Hampton, Vice President, Oconee Site 0. Kohler, Regulatory Compliance C. Little, Superintendent, Instrument and-Electrical (I&E)

M. Patrick, Performance Engineer B. Peele, Engineering Manager

  • S. Perry, Regulatory Compliance G. Rothenberger, Work Control Superintendent R. Sweigert, Operations Superintendent Other licensee employees contacted included technicians,- operators, mechanics, security force members, and staff engineer NRC Resident Inspectors
  • Harmon
  • W. Poertner B. Desai
  • Attended exit intervie.

Plant Operations (71707) General The inspectors reviewed plant operations throughout the reporting period to verify conformance with regulatory requirements, Technical Specifications (TS), *and administrative control Control room logs, shift turnover records, temporary modification log and equipment removal and restoration records -were reviewed routinely. Discussions were conducted with plant operations, maintenance, chemistry, health physics, instrument & electrical (I&E), and performance personne Activities within the control rooms were monitored on an almost daily basi Inspections were conducted on day and on night shifts, during weekdays and :on weekends. Some inspections were made during shift change in order to evaluate shift turnover performance. Actions observed were conducted as required by the licensee's Administrative Procedures. The complement of licensed personnel on each shift inspected met or exceeded the requirements

of T Operators were responsive to plant annunciator alarms and were cognizant of plant condition Plant tours were taken throughout the reporting period on a routine basis. The areas toured included the following:

Turbine Building Auxiliary Building CCW Intake Structure Independent Spent Fuel Storage Equipment Rooms Units 1,_2 and 3 Electrical Equipment Rooms Units 1, 2 and 3 Cable Spreading Rooms Units 1, 2 and 3 Penetration Rooms Units 1, 2 and 3 Spent Fuel Pool Rooms Station Yard Zone Within the Protected Area Standby Shutdown Facility Keowee Hydro Station During the plant tours, ongoing activities, housekeeping, security, equipment status, and radiation control practices were observe Within the areas reviewed, licensee activities were satisfactor Plant Status Unit 1 operated at power the entire reporting perio Unit 2 operated at power the entire reporting perio Unit 3 operated at power the entire reporting period. Unit 3 experienced a turbine runback to approximately 22 percent power on November 11, 1992, due to low stator coolant waterflow. The low flow condition occurred during a surveillance test to verify the travel stop position of the flow control valve. The travel stop

  • was -loose allowing the valve to shut. The valve was repaired and the unit returned to 100 percent powe No violations or deviations were identifie.

Surveillance Testing 61726)

Surveillance tests were reviewed by the inspectors to verify procedural and performance adequacy..The completed tests reviewed were examined for necessary test prerequisites, instructions, acceptance criteria, technical content, authorization to begin work, data collection, independent verification where required, handling of deficiencies noted, and review of completed work. The tests witnessed, in whole or in part, were inspected to determine that approved procedures were available, test equipment was calibrated, prerequisites were met, tests were conducted according to procedure, test results were acceptable and systems restoration was complete *

Surveillances reviewed and/or witnessed in whole or in part:

IP/0/A/3000/001 I&C Battery Daily Surveillance PT/0/A/0620/16 Keowee Emergency Power Test Within the areas reviewed, licensee activities were satisfactory. No violations or deviations were identifie.

Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting period to verify that work was performed by qualified personnel and that approved procedures in use adequately described work that was not within the skill of the trade. Activities, procedures, -and work requests were examined to verify; proper authorization.to begin work, provisions for fire, cleanliness, and exposure control, proper return of equipment to service, and that limiting conditions for operation were me Maintenance reviewed and/or witnessed in whole or in part:

WR 92048783 Replace 1SV-22 WR 92046343 1AS-98 Setting Is Too Hig Within the areas reviewed, licensee activities were satisfactory. No violations or deviations were identifie.

Low Pressure Injection System Walkdown (71710)

The inspectors performed a system walkdown on the accessible portions of the Unit 2 Low Pressure Injection (LPI) system. The LPI system is normally aligned to the borated water storage tank (BWST) and automatically initiates on an engineered safeguards signal when reactor coolant pressure equals 550 psig or.reactor building pressure reaches 3 psig. The LPI system is manually aligned from the control room to take a suction on the emergency sump when the inventory from the BWST is depleted. The LPI system consists of two 100 percent capacity train Each train consists of an LPI pump, LPI cooler, and associated valves and piping. The system also contains a third pump that is normally isolated that can be aligned to either.LPI trai During a unit shutdown, the LPI system is aligned in the decay heat removal mode of operation. In the decay heat removal alignment, the LPI system is aligned to the.RCS loop 2A hot leg through the decay heat removal drop line when RCS temperature is less than 250 degrees,F and pressure is less than 320 psig. The Unit 2 LPI system must be aligned in switchover during the initial cooldown phase using the LPI syste Switchover consists of aligning the LPI system to direct the reactor coolant through the 2B LPI cooler.to the suction of the A or C LPI pump then to the B LPI cooler outlet to the core flood nozzles back into the reactor vesse This alignment is necessary because the-Unit 2 LPI

coolers have a design pressure rating of 350 psig and the combination of RCS pressure and LPI pump discharge pressure would exceed this design pressure when the LPI system is first placed in service for decay heat remova When RCS pressure is reduced to less than 125 psig the LPI system is aligned in the normal decay heat removall alignment and the 2A LPI cooler can be placed inservice to remove decay hea During the review of procedure OP/2/A/1104/04, Low Pressure Injection System, the inspectors determined that several valves were not included on the valve checklist. The valves in question were valves that interfaced with other systems or vent and drain valves downstream of normally shut isolation valves not in the normal system flowpaths. The inspectors-discussed this item with operations personnel and they agreed to review the valve checklist to determine if the valves' should be included on the LPI valve checklist or if the valves were included on other valve checklist The Reactor. Building Spray pumps and the Low Pressure Injection pumps at Oconee share the same sources of suction water during accident conditions. These sources are the Borated Water Storage Tank-and the Reactor Building Emergency Sum During a Loss of Coolant Accident (LOCA),.both sets of pumps initially take a suction off the Borated Water Storage Tank (BWST) and are aligned to the emergency sump by the operators in the control room as the inventory in the BWST is depleted. In order to prevent damage to the Building Spray pumps, due to inadequate NPSH when the pumps are aligned to the.emergency sump, the Building Spray flow must be throttled to 1000 gpm and the Low pressure injection flow must be throttled to 3000 gpm in accordance with Emergency Procedures. The licensee has stated that pump runout is not a concern with the LPI pumps; however, the licensee does not have an official calculation to support this conclusion. Throttling of the Low pressure injection system flow is accomplished by valves LP 12 and LP-14. These valves are the LPI cooler outlet throttle valve During the walkdown of the LPI system, the inspectors identified that valves 2LP-12 and 2LP-14 are powered from the same non-safety related motor control center. The inspectors discussed this item with the licensee. The licensee's position is that the valves are not required to be powered from a safety related power supply and that an operator could manually throttle the valves prior-to aligning the LPI pumps to the emergency sump, if power was not available to the valve The inspectors believe that the ability to throttle the valves from the control room is a requirement for operability of the BuildingSpray system and that the valves are required to be' powered from a safety related power supply. Swapover to the emergency sump could occur -in approximately 30 minutes after a design basis large break LOCA. Even if LPI.flow could be throttled locally, prior to swapover to the emergency sump, the ability to throttle LPI flow locally after swapover-may not-be achievable due to elevated radiation levels in the LPI cooler roo This issue was discussed between NRR and Region II personnel and this item has been referred to NRR for further review to determine the following: Are common power supplies for the Unit 2 LPI throttle valves acceptable? Are Non-IE power supplies to the LPI throttle valves acceptable? Is manual throttling of LPI flow acceptable given the potential time constraints and the importance of throttling LPI flow to maintain NPSH to the reactor building spray pumps?

The resolution of the acceptability of the present configuration of the LPI throttle valves is identified as Unresolved Item 269,270,287/92-27 01: Non-Safety Related Power Supplies To The LPI Cooler Throttle Valve.

Inspection of Open Items (92700) (92701) (92702)

The following open items were reviewed using licensee reports, inspection, record review, and discussions with licensee personnel, as appropriate: (Closed) Violation 50-269,270,287/88-13-05: Failure to Document the Basis for 10 CFR 50.59 Determinatio The licensee denied the violation in response.dated September 2, 1988. In a letter dated December 7, 1988, the NRC requested the licensee to resubmit the response to the violation. The licensee resubmitted the response admitting the violation in a letter dated January 31, 1989. The inspectors reviewed the licensee's corrective actions pertaining to the violation in NRC Inspection Report Nos. 50-269,270,287/89-09 dated April 12, 1989, and determined that the corrective actions were not complete The inspector reviewed the upgraded valve replacement by Exempt Change process that was completed on March 29, 1989. Corrective actions are complete and are adequat (Closed) Violation 50-269,270,287/90-17-02: Failure to Follow Procedures Resulting in.Violation of TS 3.5. The licensee-responded to this violation by a letter dated July 27, 1990. The inspector reviewed'the I&E training package required to be read by all supervisors/crews. All signoffs indicating receipt of training were completed by September 5, 1990. The corrective actions are considered adequat (Closed) Violation 50-270/90-33-01: Failure to maintain the emergency feedwater system in accordance with OP/2/A/110 The Licensee responded to this violation by aletter dated January 9, 1991. The inspectors reviewed the corrective actions identifie (Open) URI 269,270,287/90-30-01: Clarification of T.S. 3. This Unresolved Item involves the clarification of TS 3.3.1, which stipulates the number of HPI pumps required to be operable when single failure criteria are considered. The licensee expects to submit a revised TS after receipt of an analysis from Babcock and Wilcox, (B&W). The target date for this submittal is June, 199 This item will remain open until the TS is submitte (Open) URI 269,270,287/90-30-02t Clarification of T.S. 3.4. This Unresolved Item involves the licensee's plans to clarify TS 3.4.1.a. In its present form, the TS requires that three, Emergency Feedwater (EFW) pumps and associated circuitry be operable prior to exceeding 250 degrees. The licensee's procedures and practices allow escalation above 250 degrees with the EFW pumps in Manual control, and operator action to start the pumps is acceptabl The inspectors believe that TS requires the pumps to.be in Automatic, which obviates the need for operator action. In the TS's present form, -as interpreted by the licensee, EFW can be left in Manual control for an indefinite period of time. The licensee presently,plans to resubmit TS 3.4.1.a by mid year 199 This item will remain open until the TS is-submitte (Open) IFI 269,270,287/90-30-03: Review IST Criteria for pump Testin This Inspector Followup Item involves apparent differences between the licensee's Inservice Test (IST) criteria for pump testing and the standing Section XI. of the ASME Code. At the present time, the licensee is awaiting review and approval by the NRC of their current IST program submitted on May 27, 1992. That review expected to be complete in early 1993. This item will remain open until the program is reviewed and approved by the NR (Open) IFI 50-269,270,287/90-34-02: Long Term Resolution of RBCU Foulin The licensee intends to submit a TS change to implement surveillance requirements to monitor RBCU performance. This item will remain open until the TS change is submitte (Open) Licensee Event Report (LER) 50-269/90-04: Unanticipated System Interaction During Undervoltage Condition In The 230KV

Switchyard Results In Failure to Comply With Technical Specification The LER was issued on April 30, 1990. The inspectors reviewed the licensee's planned corrective actions. The corrective action included a Technical Specification revisi6n to clarify the effect of degraded voltage and the use of the external grid protection system..This item will remain open pending completion of all corrective action.

(Open) Licensee Event Report (LER) 50-269/90-14: Equipment Malfunction and Management Deficiency Result in TS Violations on Core Flood Tank The LER associated with the Core Flood tanks was issued on October 8, 1990. The inspector reviewed the licensee's planned

'corrective actions. The modification of the level instruments on the Unit.1 Core Flood tanks is currently scheduled to be performed during the next refueling outage beginning December 199 Pending the modification, this LER remains ope..

Exit Interview (30703)

The inspection.scope and findings were summarized on December 4, 1992, with those persons indicated in paragraph 1 above. The, inspectors described the areas inspected and discussed in detail the inspection findings. The licensee did not identify.as proprietary any of th material provided to or reviewed by the inspectors during this inspectio Item Number Description/Reference Paragraph 269,270,287/92-27-01 Unresolved Item - Non-Safety Related Power Supplies To The LPI Cooler Throttle Valves (Paragraph 5)