IR 05000254/2017004

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Errata - Quad Cities Nuclear Power Station, Units 1 and 2 - NRC Integrated Inspection Report 05000254/2017004; 05000265/2017004; 07200053/2017001 and Emergency Preparedness Annual Inspection Report 05000254/2017501; 05000265/2017501
ML18047A566
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/16/2018
From: Karla Stoedter
NRC/RGN-III/DRP/RPB1
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2017001, IR 2017004, IR 2017501
Download: ML18047A566 (47)


Text

February 16, 2018

SUBJECT:

ERRATAQUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2NRC INTEGRATED INSPECTION REPORT 05000254/2017004; 05000265/2017004; 07200053/2017001 AND EMERGENCY PREPAREDNESS ANNUAL INSPECTION REPORT 05000254/2017501; 05000265/2017501

Dear Mr. Hanson:

The U.S. Nuclear Regulatory Commission (NRC) identified an administrative error in NRC Inspection Report 05000254/2017004; 05000265/2017004; 05000254/2017501; and 05000264/2017501 (ML18025B418), dated January 25, 2018. Specifically, the cover letter subject line and report body did not include the independent spent fuel storage installation inspection report number. As a result, the NRC has reissued the report in its entirety with the correct inspection report numbers included. This letter, its enclosure, and your response (if any)

will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Karla Stoedter, Chief Branch 1 Division of Reactor Projects Docket Nos. 50-254; 50-265;72-053 License Nos. DPR-29; DPR-30; Enclosure:

IR 05000254/2017004; 05000265/2017004; 07200053/2017001; 05000254/2017501; 05000265/2017501 cc: Distribution via LISTSERV

SUMMARY

Inspection Report 05000254/2017004, 05000265/2017004; 10/01/2017 - 12/31/2017; 07200053/2017001; 06/27/2017 - 12/31/2017; 05000254/2017501, 05000265/2017501; 01/01/2017-12/31/2017; Quad Cities Nuclear Power Station, Units 1 and 2; Routine Integrated Inspection Report.

This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors. The significance of inspection findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," dated April 29, 2015. Cross-cutting aspects are determined using IMC 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6.

NRC-Identified

and Self-Revealed Findings No findings were identified during this inspection.

REPORT DETAILS

Summary of Plant Status

Unit 1 The unit operated at or near full power from October 1 to October 30, 2017. On October 30, 2017, operators reduced power to 68.5 percent core thermal power in response to an unanticipated automatic closure of main turbine control valve number 1. Following repairs to a loose electro-hydraulic control (EHC) system servo cable connection, the unit was returned to full power on October 31, 2017. On November 16, 2017, operators reduced power to 68 percent core thermal power to respond to unanticipated alarms and impending closure of main turbine control valve number 1. Following repairs, which included lock-wire installation on all EHC system servo cable connections to turbine control valves, the unit was returned to full power on November 17, 2017, and remained at or near full power through the end of the inspection period. Operating at or near full power includes planned power reductions for turbine testing, control rod pattern adjustments, and other short-term power changes as requested by the transmission system operator.

Unit 2 The unit operated at or near full power for the entire inspection period with the exception of planned power reductions for turbine testing, control rod pattern adjustments and other short-term power changes as requested by the transmission system operator.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity, Emergency Preparedness

1R01 Adverse Weather Protection

Readiness for Impending Adverse WeatherFish Intrusion in the Intake Bay and the Crib House

a. Inspection Scope

During the week of December 18, 2017, the inspectors observed the licensees activities associated with readiness and corrective actions in response to an unusual amount of Gizzard Shad, which had infiltrated the stations intake bay, and affected the Unit 2 traveling water screens in the crib house and also had a noticeable effect on the Unit 2 main condenser differential pressure. The inspectors observed pre-job, pre-shift, and control room briefings to determine whether the briefings met licensee standards. The inspectors reviewed licensee procedures for responding to traveling screen high differential pressure alarms and procedures for directing reversal of flow to the main condenser. The inspectors also discussed potential compensatory measures with control room personnel. Finally, the inspectors periodically reviewed licensee activities and data collection as specified by licensee procedures to determine whether the fish intrusion and associated effects were being adequately monitored. The inspectors also reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather/environmental issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures.

Documents reviewed are listed in the Attachment to this report.

This activity constituted one readiness for impending adverse weather condition sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

The inspectors selected these systems based on their risk significance relative to the Reactor Safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.

The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.

The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

These activities constituted three partial system walkdown samples as defined in IP 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection

Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • Fire Zone (FZ) 5.0, Unit 2 Turbine Building, Elevation 595-0, Safe Shutdown Pump Room;
  • FZ 11.1.4, Unit 2 Reactor Building, Elevation 544-0, HPCI Pump Room;
  • FZ 1.1.1.1, Unit 1 Turbine Building, Elevation 5950, Diesel Generator Room; and
  • FZ 1.1.2.1, Unit 1 Reactor Building, Elevation 5540, Top of Torus Area.

The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings were identified.

Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On September 26 and October 4, 2017, the inspectors observed two fire brigade activations for a report of smoke in cabling for the Unit 1 motor control center (MCC)18/19-5 and a report of smoke coming from the Unit 2 condensate pit man-lift, respectively. Based on these observations, the inspectors evaluated the readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee staff identified deficiencies openly, discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions. Specific attributes evaluated were:

  • proper wearing of turnout gear and self-contained breathing apparatus;
  • proper use and layout of fire hoses;
  • employment of appropriate firefighting techniques;
  • sufficient firefighting equipment brought to the scene;
  • effectiveness of fire brigade leader communications, command, and control;
  • search for victims and propagation of the fire into other plant areas;
  • smoke removal operations;
  • utilization of pre-planned strategies;
  • adherence to the pre-planned drill scenario; and
  • drill objectives.

Documents reviewed are listed in the Attachment to this report.

These activities constituted one annual fire protection inspection sample as defined in IP 71111.05-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program

Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On November 7, 2017, the inspectors observed two crews of licensed operators in the plants simulator during licensed operator requalification training. The inspectors verified that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification (LOR)program simulator sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation during Periods of Heightened Activity or Risk

(71111.11Q)

a. Inspection Scope

On October 31, 2017, the inspectors observed operators raise power from approximately 75 percent to full (100 percent) core thermal power on Unit 1 following an emergent load reduction due to a spurious closure of turbine control valve number 1.

On December 11, 2017, the inspectors observed operators perform a pre-job brief and secure the Unit 2 B stator cooling water pump to support an emergent pump replacement.

During the week of December 17, 2017, the inspectors observed operators in the control room, on several occasions, during the fish intrusion event that is discussed in Section 1R01, which included multiple main condenser flow reversals.

These were activities that required heightened awareness or were related to increased risk. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board and equipment manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions.

The performance in these areas was compared to pre-established operator action expectations, procedural compliance, and task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

.3 Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the Annual Operating Test and the Biennial Written Examination administered by the licensee from October 9, 2017, through November 17, 2017, required by Title 10 of the Code of Federal Regulations (CFR), Part 55.59(a). The results were compared to the thresholds established in IMC 0609, Appendix I, Licensed Operator Requalification Significance Determination Process (SDP), to assess the overall adequacy of the licensees Licensed Operator Requalification Training (LORT) Program to meet the requirements of 10 CFR 55.59. (02.02)

This inspection constituted one annual licensed operator requalification examination results sample as defined in IP 71111.11-05.

b. Findings

No findings were identified.

.4 Biennial Review

a. Inspection Scope

The following inspection activities were conducted during the weeks of October 9 and October 16, 2017, to assess:

(1) the effectiveness and adequacy of the facility licensees implementation and maintenance of its systems approach to training (SAT)based LORT Program put into effect to satisfy the requirements of 10 CFR 55.59;
(2) conformance with the requirements of 10 CFR 55.46 for use of a plant referenced simulator to conduct operator licensing examinations and for satisfying experience requirements; and
(3) conformance with the operator license conditions specified in 10 CFR 55.53. The documents reviewed are listed in the Attachment to this report.
  • Licensee Requalification Examinations (10 CFR 55.59(c); SAT Element 4 as Defined in 10 CFR 55.4): The inspectors reviewed the licensees program for development and administration of the LORT biennial written examination and annual operating tests to assess the licensees ability to develop and administer examinations that are acceptable for meeting the requirements of 10 CFR 55.59(a).

- The inspectors conducted a detailed review of one biennial requalification written examination versions to assess content, level of difficulty, and quality of the written examination materials. (02.03)

- The inspectors conducted a detailed review of ten job performance measures and four simulator scenarios to assess content, level of difficulty, and quality of the operating test materials. (02.04)

- The inspectors observed the administration of the annual operating test to assess the licensees effectiveness in conducting the examination(s),including the conduct of pre-examination briefings, evaluations of individual operator and crew performance, and post-examination analysis. The inspectors evaluated the performance of one crew in parallel with the facility evaluators during two dynamic simulator scenarios, and evaluated various licensed crew members concurrently with facility evaluators during the administration of several job performance measures. (02.05)

- The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the last requalification examinations and the training planned for the current examination cycle to ensure that they addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The inspectors reviewed remedial training procedures and individual remedial training plans. (02.07)

  • Conformance with Examination Security Requirements (10 CFR 55.49):

The inspectors conducted an assessment of the licensees processes related to examination physical security and integrity (e.g., predictability and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.

The inspectors observed the implementation of physical security controls (e.g., access restrictions and simulator I/O controls) and integrity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition)throughout the inspection period. (02.06)

  • Conformance with Operator License Conditions (10 CFR 55.53): The inspectors reviewed the facility licensee's program for maintaining active operator licenses and to assess compliance with 10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the process for tracking on-shift hours for licensed operators, and which control room positions were granted watch-standing credit for maintaining active operator licenses. Additionally, medical records for seven licensed operators were reviewed for compliance with 10 CFR 55.53(I). (02.08)
  • Conformance with Simulator Requirements Specified in 10 CFR 55.46:

The inspectors assessed the adequacy of the licensees simulation facility (simulator) for use in operator licensing examinations and for satisfying experience requirements. The inspectors reviewed a sample of simulator performance test records (e.g., transient tests, malfunction tests, scenario based tests, post-event tests, steady state tests, and core performance tests), simulator discrepancies, and the process for ensuring continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The inspectors reviewed and evaluated the discrepancy corrective action process to ensure that simulator fidelity was being maintained. Open simulator discrepancies were reviewed for importance relative to the impact on 10 CFR 55.45 and 55.59 operator actions as well as on nuclear and thermal hydraulic operating characteristics. (02.09)

  • Problem Identification and Resolution (10 CFR 55.59(c); SAT Element 5 as Defined in 10 CFR 55.4): The inspectors assessed the licensees ability to identify, evaluate, and resolve problems associated with licensed operator performance (a measure of the effectiveness of its LORT Program and their ability to implement appropriate corrective actions to maintain its LORT Program up to date). The inspectors reviewed documents related to licensed operator performance issues (e.g., licensee condition/problem identification reports including documentation of plant events and review of industry operating experience from previous 2 years). The inspectors also sampled the licensees quality assurance oversight activities, including licensee training department self-assessment reports. (02.10)

This inspection constituted one Biennial LOR Program inspection sample as defined in IP 71111.11-05.

b. Findings

Introduction:

While performing an assessment of the licensees processes related to examination physical security and integrity (e.g. predictability and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests, the inspectors identified that Quad Cities 2015 LOR written examinations were duplicated from the 2013 LOR examinations, that 2017 LOR written examinations were duplicated from the 2015 LOR examinations, and that four individuals were administered the same written examinations from the previous exam cycle.

Description:

The inspectors identified that, with few exceptions, the licensee had duplicated or reused questions from the 2015 written exam when they created the 2017 written exam. The licensee created six LOR written exam versions (i.e., A-F), one for each crew. For the 2017 biennial exam, the licensee essentially swapped exam versions from 2015 that were given to each crew (i.e., the 2015 Version A was given to crew B in 2017 and Version B was given to crew A, etc.). The inspectors noted that no crew received the same exam version in 2017 as they did in 2015. However, due to crew personnel adjustments/realignments, the inspectors requested the licensee to investigate if, and how many, operators were going to receive the same exam in 2017 as in 2015. The licensee identified that one reactor operator had already taken the same exam in 2017 that they were given in 2015. In addition, the licensee also identified that two additional licensed operators were scheduled to take the same exam they had taken in 2015, but they had not yet been given the exam due to the exam schedule. After discussing the issue and concern with the inspectors, the licensee decided to administer those two individuals different exam versions to which they had not been previously exposed. In addition, the inspectors inquired how long the particular set of exam versions had been reused and swapped among the crews (i.e., before 2015). The licensee reviewed biennial written exams in 2013 and 2011 and determined the exam content was different and stated, there was no predictable pattern in exam versions.

After reviewing all of the 2013 exam versions, the inspectors identified that three versions were a mixture of questions between reused and new questions. For example, 2013 Version A was a mixture of questions of 2015 exam Versions C and D and two unique questions. The 2013 Version B was a mixture of 2015 Version C and D and seven unique questions. The 2013 Version F was a mixture of 2015 D and F and five unique questions. The three remaining versions from 2013 were replicated in 2015, but given to different crews. The inspectors requested the licensee determine the number of personnel that took the same exam in 2015 as in 2013, and the licensee identified three individuals who were given the same exam in 2013 and 2015 (two senior reactor operators and one reactor operator).

The inspectors are considering this issue to be an unresolved item (URI) concerning whether the repeated use of a biennial written examination for sequential requalification programs (consecutive 24 month periods), and the resulting predictability induced to the examination process, constitutes a violation of 10 CFR 55.49, Integrity of Examinations and Tests. The inspectors have requested the licensee provide the written examinations in question to the inspectors for further review. The inspectors will review individual questions of the written examinations in order to determine if there were sufficient differences between the examinations to characterize the examinations as either different or similar. The results of the review will be used to determine if a violation of 10 CFR 55.49 requirements exists. (URI 05000254/2017004-01; 05000265/2017004-01: Repeat Use of Written Exams during Licensed Operator Requalification Examinations)

1R12 Maintenance Effectiveness

Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk-significant systems:

The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components/functions classified as (a)(2), or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples defined in IP 71111.12-05.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • Work Week 17-40-04: Unit 1/2 EDG system extended limiting condition for operation due to emergent work activities and planned Unit 2 core spray system maintenance;
  • Work Week 17-42-06: Unit 2 EDG system planned maintenance, planned secondary containment breaches resulting in both units online risk change to yellow, and Unit 2 125 Vdc battery charger load test;
  • Work Week 17-51-02: Unit 1 1A 125 Vdc battery charger system emergent maintenance, and Unit 2 fish intrusion in intake bay.

These activities were selected based on their potential risk significance relative to the Reactor Safety cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents reviewed during this inspection are listed in the Attachment to this report.

This inspection constituted four maintenance risk assessments and emergent work control samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments

Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • IR 4062552: B Train CREV [control room emergency ventilation] Superheat Value High;
  • IR 4062754: 1A Core Spray Motor Bearing Oil Issue;
  • IR 4066290: 1A SBLC Pump Accumulator Schraeder Valve is Stuck Open;
  • IR 4072162: Unit 1 HPCI Did Not Trip During QCOS 2300-05;
  • IR 4077502 and IR 4081377: MCC 18/19-5 Overvoltage Relay Target Lit (partial sample); and
  • IR 4078677: EO ID [Equipment Operator Identified], Local Control Switch Would Not Start the SSMP and IR 4078579: SSMP Reserve Feed MCR [Main Control Room] Switch Will Not Close.

The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensees evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Documents reviewed are listed in the to this report.

The inspectors documented one partial operability sample related to MCC 18/19-5 over-voltage relay. The inspection of this sample continued into the next inspection period.

This operability inspection constituted six samples as defined in IP 71111.15-05.

b. Findings

No findings were identified.

1R18 Plant Modifications

Plant Modifications

a. Inspection Scope

The inspectors reviewed the following modifications:

  • Engineering Change 619131: U-1 HPCI Signal Converter Output Failed Alarm Bypass, Revision 0; and
  • Engineering Change 20370: Motor Control Center 18/19-5 Protective Relay Modification.

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the operability or availability of the affected systems. The inspectors, as applicable, observed ongoing and completed work activities to ensure that the modifications were installed as directed and consistent with the design control documents; the modifications operated as expected; post-modification testing adequately demonstrated continued system operability, availability, and reliability; and that operation of the modifications did not impact the operability of any interfacing systems. As applicable, the inspectors verified that relevant procedure, design, and licensing documents were properly updated. Lastly, the inspectors discussed the plant modification with operations, engineering, and training personnel to ensure that the individuals were aware of how the operation with the plant modification in place could impact overall plant performance. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one temporary modification sample and one permanent plant modification sample as defined in IP 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • B CREV operability test following planned maintenance;
  • Unit 1/2 EDG system testing and calibration following governor booster pump and relay replacements and other 2-year planned maintenance;
  • A SBGT auto start test, following relay replacement;
  • Unit 1 station blackout diesel generator system post-maintenance testing following 2-year planned maintenance activities;
  • Unit 1 HPCI pump operability test, following solenoid valve SV 1-2301-8 replacement;
  • Unit 2 Division I turbine first stage low pressure above setpoint calibration and functional test, following pressure switch 2-0504-A replacement;
  • SSMP system operability test following planned maintenance; and
  • Unit 2 station blackout diesel generator system post-maintenance testing following 2-year planned maintenance.

These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test documentation was properly evaluated. The inspectors evaluated the activities against TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted eight post-maintenance testing samples as defined in IP 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing

Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • QCOS 7000-08: U2 SBGT Initiation Logic Test (Routine);
  • QCOS 1400-07: Core Spray Pump Comprehensive/Performance Test (In-Service Test); and

The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:

  • did preconditioning occur;
  • the effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis;
  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was in accordance with TSs, the USAR, procedures, and applicable commitments;
  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the system design basis;
  • where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
  • where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
  • where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  • prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
  • equipment was returned to a position or status required to support the performance of its safety functions; and
  • all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two routine surveillance testing samples and one in-service test sample as defined in IP 71111.22, Sections-02 and-05.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The regional inspectors performed an in-office review of the latest revisions to the Emergency Plan, Emergency Action Levels (EALs), and EAL Bases document to determine if these changes decreased the effectiveness of the Emergency Plan.

The inspectors also performed a review of the licensees 10 CFR 50.54(q) change process, and Emergency Plan change documentation to ensure proper implementation for maintaining Emergency Plan integrity.

The NRC review was not documented in a safety evaluation report, and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection. The specific documents reviewed during this inspection are listed in the Attachment to this report.

This EAL and Emergency Plan Change inspection constituted one sample as defined in IP 71114.04-06.

b. Findings

No findings were identified.

1EP6 Drill Evaluation

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on November 8, 2017, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the Operations Support Center and Technical Support Center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare any inspector-observed weaknesses with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in IP 71114.06-05.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety, Occupational Radiation Safety

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls

Radiological Work Planning (02.02)

a. Inspection Scope

The inspectors compared the results achieved with the intended dose established in the As-Low-As-Reasonably-Achievable (ALARA) planning. The inspectors compared the person-hour estimates provided by work groups to the radiation protection group with the actual work activity time results, and evaluated the accuracy of these time estimates.

The inspectors evaluated the reasons for any inconsistencies between intended and actual work activity doses.

The inspectors evaluated whether post-job reviews were conducted to identify lessons learned and entered into the licensees CAP.

These inspection activities supplemented those documented in NRC Integrated Inspection Report 05000254/2016002; 05000265/2016002 and constituted one complete sample as defined in IP 71124.02-05.

b. Findings

No findings were identified.

Verification of Dose Estimates and Exposure Tracking Systems (02.03)

a. Inspection Scope

The inspectors assessed whether the assumptions and basis for the current annual collective exposure estimate were reasonably accurate. The inspectors assessed source term reduction effectiveness and reviewed applicable procedures for estimating exposures from specific work activities.

The inspectors reviewed the assumptions and bases in ALARA work planning documents for selected activities and verified that the licensee has established measures to track, trend, and if necessary to reduce, occupational doses for ongoing work activities.

The inspectors determined whether a dose threshold criteria was established to prompt additional reviews and/or additional ALARA planning and controls and evaluated the licensees method of adjusting exposure estimates, or re-planning work, when unexpected changes in scope or emergent work were encountered. The inspectors determined if adjustments to exposure estimates were based on sound radiation protection and ALARA principles or if they are just adjusted to account for failures to control the work. The inspectors evaluated whether there was sufficient station management review and approval of adjustments to exposure estimates and that the reasons for the adjustments were justifiable.

The inspectors reviewed selected occasions with inconsistent or incongruent results from the licensees intended radiological outcomes to determine whether the cause was attributed to a failure to adequately plan work activities, or failure to provide sufficient management oversight of in-plant work activities, or failure to conduct the work activity without significant rework, or failure to implement radiological controls as planned.

These inspection activities constituted one complete sample as defined in IP 71124.02-05.

b. Findings

No findings were identified.

Implementation of As-Low-As-Reasonably-Achievable and Radiological Work Controls (02.04)

a. Inspection Scope

The inspectors compared the radiological results achieved with the intended radiological outcomes and verified that the licensee captured lessons learned for use in the next outage.

These inspection activities supplemented those documented in NRC Integrated Inspection Report 05000254/2016002; 05000265/2016002 and 05000254/2017001; 05000265/2017001 constituted one complete sample as defined in IP 71124.02-05.

b. Findings

No findings were identified.

Problem Identification and Resolution (02.06)

a. Inspection Scope

The inspectors reviewed self-assessments and/or audits performed of the ALARA program and determined if these reviews identified problems or areas for improvement.

The inspectors assessed whether problems associated with ALARA planning and controls were being identified by the licensee at an appropriate threshold and properly addressed for resolution.

These inspection activities constituted one complete sample as defined in IP 71124.02-05.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation

Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors assessed select portable survey instruments that were available for use for current calibration and source check stickers, and instrument material condition and operability.

The inspectors observed licensee staff demonstrate performance checks of various types of portable survey instruments. The inspectors assessed whether high-range instruments responded to radiation on all appropriate scales.

The inspectors walked down area radiation monitors and continuous air monitors to determine whether they were appropriately positioned relative to the radiation sources or areas they were intended to monitor. The inspectors compared monitor response with actual area conditions for selected monitors.

The inspectors assessed the functional checks for select personnel contamination monitors, portal monitors, and small article monitors to verify they were performed in accordance with the manufacturers recommendations and licensee procedures.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

Calibration and Testing Program (02.03)

a. Inspection Scope

The inspectors assessed laboratory analytical instruments used for radiological analyses to determine whether daily performance checks and calibration data indicated that the frequency of the calibrations was adequate and there were no indications of degraded instrument performance. The inspectors assessed whether appropriate corrective actions were implemented in response to indications of degraded instrument performance.

The inspectors reviewed the methods and sources used to perform whole body count functional checks before daily use and assessed whether check sources were appropriate and aligned with the plants isotopic mix. The inspectors reviewed whole body count calibration records since the last inspection and evaluated whether calibration sources were representative of the plant source term and that appropriate calibration phantoms were used. The inspectors looked for anomalous results or other indications of instrument performance problems.

Inspectors reviewed select containment high-range monitor calibration and assessed whether an electronic calibration was completed for all range decades, with at least one decade at or below 10 rem/hour calibrated using an appropriate radiation source, and calibration acceptance criteria was reasonable.

The inspectors reviewed select monitors used to survey personnel and equipment for unrestricted release to assess whether the alarm setpoints were reasonable under the circumstances to ensure that licensed material was not released from the site. The inspectors reviewed the calibration documentation for each instrument selected and discussed the calibration methods with the licensee to determine consistency with the manufacturers recommendations.

The inspectors reviewed calibration documentation for select portable survey instruments, area radiation monitors, and air samplers. The inspectors reviewed detector measurement geometry and calibration methods for portable survey instruments and area radiation monitors calibrated onsite and observed the licensee demonstrate use of the instrument calibrator. The inspectors assessed whether appropriate corrective actions were taken for instruments that failed performance checks or were found significantly out of calibration, and that the licensee had evaluated the possible consequences of instrument use since the last successful calibration or performance check.

The inspectors reviewed the current output values for instrument calibrators. The inspectors assessed whether the licensee periodically measured calibrator output over the range of the instruments used with measuring devices that have been calibrated by a facility using National Institute of Standards and Technology traceable sources and corrective factors for these measuring devices were properly applied in its output verification.

The inspectors reviewed the licensees Title 10 of the Code of Federal Regulations, Part 61, Licensing Requirements for Land Disposal of Radioactive Waste, source term to assess whether calibration sources used were representative of the types and energies of radiation encountered in the plant.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

Problem Identification and Resolution (02.04)

a. Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring instrumentation were being identified by the licensee at an appropriate threshold and were properly addressed for resolution. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involve radiation monitoring instrumentation.

These inspection activities constituted one complete sample as defined in IP 71124.05-05.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program

Groundwater Protection Initiative Implementation (02.03)

a. Inspection Scope

The inspectors reviewed leak and spill events and Title 10 of the Code of Federal Regulations, Part 50.75(g) records and assessed whether the source of the leak or spill was identified and appropriately mitigated.

These inspection activities supplemented those documented in NRC Integrated Inspection Report 05000254/2017003; 05000265/2017003 and constituted one complete sample as defined in IP 71124.07-05.

b. Findings

No findings were identified

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator (PI) for Quad Cities Nuclear Power Station, Units 1 and 2, for the period from the third quarter 2016 through the third quarter 2017. The inspectors used PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the PI data reported during those periods. The inspectors reviewed the licensees reactor coolant system chemistry samples, TS requirements, IRs, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals. The inspectors also reviewed the licensees IR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two reactor coolant system specific activity samples as defined in IP 71151-05.

b. Findings

No findings were identified.

Mitigating Systems Performance IndexHigh Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the mitigating systems performance index (MSPI)high pressure injection systems PI for Quad Cities Nuclear Power Station, Units 1 and 2, for the period from the fourth quarter 2016 through the third quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, IRs, MSPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2016, through September 30, 2017, to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees IR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI high pressure injection system samples as defined in IP 71151-05.

b. Findings

No findings were identified.

Mitigating Systems Performance IndexHeat Removal Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPIheat removal systems PI for Quad Cities Nuclear Power Station, Units 1 and 2, for the period from the fourth quarter 2016 through the third quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, IRs, event reports, MSPI derivation reports, and NRC integrated inspection reports for the period of October 1, 2016, through September 30, 2017, to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees IR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI heat removal systems samples as defined in IP 71151-05.

b. Findings

No findings were identified.

Mitigating Systems Performance IndexResidual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPIResidual Heat Removal System PI for Units 1 and 2 for the period from the fourth quarter 2016 through the third quarter 2017. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, IRs, MSPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2016, through September 30, 2017, to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees IR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI residual heat removal systems samples as defined in IP 71151-05.

b. Findings

No findings were identified.

Mitigating Systems Performance IndexCooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the MSPIcooling water systems PI Units 1 and 2 for the period from the fourth quarter 2016 through the third quarter 2017.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the licensees operator narrative logs, IRs, MSPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2016, through September 30, 2017, to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensees IR database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI cooling water systems samples as defined in IP 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into the licensees CAP at an appropriate threshold, adequate attention was being given to timely corrective actions, and adverse trends were identified and addressed. Some minor issues were entered into the licensees corrective action program as a result of the inspectors observations; however, they are not discussed in this report.

These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter.

b. Findings

No findings were identified.

Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the 6-month period of June 1, 2017, through November 30, 2017, although some examples expanded beyond those dates where the scope of the trend warranted.

The review also included issues documented outside the CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

This review constituted one semi-annual trend review inspection sample as defined in IP 71152.

b. Observations and Assessments The inspectors reviewed the licensees internal trend review which spanned the range of four quarters for emerging cross-cutting themes. The cross-cutting areas identified by the licensee as having been impacted over the last four quarters were work management, training, avoiding complacency, and conservative bias. The inspectors reviewed the licensees assessment which did not identify any trends/themes in the areas impacted. The inspectors verified the licensee continuously monitored cross-cutting areas for the presence of recurring themes. The inspectors review did not identify any recurring themes with equipment issues or in other areas such as work management, human performance, or problem identification and resolution that were indicative of a more significant safety issue. The inspectors also performed a more focused review of the licensees corrective action database and resolution and identification of issues associated with safety-related relays. The inspectors reviewed the database to identify if any previous relay failures could be attributed to gaps in the licensees preventative maintenance strategies and work practices. No trends/themes were identified.

c. Findings

No findings were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

(Closed) Licensee Event Report 05000265/2017-001-00: High Pressure Coolant Injection Minimum Flow Valve Failed to Open On May 15, 2017, operations personnel performed surveillance procedure QCOS 2300-05, HPCI Pump Operability Test. While securing from the test, operators tripped the HPCI turbine, and the HPCI minimum flow bypass valve failed to open on low flow. Operators attempted to manually open the minimum flow bypass valve. However, when they released the control switch, the valve returned to the closed position. Since the acceptance criteria in the surveillance procedure requires proper operation of the minimum flow valve, the licensee declared the HPCI system inoperable due to the apparent failure of the minimum flow valve to operate properly. The licensee documented the issue in IR 4011130, During HPCI S/D MO 2-2301-14 did not Auto Open. The licensees investigation identified that the HPCI pump discharge flow indicating switch had an intermittent failure that was caused by a manufacturing defect.

The defect caused the minimum flow valve to receive a sporadic continuous closed signal. The licensee replaced the flow indicating switch (FIS), retested the system, and declared HPCI operable. An engineering evaluation by the licensee discussed that the minimum flow bypass valve is designed for pump protection when other discharge line valves are closed (i.e. during testing). Therefore, in the event of a loss of coolant accident, HPCI would have still been able to perform its design safety-related function because the HPCI discharge valves to the reactor would open and no pump damage would be expected to occur. Based on the inspectors discussions with the licensee, the licensee determined that their procedure direction, to declare HPCI inoperable, may have been overly restrictive and initiated a procedure change to clarify the function of the minimum flow valve. The inspectors reviewed the licensees evaluation and did not identified a performance deficiency.

Documents reviewed are listed in the Attachment to this report. This licensee event report (LER) is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

Retraction of Event Notification No. 52955: High Pressure Coolant Injection System Inoperable The original event occurred on September 8, 2017, when the Unit 2 HPCI minimum flow valve, MO 2-2301-14, flow indicating switch, FIS 2-2354, failed to meet the TS allowable value during calibration testing using procedure QCIS 2300-10, HPCI Pump Discharge Flow Switch Calibration and Functional Test, Revision 8, and HPCI was subsequently declared inoperable. The licensee reported the event as a condition that could have prevented fulfillment of a safety function in accordance with 10 CFR 50.72(b)(3)(v)(D). Since the HPCI system is a single train system, the loss of HPCI would prevent the high pressure injection safety function that HPCI provides. The flow indicating switch, FIS 2-2354, was successfully recalibrated and HPCI was returned to Operable status approximately 10 minutes after it was found out of tolerance.

After reviewing the details of this event under IR 4050176, the licensee determined that the surveillance procedure contained an overly restrictive statement that directed operators to immediately declare the HPCI system inoperable when FIS 2-2354 fails.

This statement was in conflict with TS 3.3.5.1, Condition E, which allows 7 days to restore the HPCI FIS (instrument channel only) to an operable status prior to entry into TS 3.3.5.1, Condition H, which requires declaring HPCI inoperable immediately.

Therefore, during the period of the FIS inoperability10 minutesthe HPCI system was not required to be declared inoperable in accordance with TS. Licensee corrective actions included a revision to the procedure which would direct entry into the appropriate instrumentation TS.

The inspectors reviewed the licensees basis for the event retraction and verified that HPCI was not required to be declared inoperable at the time of the event. The inspectors noted that while the FIS failed the calibration, it would have still functioned and opened the minimum flow valve. However, it would have opened at a lower flow rate than required by the TS. The inspectors also noted that this FIS calibration surveillance failure differed from the event described in LER 05000265/2017-001 due to the failure mechanism of the FIS. The event described in that LER prevented the minimum flow valve from operating automatically or manually, and the minimum flow valve was declared inoperable during that event, again due to procedural guidance in another surveillance procedure that was later determined to be overly restrictive. No performance deficiencies were identified.

This event follow-up review constituted one sample as defined in IP 71153-05.

(Closed) Licensee Event Report 05000254/2017-003-00: Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue On September 21, 2017, the licensee identified a refrigerant leak at an expansion joint located on the discharge piping of the CREV air conditioning (AC) system compressor.

The licensee declared the refrigeration condensing unit inoperable and entered TS 3.7.5, Condition A, which required restoration of the CREV AC system within 30 days. The licensee was required to report the condition under 10 CFR 50.72/73 (a)(2)(v)(D)because the CREV AC system is a single train safety system required to mitigate the consequences of an accident. The licensee determined that the piping failure was caused by high cycle fatigue at the expansion joint, which had been in service for approximately 20 years. As a result, the licensee replaced the compressor discharge pipe fitting (expansion joint).

The licensee had experienced three compressor failures over the 20-year timespan, which were suspected to be the main causes of the increased vibrations on the piping.

Due to previous compressor modifications following the prior failures, the licensee expected the replaced fitting will continue to function beyond the life of the plant. The inspectors reviewed the licensees evaluation and corrective actions. No performance deficiencies were identified.

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA5 Other Activities

Review of Independent Spent Fuel Storage Installation Storage Pad Design (60856, Appendix A)

a. Inspection Scope

The licensee currently has an Independent Spent Fuel Storage Installation (ISFSI) pad with a capacity to store 60 casks and plans to expand the ISFSI capacity by installation of a new pad to accommodate an additional 114 casks. Title 10 of the Code of Federal Regulations (CFR) 72.212(b)(5)(ii) requires that licensees perform written evaluations, before use, which establish that cask storage pads and areas have been designed to adequately support the static and dynamic loads of the stored casks, considering potential amplification of earthquakes through soil-structure interaction, and soil liquefaction potential or other soil instability due to vibratory ground motion.

The inspectors evaluated the licensees soil and ISFSI pad engineering design evaluations for the new pad to verify the licensees compliance with the cask Certificate of Compliance (CoC), 10 CFR Part 72 requirements, and industry standards.

The licensee was utilizing the Holtec HI-STORM 100S, Version B (218) dry cask storage system. The new reinforced concrete pad was 35 inches thick and capable of supporting 114 HI-STORM casks in a 6-by-19 array. The pad was 89 feet wide and 307.5 feet long. The licensee designed and constructed the ISFSI pad as an important-to-safety (category C) structure.

The inspectors reviewed the licensees soil investigation reports and calculations documenting the engineering properties and design soil profile of the ISFSI site based on new geotechnical investigations of the ISFSI areas combined with the data in the plant UFSAR. The inspectors reviewed documents to verify that the pad design duly addressed geological and hydrological considerations using the information from the earlier and the new soil investigations as applicable. The inspectors reviewed the licensees liquefaction analysis to verify seismic input and safety factors were consistent with Regulatory Guidance 1.198, Procedures and Criteria for Assessing Seismic Soil Liquefaction at Nuclear Power Plant Sites.

The inspectors reviewed documents for the generation of new seismic acceleration time histories from the seismic ground motion spectra for the reactor site to be used as inputs for the ISFSI analyses. The inspectors reviewed the soil structure interaction analysis methodology and calculations to verify adequacy of the soil/pad/cask analytical model. The inspectors reviewed the ISFSI pad structural design to verify the methodology, load factors and acceptance criteria, as well as considerations of settlements, static/dynamic and sequential/partial loadings.

The inspectors reviewed the licensees cask haul path evaluations to verify that maximum expected loads were considered in the design of the new haul path. The inspectors interviewed licensee personnel and performed walkdowns of the haul path and the ISFSI areas to verify that licensee had reviewed the haul path for the right-of-way requirements and potential interferences from nearby structures and overhead lines and that any impact on buried utilities was also addressed, as applicable.

b. Findings

No findings were identified.

On-site Fabrication of Components and Construction of an Independent Spent Fuel Storage Installation (60853)

a. Inspection Scope

The inspectors performed a walkdown of the new ISFSI pad construction site on September 26 and 27, 2017, after the licensee had performed significant earthwork and placed engineered fill for the pad, but before any concrete formwork or rebar for the pad had been placed. The inspectors observed the licensees process for setting up and performing a plate load test on the engineered fill for the ISFSI pad. The inspectors also interviewed licensee and contractor personnel to evaluate their understanding of the design and construction specifications for the ISFSI pad.

The inspectors evaluated the licensees construction activities for the new pad to verify the licensees compliance with the cask CoC, 10 CFR Part 72 requirements, the cask Final Safety Analysis Report, the ISFSI pad design specification, and applicable industry standards.

As the licensee continues the construction process for this ISFSI pad expansion into 2018 to include both rebar and concrete placement, the inspectors will continue to utilize IP 60853 to evaluate the licensees compliance. The results of this inspection will be documented in a future inspection report.

b. Findings

No findings were identified.

4OA6 Management Meetings

Exit Meeting Summary

On January 3, 2018, the inspectors presented the inspection results to Mr. H. Dodd and other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was considered proprietary.

Interim Exit Meetings Interim exits were conducted for:

  • The results of the biennial LORT program inspection were presented to Mr. H. Dodd, Plant Manager, and other licensee staff members on October 20, 2017.
  • The inspectors presented the characterization of a potential enforcement issue (URI) identified during the biennial LORT inspection to Mr. E. Pannell, Training Manager, and other licensee staff members via telephone conference on January 2, 2018.
  • The results of the ISFSI pad inspection were presented to Mr. C. Alguire and other members of the licensee staff via telephone conference on November 20, 2017.
  • The results for the radiation safety program review inspection were presented with Mr. H. Dodd, Plant Manager, on December 14, 2017.

The inspectors confirmed that none of the potential report inputs discussed were considered proprietary. Proprietary material received during the inspections was returned to the licensee.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

H. Dodd, Plant General Manager
M. Anderson, Maintenance Director
J. Bries, Operations Director
T. Bell, Engineering Director
D. Collins, Radiation Protection Manager
J. Cox, Shift Operations Superintendent
R. Craddick, Organizational Effectiveness Manager
M. Humphrey, Regulatory Assurance
T. Petersen, Regulatory Assurance
J. Roos, System Engineering Electrical Manager
T. Wojcik, Engineering Manager
J. Woolridge, Chemistry Manager

U.S. Nuclear Regulatory Commission

L. Kozak, Acting Chief, Reactor Projects Branch 1
R. Murray, Senior Resident Inspector
K. Carrington, Resident Inspector

Illinois Emergency Management Agency (IEMA)

C. Mathews, IEMA
C. Settles, IEMA

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000254/2017004-01; URI Repeat Use of Written Exams during Licensed Operator
05000265/2017004-01 Requalification Examinations (Section 1R11)

Closed

05000265/2017001-00 LER High Pressure Coolant Injection Minimum Flow Valve Failed to Open (Section 4OA3.1)
05000254/2017003-00 LER Control Room Emergency Ventilation Air Conditioning Piping Refrigerant Leak Due to High Cycle Fatigue (Section 4OA3.3)

Discussed

None.

LIST OF DOCUMENTS REVIEWED