IR 05000220/2024004

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Integrated Inspection Report 05000220/2024004 and 05000410/2024004 and Independent Spent Fuel Storage Installation Inspection Report 07201036/2024004
ML25043A045
Person / Time
Site: Nine Mile Point  
Issue date: 02/12/2025
From: Jason Schussler
Division of Operating Reactors
To: Rhoades D
Constellation Energy Generation
References
IR 2024004
Download: ML25043A045 (1)


Text

February 12, 2025

SUBJECT:

NINE MILE POINT NUCLEAR STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000220/2024004 AND 05000410/2024004 AND INDEPENDENT SPENT FUEL STORAGE INSTALLATION INSPECTION REPORT 07201036/2024004

Dear David Rhoades:

On December 31, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Nine Mile Point Nuclear Station, Units 1 and 2. On February 6, 2025, the NRC inspectors discussed the results of this inspection with Carl Crawford, Plant Manager, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Jason E. Schussler, Chief Projects Branch 1 Division of Operating Reactor Safety Docket Nos. 05000220, 05000410, and 07201036 License Nos. DPR-63 and NPF-69

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000220, 05000410, and 07201036

License Numbers:

DPR-63 and NPF-69

Report Numbers:

05000220/2024004, 05000410/2024004, and 07201036/2024004

Enterprise Identifier: I-2024-004-0039

I-2024-001-0104

Licensee:

Constellation Energy Generation, LLC

Facility:

Nine Mile Point Nuclear Station Units 1 and 2

Location:

Oswego, NY

Inspection Dates:

October 1, 2024 to December 31, 2024

Inspectors:

C. Kline, Senior Resident Inspector

B. Sienel, Resident Inspector

C. Borman, Health Physicist

R. Chan, Operations Engineer

M. Donithan, Senior Operations Engineer

T. Fish, Senior Operations Engineer

C. Hargest, Health Physicist

M. Henrion, Senior Project Engineer

Y. Kim, Senior Structural Engineer

K. Mangan, Senior Reactor Inspector

D. McHugh, Reactor Inspector

L. Sinclair, Operations Engineer

G. Stock, Reactor Operations Engineer

T. Winkel, Health Physicist

G. Zhao, Structural Engineer

Approved By:

Jason E. Schussler, Chief

Projects Branch 1

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Nine Mile Point Nuclear Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000410/2024-002-00 Unit 2 Automatic Reactor Scram on Turbine Trip due to Failed Breaker 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On October 25, 2024, operators reduced power to 66 percent for a planned rod pattern adjustment and turbine valve testing. The unit was returned to rated thermal power on October 27, 2024. On October 30, 2024, operators reduced power to 76 percent in response to indications of a fuel element defect. Operators increased reactor power to 90 percent following power suppression testing on November 6, 2024. On December 6, 2024, operators reduced power to 70 percent for a planned rod pattern adjustment. Power was restored to 90 percent the following day. Subsequently, several power adjustments of less than 1 percent were made in response to the fuel defect and Unit 1 completed the inspection period at 89 percent rated thermal power.

Unit 2 began the inspection period at rated thermal power. On November 23, 2024, operators reduced power to 64 percent for a planned rod pattern adjustment and feedwater pump realignment. Power was returned to rated thermal power on November 24, 2024, where it remained for the rest of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures for the following systems: fire protection, reactor building ventilation, FLEX equipment, and circulating water on December 16, 2024.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 high pressure core spray system on October 22, 2024
(2) Unit 1 emergency diesel generator (EDG) 103 on October 22, 2024
(3) Unit 1 11 liquid poison system on October 29, 2024

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) Unit 2 standby liquid control system on November 19, 2024

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 2 turbine building 306', fire area 50, on October 9, 2024
(2) Unit 2 control building 288', fire area 24, on October 16, 2024
(3) Unit 1 reactor building northeast 198' to 237' containment spray areas, fire area 1, on December 18, 2024

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) Unit 1 reactor building elevation 198' northeast corner room on December 18, 2024

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Unit 2 Division II standby diesel generator jacket water heat exchanger 2EGS*E2B

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (2 Samples)

(1) The inspectors reviewed and evaluated the Unit 1 licensed operator examination failure rates for the requalification annual operating exams administered October - November 2024 and the biennial written examinations administered October - November 2024.
(2) The inspectors reviewed and evaluated the Unit 2 licensed operator examination failure rates for the requalification annual operating exam completed on November 14, 2024.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the Unit 1 licensed operator biennial requalification written examinations administered October - November 2024.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the Unit 1 annual requalification operating test administered week of October 28, 2024.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by Title 10 of the Code of Federal Regulations (10 CFR) Part 55.59(a)(2) and that the facility licensee is effectively evaluating its licensed operators for mastery of training objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed and evaluated Unit 1 licensed operator performance in the control room during a downpower to 66 percent for rod pattern change and turbine stop valve testing on October 25, 2024.
(2) The inspectors observed and evaluated Unit 2 licensed operator performance in the control room during a downpower to 62 percent for rod pattern adjustment and feed pump realignment on November 23, 2024.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed and evaluated a Unit 2 annual simulator examination with scenarios that included safety system failures, steam leaks in primary containment, and failures to scram on October 15, 2024.
(2) The inspectors observed and evaluated a Unit 1 annual simulator examination with scenarios that included pressure regulator failures, pump and valve malfunctions, a fuel element failure, and an unisolable leak into secondary containment on November 5, 2024.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended functions:

(1) Unit 2 'F' service water following failure of discharge check valve failure to close on August 29, 2024
(2) Unit 1 diesel fire pump following failure on October 8, 2024
(3) Unit 1 EDG 102 following circulating oil pump trip on October 31, 2024

Quality Control (IP Section 03.02) (2 Samples)

The inspectors evaluated the effectiveness of maintenance and quality control activities to ensure the following SSCs remain capable of performing their intended functions:

(1) Commercial grade dedication of bearing installed in the Unit 2 Division I standby diesel generator fuel oil transfer system pump 2EGF*P1C on November 17, 2024
(2) In-process controls during Unit 2 Division III standby diesel generator system outage window on November 22, 2024

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 2 elevated risk during high pressure core spray system outage window on October 21, 2024
(2) Unit 1 elevated risk during planned 102 EDG maintenance on October 22, 2024
(3) Unit 1 elevated risk during planned 12 liquid poison system maintenance on October 29, 2024
(4) Unit 2 elevated risk during planned Division II standby diesel generator maintenance on October 30, 2024
(5) Unit 2 elevated risk during planned Division III standby diesel generator maintenance on November 21, 2024

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 1 turbine stop valve 11 input to reactor protection system following failure to respond during testing on October 8, 2024
(2) Unit 1 EDG 102 following the trip of the circulating oil pump breaker on October 31, 2024
(3) Unit 2 safety relief valve 2MSS*PSV122 following increased tailpipe temperature on November 13, 2024
(4) Unit 2 Division I diesel generator room area cooler 2HVP*UC1A test failure on November 13, 2024
(5) Unit 1 emergency condenser (EC) radiation monitoring following prolonged degradation of EC radiation monitor 121 on November 19, 2024

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Permanent Modification: ECP-24-000154, Replacement of RCIC [reactor core isolation cooling] Division II Differential Pressure Transmitter

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (6 Samples)

(1) N1-PM-M9, Operation of Fire Pumps, following fuel injector replacement and governor adjustment, on October 9, 2024
(2) N1-ST-M4A, Emergency Diesel Generator 102 and PB 102 Operability Test, following planned maintenance, on October 23, 2024
(3) N1-ST-Q8B, Liquid Poison Pump 12 and Check Valve Operability Test, following planned 12 liquid poison pump preventive maintenance, on October 31, 2024
(4) N2-PM-@026, Diesel Generator Start - Division I and II, following maintenance, on November 6, 2024
(5) N2-OSP-EGS-M@001, Diesel Generator and Diesel Air Start Valve Operability Test - Division I and II, following maintenance, on November 13, 2024
(6) N2-OSP-EGS-R005, Diesel Generator Emergency Core Cooling System Start -

Division III, following planned maintenance, on November 22, 2024

Surveillance Testing (IP Section 03.01) (1 Sample)

(1) N2-OSP-EGS-M@001, Unit 2 Division I Diesel Slow Start, on November 13, 2024

Inservice Testing (IST) (IP Section 03.01) (2 Samples)

(1) N1-ST-Q6A, Containment Spray System Loop 111 Quarterly Operability Test, on October 2, 2024
(2) N2-OSP-CSH-Q@002, High Pressure Core Spray Pump and Valve Operability Test, on October 23, 2024

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1) N1-ST-Q4, Reactor Coolant System Isolation Valves Operability Test, on November 14,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07)===

(1) Unit 1 for the period of October 1, 2023 through September 30, 2024
(2) Unit 2 for the period of October 1, 2023 through September 30, 2024

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 for the period of October 1, 2023 through September 30, 2024
(2) Unit 2 for the period of October 1, 2023 through September 30, 2024

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 for the period of October 1, 2023 through September 30, 2024
(2) Unit 2 for the period of October 1, 2023 through September 30, 2024

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) Units 1 and 2 for the period of October 1, 2023 through September 30, 2024

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) Units 1 and 2 for the period of October 1, 2023 through September 30, 2024

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Issue Reports (IRs) 04774076, 04758780, and 04762854 - Review of Corrective Actions for Unit 1 Diesel Fire Pump
(2) IR 04803847 - Breaker 41M-2EXSX01 Generator Exciter Field Breaker Failure
(3) IR 04813728 - Review of Corrective Actions for Unit 1 EDG Lube Oil Pump Failures
(4) IR 04723637 - Review of Corrective Actions for Unit 2 Service Water Pump 'D' Inboard Bearing Failure

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors reviewed Constellations corrective action program to identify potential trends that might be indicative of a more significant safety issue.

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensees event reporting determinations to ensure it complied with reporting requirements.

(1) LER 05000410/2024-002-00, Unit 2 Automatic Reactor Scram on Turbine Trip due to Failed Breaker (ADAMS Accession No. ML24326A058). The inspection conclusions associated with this LER are documented in this report under Inspection Results. This LER is Closed.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60853 - Onsite Fabrication of Components and Construction of an Independent Spent Fuel Storage Installation (ISFSI)

(1) The inspectors observed and evaluated the licensees activities related to concrete placement for the expansion of their ISFSI pad, which will eventually store spent fuel previously generated by the licensee, on October 30-31,

INSPECTION RESULTS

Minor Performance Deficiency 71152A Breaker 41M-2EXSX01 Generator Exciter Field Breaker Failure

Minor Performance Deficiency: In response to operating experience from LaSalle Station, Constellation created a work order at Nine Mile Point Station, (WO) C93855815, to check the main generator field breaker for high resistance. Constellation completed the WO at Nine Mile Point Station on March 26, 2024. The inspectors noted the WO did not contain step by step instructions, specifically it did not identify the location of the resistance measurements, or the instrument to be used. Upon review the inspectors noted the acceptance criteria in the WO was greater than 150 micro ohms and a digital voltage meter was used for the measurement. The inspectors noted the appropriate acceptance criterion is less than 150 micro ohms and the appropriate instrument is a digital low resistance ohm meter as stated in preventative maintenance document N2-EPM-EXS-V553, "Main Generator/Exciter Field Breaker PM." As a result of not having specific step by step work order instructions the inspectors noted one resistance measurement was recorded as 0.09 ohms. Also, the inspectors reviewed the completed work order instructions and concluded the exact measurement location is not clearly specified. Consequently, the inspectors could not determine if a high resistance connection existed in March 2024. Notably, 6 months following these measurements and work order completion, on September 23, 2024, the field breaker failed and caught fire. The breaker failure lead in a reactor scram and the fire was extinguished by onsite personnel. The inspectors noted that no safety related components were impacted by the fire.

Following the breaker failure and fire Constellation performed a root cause evaluation (RCE). The RCE concluded that a mechanical fault internal to the breaker caused a high resistance connection to develop. The RCE provided computer plot trends which indicated that the voltage and current were within normal values up to the time of the failure. These recorded plot trends are an indication that the circuit breaker did not have a high resistance connection until just before the failure.

Maintenance procedure MA-AA-716-010-10, "Writers Guide for Maintenance Work Order Instructions," requires that work orders have step by step instructions to accomplish scope of the WO task and to identify appropriate acceptance criteria. Contrary to this, the previously cited, WO C93855815 did not provide step by step instruction or appropriate acceptance criteria to complete the scope of the WO task. Specifically, the WO only took one resistance measurement when a minimum of two was required and the acceptance criterion should have specified the requirement of less than 150 micro ohms.

Screening: The inspectors determined the performance deficiency was minor. Constellation determined that it was unlikely that a high resistance connection existed until just prior to failure of the breaker that caused the reactor scram on September 23, 2024. The conclusion is support by computer plot data noting voltage and current trends. Therefore, the performance deficiency of inaccurate work instructions and acceptance criteria was not a clear contributor to the breaker failure. This minor performance deficiency is captured in IR 04803847.

Observation: Review of Corrective Actions for Unit 1 Diesel Fire Pump 71152A The inspectors reviewed Constellations cause determination associated with the degraded performance of the Unit 1 diesel fire pump engine and evaluated the effectiveness of intermediate and long-term corrective actions that were performed following the diesel failing to start or run on multiple occasions between October 2023 and July 2024. The inspectors noted that the pump is credited as a fire suppression water source and is also credited in the probabilistic risk assessment to mitigate several accident scenarios assuming the failure of multiple safety-related equipment.

The inspectors observed that following preventive maintenance, which replaced the six engine fuel injectors in September 2023, the diesel engine failed to run on two occasions (October 2023 and March 2024) due to engine malfunction. Constellation staff determined the failures were caused by the fuel injectors. Following an investigation, Constellation staff concluded the fuel injector degraded performance was due to inadequate fuel injector refurbishment that had been performed at an offsite facility. Once identified, Constellation, using a different vendor, refurbished and witnessed testing of 18 injectors. Six injectors, chosen based on test results, were then installed in the engine. The inspectors noted that the injectors were refurbished because injectors for this engine are no longer manufactured.

After installing the injectors, Constellation implemented a condition monitoring program to monitor diesel performance. In August 2024, the engine was determined to not meet performance monitoring standards and was declared non-functional. Maintenance staff with vendor support performed engine tuning activities to restore performance. Following adjustments to the engine, on October 10, 2024, Constellation staff completed a 12-hour endurance run on the diesel fire pump with satisfactory results.

The inspectors also reviewed Constellation staffs evaluations of two additional engine-failed-to-start and/or -run events. In one case, the diesel air inlet manifold emergency close damper had repositioned closed prior to the engine start, and in the second case the air start motor failed to operate. The inspectors reviewed the causes and corrective actions associated with these failures and determined the actions corrected the condition and associated cause.

Inspectors noted that during the periods the diesel fire pump was not functional, Constellation staff opened the cross-connect between the Unit 1 and Unit 2 fire headers. This action allowed Unit 1 to credit the use of the Unit 2 fire pumps in order to comply with regulatory requirements for fire protection and to reduce overall risk for design basis events. During the inspection, the inspectors questioned if the configuration complied with fire protection standards for separate water supply sources. Constellation staff identified a potential hot short location for the motor operated valve opened as part of the compensator action. The issue was entered into the corrective action program for resolution. The inspectors determined that the fire scenario that could cause a hot short on the motor operated valve would not impact the other credited fire pump.

The inspectors reviewed the condition reports, corrective actions, and other documentation.

The inspectors noted that Constellations evaluation and corrective actions were in accordance with site procedures. The inspectors did not identify any performance deficiencies or violations as a result of this inspection.

Observation: Review of Corrective Actions for Unit 1 EDG Lube Oil Pump Failures 71152A The inspectors reviewed Constellations corrective action program evaluations and corrective actions regarding Unit 1 EDGs 102 and 103 circulating lube oil pump failures. The purpose of the pumps is to maintain a constant flow of lubricating oil throughout the EDGs when they are in standby, and in conjunction with the standby lube oil heater, to keep the lube oil warm.

They are not a support function for EDG lubrication, are not safety-related, and are not covered by technical specifications (TSs). In accordance with N1-OP-45, "Emergency Diesel Generators," if this lube oil pump is inoperable, the affected EDG remains operable as long as lube oil temperature remains above 85 degrees Fahrenheit. If sump temperatures fall below 85 degrees Fahrenheit, the EDG is inoperable.

Since 2021 there have been seven trips of the circulating lube oil pumps on EDGs 102 (four trips) and 103 (three trips). The licensee documented those trips in IRs 04427748, 04467177, 04479221, 04528148, 04673045, 04809936, and 04813728. They determined that the probable cause of the pump motor failures was a vibration-induced degradation to the motor brush holders, which restricted brush motion, resulting in arcing between the brush contact surfaces and the commutator.

After both motors were replaced with new ones in late 2022 (WOs C93841969 and C93824032), they tripped again after approximately 6 months (EDG 102) and 22 months (EDG 103). The same failure mechanism was identified in each, but with a new hypothesis: Vibration readings on the motors have always been normal, but it was noted that the pumps keep running while the EDG is running, a possible contributing factor is that the vibrations from the EDG skid are causing the brush holder degradation. In discussion with the system engineer it was determined that the original equipment vendor changed the configuration of the motors mounting plate. Proper fitting in the current configuration requires modification to the holes in the mounting plate and shimming the motor upwards in relation to the pump.

An action was established to query the vendor for pumps with a more robust design, and evaluate using a brushless direct current motor, which would eliminate motor brushes as a failure mechanism. As a compensatory measure, the licensee has established a crash cart with a new pump and motor and a planned WO to quickly respond to a motor failure on either EDG. This pre-planning should help prevent EDG TS inoperability time due to the engines lube oil cooling to below 85 degrees Fahrenheit.

The licensee also has a compensatory action to raise the temperature in the EDG rooms if a circulating lube oil pump fails. This should slow the rate of cooling of the lube oil in the engine sump, and delay TS entry, but hasnt been invoked yet, so its efficacy is unknown at this time.

The inspectors reviewed the condition reports, corrective actions, and other documentation.

The inspectors noted that Constellations evaluation and corrective actions were in accordance with site procedures. The inspectors did not identify any performance deficiencies or violations as a result of this inspection.

Observation: Breaker 41M-2EXSX01 Generator Exciter Field Breaker Failure 71152A On September 23, 2024, at 0720, with Unit 2 in mode 1 at 100 percent power, the reactor automatically scrammed due to turbine stop valve closure on a turbine trip. The scram was not complex. The turbine trip was caused from the loss of field relay actuation. The loss of field was caused by a high resistance connection on the negative poll of the main generator field breaker which resulted in a fire. The fire was extinguished by on-site personnel and did not impact any safety-related components.

The main generator field breaker provides the current path from the exciter to the main field. Field current is adjusted using the voltage regulator. Normal field current is approximately 4500 amps. Due to the large current through the field breaker, small resistance in the connections would cause a large amount of heat.

Constellation PowerLabs performed a failure analysis and concluded that the cause of the initial high resistance between the negative pole contacts is unknown. Based on the evidence, it may have been attributed to 1) low contact force due to the missing stationary contact springs; and/or 2) foreign or displaced material in the contact path.

Constellation performed an RCE. The RCE concluded that a mechanical fault internal to the breaker caused a high resistance connection to develop, ultimately resulting in loss of the generator field. Constellation provided voltage and current trends that indicate that the failure did not occur over time which supports the RCE conclusion. The corrective action to prevent recurrence is to eliminate the main generator field breaker.

The inspectors identified a minor performance deficiency associated with the prior work activities on the breaker which is documented within this report; the inspectors did not identify any additional findings or violations as a result of this inspection.

Observation: Unit 2 Service Water Pump 'D' Inboard Bearing Failure 71152A The inspectors reviewed Constellation's evaluation and corrective actions associated with failure of Unit 2 service water pump 'D' inboard bearing on December 14, 2023. Specifically, inspectors focused on the failure analysis and corrective actions completed under IR 04723637.

On December 14, 2023, operators were alerted to rising service water pump 'D' inboard bearing temperature by alarm 3601202, "Service Water Pump 1B/1D/1F Pump/Motor BRG Temp High." Operations personnel took alarm response procedure actions and field personnel reported increased seal leakage and an acrid odor in the Division II service water bay. The subsequent rise and fall of bearing temperature were consistent with bearing failure. The pump was secured and the bearing was replaced.

Subsequent material failure analysis identified foreign material (lead, iron, aluminum and silicon) in the oil, in the displaced Babbitt material, and embedded in the bearing surface. Constellation determined that the most likely source of the foreign material was from the accumulation of wear products in the oil reservoir. The wear materials were disturbed during the oil replacement preventive maintenance action which had been completed two weeks prior to bearing failure. The oil reservoir drain is approximately 1/4 inch above the bottom of the oil reservoir and complete reservoir draining is not possible without more intrusive disassembly. Access to the reservoir requires rolling out the lower bearing, a task which normally occurs every six years, during pump refurbishment by contracted personnel. To prevent reoccurrence, Constellation revised the refurbishment contracting standard to include a witness point for Constellation personnel to inspect the oil reservoir during bearing inspection. The bearing inspection is an existing quality control point conducted by Constellation personnel as part of refurbished pump receipt and is conducted at contractor facilities. The inspectors noted that the current inspection requirement assumes skill-of-the-trade as the inspection standard and would benefit from inclusion of an explicit inspection standard.

The inspectors reviewed the evaluation, extent of condition review, procedures, manufacturers failure analysis and relevant IRs, and interviewed the licensee subject matter expert on the topic. The inspectors noted that Constellations evaluation and corrective actions were in accordance with site procedures. The inspectors did not identify any performance deficiencies or violations as a result of this inspection.

Observation: Semiannual Trend 71152S The inspectors evaluated a sample of issues and events that occurred from July 2024 through December 2024 to determine whether issues were appropriately considered as emerging or adverse trends. The inspectors verified issues were appropriately evaluated by Constellation staff for potential trends and addressed within the scope of the corrective action program or through department review. The inspectors did not identify any new trends that could indicate a more significant safety issue. The inspectors determined that Constellation personnel identified trend issues at a low threshold and entered them into the corrective action program for resolution. The inspectors noted licensee-identified trends in grounds experienced on the Unit 1 battery 11 and Unit 1 electromatic relief valve battery elevated cell temperatures. Neither trend currently impacts system operability and Constellation personnel are monitoring these conditions. The inspectors independently evaluated the deficiencies noted above for significance in accordance with the guidance in IMC 0612, Appendix B, "Issue Screening," and Appendix E, "Examples of Minor Issues." The inspectors determined that none of the conditions were deficiencies of greater than minor significance and, therefore, are not subject to enforcement action in accordance with the NRC's Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

x On February 6, 2025, the inspectors presented the integrated inspection results to Carl Crawford, Plant Manager, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

N1-OP-64

Meteorological Monitoring

21

N2-OP-102

Meteorological Monitoring

28

71111.04

Procedures

N1-OP-12

Liquid Poison System

03000

N1-OP-45

Emergency Diesel Generators

2

N2-OP-36A

Standby Liquid Control System

2

N2-OP-36A-

Lineups

Standby Liquid Control System - Lineups

001

71111.05

Fire Plans

N1-PFP-0101

Unit 1 Pre-Fire Plans

00700

N2-FPI-PFP-0201 Unit 2 Pre-Fire Plans

007

71111.06

Corrective Action

Documents

04806541

Procedures

N1-IPM-104-001

Reactor Building Floor/Equipment Drain Sump Level and

Wall Mounted Level Switch Instrument Calibration

completed

07/22/2023

and

06/21/2021

71111.07A Corrective Action

Documents

04813443

NDE Reports

WO-01456-090

Work Orders

C93934972

71111.12

Corrective Action

Documents

04718185

04718539

04718736

04774366

Miscellaneous

Unit 1 Fire Protection a(1) Action Plan

09/03/2024

03790

PREF [procurement requirements evaluation form[

97-0884

Nuclear Procurement Test and Inspection Report

Procedures

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1004

Maintenance Rule - (a)(1) and (a)(2) Requirements

N2-OSP-EGF-

Q@001

D.G. Fuel Oil Transfer Pump and Valve Operability Test and

ASME XI Functional Pressure Test

00700

Work Orders

C93949157

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.13

Corrective Action

Documents

Resulting from

Inspection

04813350

Procedures

OP-AA-201-012-

1001

Operations On-line Fire Risk Management

OP-NM-201-012-

1001

Operations On-line Fire Risk Management at NMP

200

71111.15

Corrective Action

Documents

04722262

04785411

04786004

04790485

04801863

04804263

04805206

04812434

04813728

Miscellaneous

ACMP

Safety Relief Valve 2MSS*PSV122 Leaking By

10/02/2024

Procedures

N1-OP-50B

Process Radiation Monitoring System

01600

71111.18

Engineering

Changes

ECP-24-000154

Replacement of RCIC Division II Differential Pressure

Transmitter

000

71111.24

Corrective Action

Documents

04806124

04813584

Procedures

N1-PM-M9

Operation of Fire Pumps

019

N1-ST-M4A

Emergency Diesel Generator 102 and PB 102 Operability

Test

033

N1-ST-Q25

Emergency Diesel Generator cooling Water Quarterly Test

035

N1-ST-Q6A

Containment Spray System Loop 111 Quarterly Operability

Test

23

N1-ST-Q8B

Liquid Poison Pump 12 and Check Valve Operability Test

01600

N2-OSP-EGF-

Q@001

D.G. Fuel Oil Transfer Pump and Valve Operability Test and

ASME XI Functional Pressure Test

008

N2-OSP-EGS-

Diesel Generator and Diesel Air Start Valve Operability Test

26

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

M@001

- Division I and II

N2-OSP-EGS-

R005

U2 Diesel Generator ECCS Start Division III

006

N2-PM-@026

Diesel Generator Start Following Maintenance - Division I

and II

006

Work Orders

C93794734

C93934972

C93949313

C93957061

71151

Miscellaneous

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

71152A

Corrective Action

Documents

04427748

04467177

04479221

04528148

04673045

04710571

04723637

04758100

04758780

04762854

04774076

04774366

04780622

04780806

04785641

04793583

04794402

04803847

04807780

04809936

04813728

Drawings

C-18030-C

Fire Protection Water System Piping and Instrumentation

Diagram

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Evaluations

S0-FLOOD-F001

Internal Flooding Hazard Analysis

Procedures

N1-MPM-100-851 Diesel Fire Pump Engine Preventive Maintenance

00800

N1-OP-21A

Fire Protection System - Water

2600

Work Orders

C93809476

C93823235

C93946369

71152S

Corrective Action

Documents

04779953

04782058

04784717

04784908

04788195

04796362

04800026

04800111

04802058

04803976

04806900

04807958

04813704

04815161

04815162

04819350

04821372