Letter Sequence Request |
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TAC:ME0274, Steam Generator Tube Integrity (Approved, Closed) |
Results
Other: 3F0111-04, Comments on the Safety Evaluation Report with Open Items Related to the License Renewal and Amendment 18, 3F0412-03, Revised Commitment for the Reactor Vessel Internals Aging Management Program for License Renewal and License Renewal Application Amendment 24, 3F1208-02, Systems Drawings Supporting License Renewal, 3F1209-06, License Renewal Application 10 CFR Part 54.21(b) Annual Update, 3F1211-01, License Renewal Application 10 CFR Part 54.21(b), Annual Update, 3F1212-01, License Renewal Application 10 CFR Part 54.21(b) Annual Update, ML090090233, ML090210171, ML091200415, ML091660559, ML091820465, ML092600889, ML092610309, ML093200023, ML100050166, ML110410597, ML11137A009, ML12213A058
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MONTHYEAR3F1208-02, Systems Drawings Supporting License Renewal2008-12-16016 December 2008 Systems Drawings Supporting License Renewal Project stage: Other ML0900902332009-02-27027 February 2009 Determination of Acceptability and Sufficiency for Docketing, and Opportunity for a Hearing Regarding the Application from Florida Power Corp., for Renewal of the Operating License for Crystal River Unit 3 Nuclear Generating Plant Project stage: Other ML0902101712009-02-27027 February 2009 Notice of Opportunity for Hearing Regarding Renewal of Facility Operating License No. DPR-72 for an Additional 20-year Period Florida Power Corporation Corporation Crystal River Unit 3 Nuclear Generating Plant Docket No. 50-302 Project stage: Other ML0908501762009-04-20020 April 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 3F0509-01, Response to Request for Additional Information for the Review of the License Renewal Application2009-05-11011 May 2009 Response to Request for Additional Information for the Review of the License Renewal Application Project stage: Response to RAI ML0912004152009-05-22022 May 2009 Proposed Review Schedule Regarding the Application from Florida Power Corporation for Renewal of the Operating License for Crystal River Unit 3 Nuclear Generating Plant Project stage: Other 3F0509-07, License Amendment Request 303, Revision 1, Supplement 1: Revision to Final Safety Analysis Report Sections 5.4.3, Structural Design Criteria, and 5.4.5.3, Missile Analysis, Response to Request for Additional Information2009-05-22022 May 2009 License Amendment Request 303, Revision 1, Supplement 1: Revision to Final Safety Analysis Report Sections 5.4.3, Structural Design Criteria, and 5.4.5.3, Missile Analysis, Response to Request for Additional Information Project stage: Supplement ML0918204652009-07-0808 July 2009 Plan for the Aging Management Program Regulatory Audit Regarding the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Review Project stage: Other ML0916605592009-07-30030 July 2009 Audit Report Regarding the LRA for the Crystal River, Unit 3 Project stage: Other ML0917400702009-08-0303 August 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI ML0920800452009-08-14014 August 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Project stage: RAI ML0920302082009-08-14014 August 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI ML0922507012009-08-20020 August 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI ML0920200122009-08-20020 August 2009 RAI, License Renewal Application Project stage: RAI ML0923303432009-08-31031 August 2009 Nuclear Generating Plant, RAI, License Renewal Application Project stage: RAI ML0923308312009-08-31031 August 2009 Request for Additional Information Regarding License Renewal Application Project stage: RAI ML0923300072009-08-31031 August 2009 RAI for the Review of the Crystal River Unit 3 Nuclear Generating Plant, LRA Project stage: RAI ML0923309042009-09-0202 September 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Project stage: RAI 3F0909-02, Response to Request for Additional Information for the Review of the License Renewal Application2009-09-11011 September 2009 Response to Request for Additional Information for the Review of the License Renewal Application Project stage: Response to RAI ML0926008892009-09-11011 September 2009 Areva Np, Inc., 51-9057252-001, Rev. 1, CR3 Reconciliation of 60-Year Fluence Projections Used in Reactor Vessel Beltline Embrittlement Calculations for License Renewal, Enclosure Attachment 3 Project stage: Other ML0921602132009-09-11011 September 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Project stage: RAI 3F0909-03, Response to Requests for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC No. ME0274) and Amendment 22009-09-11011 September 2009 Response to Requests for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC No. ME0274) and Amendment 2 Project stage: Response to RAI 3F0909-04, Response to Requests for Additional Information for the Review of the License Renewal Application and Amendment 32009-09-18018 September 2009 Response to Requests for Additional Information for the Review of the License Renewal Application and Amendment 3 Project stage: Response to RAI ML0923706692009-09-22022 September 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Unit Plant, License Renewal Application Project stage: RAI ML0926103092009-09-29029 September 2009 Scoping and Screening Audit Report Regarding the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Project stage: Other 3F0909-06, Response to Requests for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC ME0274) and Amendment 42009-09-30030 September 2009 Response to Requests for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC ME0274) and Amendment 4 Project stage: Response to RAI 3F1009-06, Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application (TAC No. ME0274) - Sections B.2.37-1, 3.3.2.2, and XI.S82009-10-0202 October 2009 Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application (TAC No. ME0274) - Sections B.2.37-1, 3.3.2.2, and XI.S8 Project stage: Response to RAI 3F1009-07, Response to Request for Additional Information for the Review of Unit 3 Nuclear Generating Plant License Renewal Application and Amendment 52009-10-13013 October 2009 Response to Request for Additional Information for the Review of Unit 3 Nuclear Generating Plant License Renewal Application and Amendment 5 Project stage: Response to RAI ML0926405542009-10-15015 October 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 3F1009-08, Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application (TAC No. ME0274) - and Amendment 62009-10-22022 October 2009 Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application (TAC No. ME0274) - and Amendment 6 Project stage: Response to RAI ML0929606602009-10-27027 October 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI ML0929403222009-11-0303 November 2009 Request for Additional Information for the Review of the Crystal River, Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 3F1109-05, Response to Request for Additional Information for Review of License Renewal Application, Section 2.32009-11-12012 November 2009 Response to Request for Additional Information for Review of License Renewal Application, Section 2.3 Project stage: Response to RAI ML0932305592009-11-30030 November 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application Project stage: RAI ML0930301472009-12-0101 December 2009 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Review Application Project stage: RAI 3F1209-03, Response to Request for Additional Information for the Review of the License Renewal Application2009-12-0303 December 2009 Response to Request for Additional Information for the Review of the License Renewal Application Project stage: Response to RAI ML0932704962009-12-10010 December 2009 Areva Np, Inc. - Request for Withholding Information from Public Disclosure for Crystal River Unit 3 Nuclear Generating Plant Project stage: Withholding Request Acceptance ML0933102952009-12-10010 December 2009 Areva Np, Inc.- Request for Withholding Information from Public Disclosure for Crystal River Unit 3 Nuclear Generating Plant Project stage: Withholding Request Acceptance 3F1209-06, License Renewal Application 10 CFR Part 54.21(b) Annual Update2009-12-14014 December 2009 License Renewal Application 10 CFR Part 54.21(b) Annual Update Project stage: Other ML0932000232009-12-14014 December 2009 AMP Audit Report Regarding the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: Other 3F1209-11, 10 CFR 50.46 Loss-of-Coolant Accident Evaluation Model Change and Peak Cladding Temperature Change Report2009-12-16016 December 2009 10 CFR 50.46 Loss-of-Coolant Accident Evaluation Model Change and Peak Cladding Temperature Change Report Project stage: Request 3F1209-12, Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC No. ME0274) and Amendment 82009-12-30030 December 2009 Response to Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application (TAC No. ME0274) and Amendment 8 Project stage: Response to RAI ML1000501662010-01-25025 January 2010 Revised Review Schedule Regarding the Application from Florida Power Corporation for Renewal of the Operating License for Crystal River Unit 3 Nuclear Generating Plant Project stage: Other 3F0110-04, Response to Request for Additional Information for the Review of the License Renewal Application & Amendment 92010-01-27027 January 2010 Response to Request for Additional Information for the Review of the License Renewal Application & Amendment 9 Project stage: Response to RAI ML1001000102010-02-0202 February 2010 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 3F0310-01, Response to Request for Additional Information for Review of License Renewal Application and Amendment 102010-03-0303 March 2010 Response to Request for Additional Information for Review of License Renewal Application and Amendment 10 Project stage: Response to RAI ML1011302232010-05-21021 May 2010 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI ML1014105122010-06-0202 June 2010 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 3F0610-02, Response to Requests for Additional Information for the Review of License Renewal Application (TAC No. ME0274) and Amendment 112010-06-21021 June 2010 Response to Requests for Additional Information for the Review of License Renewal Application (TAC No. ME0274) and Amendment 11 Project stage: Response to RAI ML1017404972010-07-0808 July 2010 Request for Additional Information for the Review of the Crystal River Unit 3 Nuclear Generating Plant, License Renewal Application Project stage: RAI 2009-07-30
[Table View] |
Text
Progress Energy Crystal River Nuclear Plant Docket No. 50-302 Operating License No. DPR-72 March 31, 2011 3F0311-10 Mr. Michael Cheok, Deputy Director Division of Inspection and Regional Support Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, DC 20555-0001
Subject:
Crystal River Unit 3 - Groundwater Protection - Data Collection Questionnaire
Reference:
FPC to NRC letter, 3F0706-03, dated July 25, 2006, "Groundwater Protection -
Data Collection Questionnaire" (Accession No. ML062280588)
Dear Mr. Cheok:
The nuclear industry, in conjunction with the Nuclear Energy Institute, developed a questionnaire to facilitate the collection of groundwater data at commercial nuclear reactor sites in 2006. The objective of the questionnaire was to compile baseline information about the status of site programs for monitoring and protecting groundwater and to share that information with Nuclear Regulatory Commission.
Florida Power Corporation, doing business as Progress Energy Florida, Inc., submitted the completed questionnaire for Crystal River Unit 3 (CR-3) by the above referenced letter.
During a recent review of the CR-3 Groundwater Protection - Data Collection Questionnaire response, it became apparent that three historical events that occurred at CR-3 were not included in the response to Question 3 in the above referenced submittal. As denoted by a revision line bar located in the right margin, this submittal provides the supplemental information to Question 3 and a minor administrative clarification to Question 5 which references the Question 3 response. This letter completely supersedes the above referenced submittal.
This submittal contains no new regulatory commitments.
If you have any questions regarding this submittal, please contact Mr. Dan Westcott, Superintendent, Licensing and Regulatory Programs at (352) 563-4796.
Sincerely, ames W. Holt Plant General Manager Crystal River Nuclear Plant Enclosure xc:
USNRC Document Control Desk USNRC Resident Inspector - Crystal River Unit 3 NRR Project Manager - Crystal River Unit 3 USNRC Regional Administrator - Region II Ralph Andersen, Nuclear Energy Institute Progress Energy Florida, Inc.
Crystal River Nuclear Plant 15760 W. Power Line Street Crystal River, FL 34428
FLORIDA POWER CORPORATION CRYSTAL RIVER - UNIT 3 DOCKET NUMBER 50-302/LICENSE NUMBER DPR-72 ENCLOSURE GROUNDWATER PROTECTION - DATA COLLECTION QUESTIONNAIRE
U. S. Nuclear Regulatory Commission Enclosure 3F0311-10 Page 1 of 3 Groundwater Protection - Data Collection Questionnaire
- 1. Briefly describe the program and/or methods used for detection of leakage or spills from plant systems, structures, and components that have a potential for an inadvertent release of radioactivity from plant operations into groundwater.
Crystal River Unit 3 has programs and procedures in place to rapidly identify and correct leakage including those in outdoor areas. Operations personnel perform routine rounds of plant systems and structures daily. These rounds include the requirements to identify and report leaks and spills into the site work request system and/or the site corrective action program. Response to spills includes notification of Control Room and Radiation Protection personnel for assessment and cleanup.
Health Physics personnel perform dose rate and contamination surveys weekly within the Protected Area, including taking smears of areas around storm drains.
There are no underground tanks at this facility that contain radioactive materials.
There are above ground tanks that are outside the immediate facility buildings that contain radioactive liquids. Potential leak sources and components have been identified.
The spent fuel pool system has a functional leak detection system. The tell-tale drains are monitored daily on Operator rounds and documented in site logs. It should be noted that the spent fuel pools do not sit on the bottom floor of the facility.
Engineers perform periodic walk downs of the systems for which they are responsible. These rounds include the requirements to identify and report leaks and spills into the site work request system and/or the site corrective action program. Response to spills includes notification of Control Room and Radiation Protection personnel for assessment and cleanup.
Leakage from components that result in an unplanned release are documented on a Nuclear Condition Report (NCR) and a determination of reportability is made by plant personnel, including notification of required agencies, if necessary.
- 2. Briefly describe the program and/or methods for monitoring onsite groundwater for the presence of radioactivity released from plant operations.
Presently, there are no on-site groundwater monitoring stations utilized by the Radiological Environmental Monitoring Program (REMP). The closest groundwater monitoring well is 3.6 miles east of the facility. The well is sampled and analyzed for tritium and gamma radionuclides. There are three drinking water wells that are also sampled quarterly for the same parameters. The drinking water wells are located off-site: (1) ESE 7.4 miles from the facility, (2)
ESE 6.0 miles from the facility, and (3) N 5.3 miles from the facility.
U. S. Nuclear Regulatory Commission Enclosure 3F031 1-10 Page 2 of 3 Typical detection levels in pCi/I are as follows:
H-3
< 147 Mn-54
< 5 Fe-59
< 8 Co-58
< 5 Co-60
< 5 Zn-65
< 9 Zr-Nb-95
< 7 1-131
< 5 Cs-134
< 5 Cs-137
< 4 Ba-La-140
< 15 Due to the direction of groundwater movement at the facility (toward the southwest and the Gulf of Mexico) and the coastal location of the facility, future sources of drinking water will not be impacted by facility operation. The groundwater at the facility proper is too saline for use as a potable water source.
Hence, well locations east of the facility were chosen as sources of drinking water.
- 3. If applicable, briefly summarize any occurrences of inadvertent releases of radioactive liquids that had the potential to reach groundwater and have been documented in accordance with 10 CFR 50.75(g).
In December 1995, a leak was discovered in piping which forms part of the Crystal River Unit 3 (CR-3) Emergency Feedwater System. This piping provides a recirculation flow path from the Emergency Feedwater Pumps (EFP-1/2) to the Emergency Feedwater Tank (EFT-2), and provides a minimum flow path for pump protection during delivery of Emergency Feedwater. The leak was located in a buried section of carbon steel piping, approximately one hundred feet from EFT-2. The leak resulted from a through-wall flaw located on the exterior surface of the pipe. The cause of this flaw appeared to be corrosion through contact with the soil due to poor coating installation. The damaged section was replaced in 1996 and cathodic protection was installed. It is not known how much water could have potentially leaked out of this pipe and into the surrounding soil.
An interior inspection of the Condensate Storage Tank (CDT-1) performed during August 1997, identified two small holes in the bottom of the tank. This event was documented in a CR-3 Corrective Action Program as Precursor Card (PC) # 3-C97-7254. The limestone underneath the tank was sampled and showed no contamination. It is not known how much water potentially leaked from this tank.
On April 21, 1998, while performing a planned authorized discharge from the Station Drain Tank (SDT-1) to the evaporation/percolation pond, an unplanned release of effluent (water) occurred from an underground transfer pipe which was found to be leaking in the vicinity of a storm drain. It was estimated that approximately 900 gallons leaked into the storm drain and from there flowed into the site discharge canal. It is expected that some water was also released into the ground through the compacted limestone foundation of the west berm. This volume could not be determined, but was estimated to be less than 7650 gallons.
This tank contained secondary plant water that contained tritium at a concentration of 3.6E-4 pCi/ml. No gamma emitters were identified. Additionally, as part of the repair efforts for this 1998 spill, the line from the tank that travelled underground behind CDT-1 and turned "under the berm", was hydrostatically
U. S. Nuclear Regulatory Commission Enclosure 3F031 1-10 Page 3 of 3 tested and found leaking and was abandoned in place. This line may have leaked for years and it is very possible there were previous leaks in the SDT-1 discharge line prior to the recognition of this 1998 leak. As such, it is difficult to determine how much water, being sent to the settling ponds, potentially leaked out of that line into the ground under the berm/fabri-form. This event was documented in PC #3-C98-2106 and was reported to the NRC by NRC 90 Days After Startup (Breaker Closure)|letter dated April 23, 1998]] (Accession No. ML9804290230). This event was also documented in the CR-3 1998 Radioactive Effluent Release Report.
On October 2, 1999, during a secondary plant condensate release to the on-site percolation pond, a leak in the fiberglass wastewater line occurred that resulted in a small amount of water leaking onto the ground. The water contained low level tritium and secondary condensate corrosion control treatment chemicals.
All affected soil was excavated. There was no groundwater contamination from this spill. This event was documented on precursor card (PC) 3-C99-3279.
- 4. If applicable, briefly summarize the circumstances associated with any onsite or offsite groundwater monitoring result indicating a concentration in groundwater of radioactivity released from plant operations that exceeds the maximum contaminant level (MCL) established by the USEPA for drinking water.
There have been no instances of groundwater contamination that remotely challenged the MCL for drinking water.
- 5. Briefly describe any remediation efforts undertaken or planned to reduce or eliminate levels of radioactivity resulting from plant operations in soil or groundwater onsite or offsite.
There was one instance (reference Bullet 4 of the response to Question 3 above) of remediation of a leaking pipe on a secondary plant discharge pipe to the site percolation pond that resulted in a small amount of secondary plant water containing low levels of tritium leaking into the soil. The liquid did not reach the groundwater and all affected soil material was excavated, as necessary, and disposed of.