05000529/LER-2012-003, Regarding Entry Into Mode 3 with One Auxiliary Feedwater Train Inoperable

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Regarding Entry Into Mode 3 with One Auxiliary Feedwater Train Inoperable
ML13004A092
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 12/28/2012
From: Mims D
Arizona Public Service Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 12-003-00
Download: ML13004A092 (6)


LER-2012-003, Regarding Entry Into Mode 3 with One Auxiliary Feedwater Train Inoperable
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
LER closed by
IR 05000528/2013002 (14 May 2013)
5292012003R00 - NRC Website

text

10 CFR 50.73 A MA subsidiary of Pinnacle West Capital Corporation Dwight C. Mims Mail Station 7605 Palo Verde Nuclear Senior Vice President Tel. 623-393-5403 P.O. Box 52034 Generating Station Nuclear Regulatory and Oversight Fax 623-393-6077 Phoenix, Arizona 85072-2034 102-06638-DCM/DFH December 28, 2012 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS) Unit 2 Docket No. STN 50-529 License No. NPF-51 Licensee Event Report 2012-003-00 Enclosed please find Licensee Event Report (LER) 50-529/2012-003-00 that has been prepared and submitted pursuant to 10 CFR 50.73. This LER reports a condition prohibited by Technical Specifications when Unit 2 entered Mode 3 operations with one Auxiliary Feedwater train inoperable.

In accordance with 10 CFR 50.4, copies of this LER are being forwarded to the Nuclear Regulatory Commission (NRC) Regional Office, NRC Region IV and the Senior Resident Inspector. If you have questions regarding this submittal, please contact Mark McGhee, Operations Support Manager, Regulatory Affairs, at (623) 393-4972.

Arizona Public Service Company makes no commitments in this letter.

Sincerely, A-<I ley DCM/DFH/hsc Enclosure cc:

E. E. Collins Jr.

NRC Region IV Regional Administrator L. K. Gibson NRC NRR Project Manager (electronic / paper)

M. A. Brown NRC Senior Resident Inspector for PVNGS A member of the STARS (Strategic Teaming and Resource Sharihg) Alliance Callaway

  • Comanche Peak
  • Diablo Canyon
  • Palo Verde
  • San Onofre
  • Wolf Creek

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-20 10)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Palo Verde Nuclear Generating Station (PVNGS) Unit 2 05000529 1i OF 5
4. TITLE Entry into Mode 3 with one Auxiliary Feedwater Train Inoperable
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YE ISEQUENTIAL IREV IFACILITY.

NAME DOCKET NUMBER MONR YEAR SUE RENO.

MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 11 2

2012 2012 - 003 00 12 28 2012

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

El 20.2201(b)..

[ E 20.2203(a)(3)(i)

El 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii) 3 El 20.2201(d)

El 20.2203(a)(3)(ii)

[E 50.73(a)(2)(ii)(A)

El 50.73(a)(2)(viii)(A)

El 20.2203(a)(1).

El 20.2203(a)(4)

El 50.73(a)(2)(ii)(B)

[I 50.73(a)(2)(viii)(B)

El 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

El 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

10. POWER LEVEL El 20.2203(a)(2)(ii)

E '50.36(c)(1)(ii)(A)

[: 50.73(a)(2)(iv)(A)

[I 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

El 50.36(c)(2) "

El 50.73(a)(2)(v)(A)

El 73.71(a)(4).

El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

El 50.73(a)(2)(v)(B)

El 73.71(a)(5) 0 [E

20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

[E OTHER El 20,2203(a)(2)(vi)

Z 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

Specify in Abstract below or in Each essential AF pump provides 100 percent of the required flow capacity to the steam generators to remove decay heat and cool the unit to Shutdown Cooling (SDC) System entry conditions. The non-essential AF pump is used during normal unit startup, shutdown, and hot standby conditions and provides sufficient feedwater to remove decay heat under no load conditions and to cool the unit to SDC entry conditions. The two motor driven AF pumps receive electric power from one of the two 4.16 KV safety related buses. The steam turbine driven AF pump receives steam from either steam generator's main steam lines upstream of the main steam isolation valves (MSIV). Each steam supply line is capable of supplying 100 percent of the required steam flow for the steam turbine driven AF pump and is configured with a supply valve which is actuated by the Auxiliary Feedwater Actuation Signal (AFAS).

The two steam supply valves (SGA-UV-1 34 and SGA-UV-1 38) for steam turbine driven AF pump "A" are 125 VDC motor operated, 6 inch gate valves. The valves are located in the Main Steam Support Structure and are installed with the bonnet and valve actuator assembly at a 45 degree angle from vertical to allow for access to the valve actuator. Each is interlocked with a 1.5 inch, motor operated bypass valve (SGA-UV-1 34A and SGA-UV-138A). When the steam turbine driven AF pump is started, the small bypass valve opens prior to the larger 6 inch supply valve to allow controlled turbine acceleration on startup and prevent turbine overspeed. The large 6 inch steam supply valves then open after a nominal time delay to provide full steam supply capability.

The steam supply valves also function as containment isolation valves that are open during accident conditions. These valves do not receive a closure signal following receipt of a Containment Isolation Actuation Signal but are automatically opened to support the AF system function. The valves may be remotely opened or closed by Operations personnel with controls in the control room or the remote shutdown panel.

3.

INITIAL PLANT CONDITIONS

On November 2, 2012, at 11:33, PVNGS Unit 2 was in Mode 3, Hot Standby. Reactor coolant system temperature and pressure were being increased in preparation for planned equipment testing at normal operating temperature and pressure following refueling.

There were no structures, systems, or components inoperable at the time of the event that contributed to the event.

4.

EVENT DESCRIPTION

On October 23, 2012, during refueling outage 2R1 7 with Unit 2 in Mode 5, scheduled work was performed on turbine driven AF pump steam supply valve SGA-UV-1 38 to correct a valve seat leakage condition. The work activity required disassembly and re-assembly of the valve and was completed later on the same day. Post maintenance valve testing could NRC FORM

'66A (10-201071 PRINTED ON RECYCLED PAPER

not be completed at that time because the plant was at cold shutdown conditions and the testing required normal hot standby steam pressure conditions in Mode 3.

At 00:07 on November 02, 2012, Unit 2 entered Mode 3 as Operations personnel conducted activities to heatup and pressurize the RCS following refueling activities. Operations personnel entered TS LCO 3.7.5, Condition A, at 09:30, when steam driven AF pump, AFA-P01, was declared inoperable to support planned surveillance testing in accordance with procedure 73ST-9AF04, AFA-P01 Full Flow In-service Test. This surveillance test is used to verify the operability of AF Train A, including the steam driven AF pump steam supply valve SGA-UV-1 38. At 11:33 on November 02, 2012, during the test, a steam leak was identified on the bonnet of valve SGA-UV-1 38 when the valve was opened. Operations personnel closed the valve to stop the steam leak, declared valve SGA-UV-1 38 inoperable and stopped the testing activity.

To establish conditions to repair the valve, a plant cooldown was conducted and TS LCO 3.7.5 Condition A was exited at 01:33 on November 3, 2012, when Unit 2 entered Mode 4 where the steam driven AF pump was no longer required to be OPERABLE. The cooldown activity was continued to place Unit 2 in Mode 5 where plant conditions would allow the leaking valve to be repaired. Maintenance and Engineering personnel identified that an improperly seated segmented bonnet seal ring had caused the steam leak at the valve bonnet. The valve was repaired on November 3, 2012, and was successfully retested on November 4, 2012, after Unit 2 was returned to Mode 3.

5.

ASSESSMENT OF SAFETY CONSEQUENCES

This condition did not adversely affect plant safety or the health and safety of the public.

The condition did not result in any challenges to the fission product barriers or result in any releases of radioactive materials.

The leak on the bonnet of valve SGA-UV-1 38 would have resulted in steam leakage to the Main Steam Support Structure room when the steam driven AF pump steam supply valve (SGA-UV-1 38) was opened such that the pump would not have been able to provide the required feedwater flow under all plant conditions. However, there was no actual safety consequence because the decay heat load is very low following core refueling and the two motor driven AF pumps were operable at all times during the event.

The containment isolation function of valve SGA-UV-1 38 could still be met because the flow path from containment is isolated from the leaking bonnet area when the valve is in the closed position.

This event did not prevent the fulfillment of a safety function and did not result in a safety system functional failure as described by 10 CFR 50.73(a)(2)(v).

6.

CAUSE OF THE EVENT

The cause of this event was determined to be inadequate work instructions. The work instructions did not provide detailed guidance for installing an angled bonnet. The steam driven AF pump steam supply valves are installed with the bonnet and valve actuator assembly at a 45 degree angle from vertical to allow for access to the valve actuator. Valve maintenance activities are complicated by this configuration because the segmented bonnet seal rings are subject to displacement by gravity during work to assemble the valve. The bonnet seal rings must be correctly placed to ensure adequate sealing of the body to bonnet joint. The work instruction also lacked guidance to verify correct valve reassembly in the cold condition prior to performing the post maintenance testing at normal operating temperature and pressure.

7.

CORRECTIVE ACTIONS

As an immediate corrective action, Operations personnel closed the valve to stop the leak and declared valve SGA-UV-138 inoperable. Unit 2 was cooled down and placed in Mode 5 where the AF system is not required and the valve was repaired.

To prevent recurrence, corrective actions will revise work instructions to provide detailed guidance for valve re-assembly on valves that are configured with an angled bonnet. Work instructions will also incorporate guidance for as-found and as-left dimensional checks of the valve body to bonnet joint as a method to verify proper valve re-assembly.

Any additional corrective actions taken as a result of this event will be implemented in accordance with the PVNGS corrective action program. If information is subsequently developed that would significantly affect a reader's understanding or perception of this event, a supplement to this LER will be submitted.

8.

PREVIOUS SIMILAR EVENTS

In the past three years, PVNGS has not reported a similar event where a unit entered Mode 3 with an inoperable auxiliary feedwater train.

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