05000530/LER-2012-001, Regarding Manual Reactor Trip During Low Power Physics Testing

From kanterella
Jump to navigation Jump to search
Regarding Manual Reactor Trip During Low Power Physics Testing
ML12193A089
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 06/21/2012
From: Weber T
Arizona Public Service Co, APS
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
102-06535-TNW/MAM/DCE LER 12-001-00
Download: ML12193A089 (2)


LER-2012-001, Regarding Manual Reactor Trip During Low Power Physics Testing
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
LER closed by
IR 05000528/2013002 (14 May 2013)
5302012001R00 - NRC Website

text

10 CFR 50.73 LA subsidiary of Pinnacle West Capital Corporation Palo Verde Nuclear Generating Station Thomas N. Weber Department Leader Nuclear Regulatory Affairs Tel. 623-393-5764 Fax 623-393-5422 Mail Station 7635 P.O. Box 52034 Phoenix, Arizona 85072-2034 102-06535-TNW/MAM/DCE June 21, 2012 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001

Reference:

Arizona Public Service Company (APS) Letter No. 102-06532-DCM/TNW/MAM/DCE, dated June 14, 2012, Licensee Event Report (LER) 2012-001-00

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 3 Docket No. STN 50-530 License No. NPF-74 Correction to NRC Form 366 for LER 2012-001-00 Attached please find a corrected page for the NRC Form 366 previously submitted in the referenced letter. The following change was made to correct an administrative error:

Block 7 has been changed to list the Report Date "DAY" value of "14", which was omitted.

Please update your files accordingly. If you have questions regarding this submittal, please contact Mark McGhee, Operations Support Manager, Regulatory Affairs, at (623) 393-4972.

Arizona Public Service Company makes no commitments in this letter.

Sincerely, TNW/MAM/DCE/hsc Enclosure cc:

E. E. Collins Jr.

L. K. Gibson M. A. Brown NRC Region IV Regional Administrator NRC NRR Project Manager (electronic / paper)

NRC Senior Resident Inspector for PVNGS A member of the STARS (Strategic Teaming and Resource Sharing) Alliance iiU

- t- -C9 Callaway
  • Comanche Peak
  • Diablo Canyon
  • Palo Verde
  • San Onofre
  • Wolf Cre

CORRECTED COPY NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Palo Verde Nuclear Generating Station (PVNGS) Unit 3 05000530 1 OF 5
4. TITLE Unit 3 Manual Reactor Trip During Low Power Physics Testing
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV FACILITY NAME DOCKET NUMBER NUMBERAY YEANO.ARMONTH DAY YEAR NUMBER NO.

FACILITY NAME DOCKET NUMBER 04 15 2012 2012 - 001 -

00 06 14 2012

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

El 20.2201(b)

El 20.2203(a)(3)(i)

[I 50.73(a)(2)(i)(C)

[I 50.73(a)(2)(vii) 2 [1 20.2201(d)

El 20.2203(a)(3)(ii)

El 50.73(a)(2)(ii)(A)

El 50.73(a)(2)(viii)(A)

El 20.2203(a)(1)

El 20.2203(a)(4)

El 50.73(a)(2)(ii)(B)

El 50.73(a)(2)(viii)(B)

El 20.2203(a)(2)(i)

[I 50.36(c)(1)(i)(A)

El 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

10. POWER LEVEL

[] 20.2203(a)(2)(ii)

El 50.36(c)(1)(ii)(A)

[D 50.73(a)(2)(iv)(A)

El 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

El 50.36(c)(2)

El 50.73(a)(2)(v)(A)

[1 73.71(a)(4)

El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

El 50.73(a)(2)(v)(B)

El 73.71(a)(5) 0 El 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

[I 50.73(a)(2)(v)(C)

E] OTHER El 20.2203(a)(2)(vi)

El 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

Specify in Abstract below or in NRC Form 366A

12. LICENSEE CONTACT FOR THIS LER

=ACILITY NAME TELEPHONE NUMBER (Include Area Code)

Mark McGhee, Operations Support Manager, Regulatory Affairs 623-393-4972MANU-REPORTABLE MANU-REPORTABLE

CAUSE

SYSTEM COMPONENT FACTURER TO EPIX

CAUSE

SYSTEM COMPONENT FACTURER TO EPIX

14. SUPPLEMENTAL REPORT EXPECTED
15. EXPECTED MONTH DAY YEAR SUBMISSION 0D YES (If yes, complete 15. EXPECTED SUBMISSION DATE)

El NO DATE 08 31 2012 ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)

On April 15, 2012, at approximately 12:16 Mountain Standard Time, Unit 3 was manually tripped during low power physics testing (LPPT) following completion of its 1 6 th refueling outage. An automatic control element drive mechanism timer module (ACTM) was installed on each control element drive mechanism (CEDM) during the refueling outage to minimize the occurrence of slipped or dropped control element assemblies (CEAs) resulting from CEDM or control system (CEDMCS) abnormalities. Regulating CEA group 1 was being inserted during a reactor coolant system (RCS) boron dilution test directed by the LPPT procedure. During the insertion, the ACTM for CEA 57 stopped movement of the CEA and actuated related alarms. Control room staff stopped insertion of regulating CEA group 1 and RCS dilution. Power increased, approaching the LPPT procedural limit of 0.5% power because of the residual RCS dilution effect. The control room staff manually tripped the reactor to comply with the procedural power limit. The LPPT procedure did not provide contingency direction to insert other CEA groups to compensate for the RCS dilution.

The root cause investigation is in progress. In response to the event, the LPPT procedure was revised to provide contingency direction to insert regulating CEA group 5 in the event planned CEA insertion could not continue during the test. Similar events have not occurred in the prior three years.

NRC FORM 366 (10-2010)