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| 05000528/LER-1986-001-01, :on 860125,diesel Generator B Failed to Start During Manual Start Attempt.Caused by Failed Resistor in Electric Governor Circuitry.Failed Resistor & Amplifier Module Replaced & Diesel Tested Satisfactorily |
- on 860125,diesel Generator B Failed to Start During Manual Start Attempt.Caused by Failed Resistor in Electric Governor Circuitry.Failed Resistor & Amplifier Module Replaced & Diesel Tested Satisfactorily
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| 05000529/LER-1986-001, :on 860103,source Range Monitor Channel Checks Not Performed within Max Allowable Time.Caused by Failure of Operator to Perform Test on Schedule.Step Added to Procedure to Initiate Test in Mode 6 |
- on 860103,source Range Monitor Channel Checks Not Performed within Max Allowable Time.Caused by Failure of Operator to Perform Test on Schedule.Step Added to Procedure to Initiate Test in Mode 6
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| 05000529/LER-1986-002, :on 860220,during Cold Shutdown,Train a Main Steam Isolation Signal Occurred,Actuating Esf.Caused by Incorrect Amperage fuse.Eight-amp Fuse Installed in Affected Path |
- on 860220,during Cold Shutdown,Train a Main Steam Isolation Signal Occurred,Actuating Esf.Caused by Incorrect Amperage fuse.Eight-amp Fuse Installed in Affected Path
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| 05000529/LER-1986-002-01, :on 860220,during Cold Shutdown,Train a Main Steam Isolation Sys Actuation Occurred.Caused by Use of Undersized Fuse in 2-4 Logic Trip path.Eight-amp Fuse Installed in Affected Path |
- on 860220,during Cold Shutdown,Train a Main Steam Isolation Sys Actuation Occurred.Caused by Use of Undersized Fuse in 2-4 Logic Trip path.Eight-amp Fuse Installed in Affected Path
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| 05000528/LER-1986-002, :on 860106,third Quarter Strontium Air Filter Analysis Composite Samples Discovered in Warehouse Awaiting Shipment for Analysis.Caused by Incorrect Processing of Purchase Order |
- on 860106,third Quarter Strontium Air Filter Analysis Composite Samples Discovered in Warehouse Awaiting Shipment for Analysis.Caused by Incorrect Processing of Purchase Order
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| 05000528/LER-1986-003-01, :on 860806,Units 1 & 2 Reactors Tripped at 100% & 7%,respectively,on Low Flow Projected DNBR Trip Signals from Core Protection Calculators.Caused by Faulty Current Transformer.Similar Transformers Tested |
- on 860806,Units 1 & 2 Reactors Tripped at 100% & 7%,respectively,on Low Flow Projected DNBR Trip Signals from Core Protection Calculators.Caused by Faulty Current Transformer.Similar Transformers Tested
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| 05000529/LER-1986-003, :on 860122,logarithmic Power Level Channel Check Not Completed During Surveillance Test.Caused by Operator Error.Personnel Counseled on Following Procedures. Technical Advisors Now Reviewing Tests |
- on 860122,logarithmic Power Level Channel Check Not Completed During Surveillance Test.Caused by Operator Error.Personnel Counseled on Following Procedures. Technical Advisors Now Reviewing Tests
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| 05000528/LER-1986-004-01, :on 860128,pressurizer Pressure Raised Above 430 Psia W/O Removing Power to key-locked Open Safety Injection Tank Isolation Valves.Caused by Ambiguous Info in Tech Specs.Procedures & Tech Specs Revised |
- on 860128,pressurizer Pressure Raised Above 430 Psia W/O Removing Power to key-locked Open Safety Injection Tank Isolation Valves.Caused by Ambiguous Info in Tech Specs.Procedures & Tech Specs Revised
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| 05000529/LER-1986-004, :on 860124,inadvertent Actuation of Containment Purge Isolation Actuation Signal & Control Room Essential Filtration Actuation Signal Occurred.Caused by Personnel Error.Technicians Will Attend Briefing |
- on 860124,inadvertent Actuation of Containment Purge Isolation Actuation Signal & Control Room Essential Filtration Actuation Signal Occurred.Caused by Personnel Error.Technicians Will Attend Briefing
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| 05000529/LER-1986-005-01, :on 860130,control Room Essential Filtration Actuation Occurred Due to Train a Instrument & Control Power Failure.Caused by Inadequate Control of Mod to Vital Power Inverter.Inverters Inspected |
- on 860130,control Room Essential Filtration Actuation Occurred Due to Train a Instrument & Control Power Failure.Caused by Inadequate Control of Mod to Vital Power Inverter.Inverters Inspected
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| 05000529/LER-1986-006-01, :on 860208,containment Purge Isolation & Control Room Essential Filtration Actuation Signals Actuated on Both Channels.Caused by Failure of Technician to Fully Analyze Effects of Actions Prior to Beginning |
- on 860208,containment Purge Isolation & Control Room Essential Filtration Actuation Signals Actuated on Both Channels.Caused by Failure of Technician to Fully Analyze Effects of Actions Prior to Beginning
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| 05000528/LER-1986-006, :on 860109,turbine Trip Initiated by Manual Actuation of Differential Generator Protection Relay, Resulting in Loss of Power to Reactor Coolant Pumps.Power Restored.Study Underway |
- on 860109,turbine Trip Initiated by Manual Actuation of Differential Generator Protection Relay, Resulting in Loss of Power to Reactor Coolant Pumps.Power Restored.Study Underway
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| 05000529/LER-1986-007-01, :on 860227,discovered That Surveillance Test Procedure Not Performed within Required Time Interval.Caused by Inadequate Procedures.Form Notifying Control Room Personnel of Procedure Changes Put Into Effect |
- on 860227,discovered That Surveillance Test Procedure Not Performed within Required Time Interval.Caused by Inadequate Procedures.Form Notifying Control Room Personnel of Procedure Changes Put Into Effect
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| 05000528/LER-1986-007, :on 860226,particulate Air Filter from Plant Vent Radiation Monitoring Unit RU-143 Inadvertently Discarded.Caused by Chemistry Technician Error.Applicable Procedure Revised to Include Caution Statement |
- on 860226,particulate Air Filter from Plant Vent Radiation Monitoring Unit RU-143 Inadvertently Discarded.Caused by Chemistry Technician Error.Applicable Procedure Revised to Include Caution Statement
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| 05000529/LER-1986-008, Corrected Forwarding Ltr to LER 86-008-00,changing Identification Number from ANPP-86646-EEVB/PGN/98.05 to ANPP-36646-EEVB/PGN/98.05 | Corrected Forwarding Ltr to LER 86-008-00,changing Identification Number from ANPP-86646-EEVB/PGN/98.05 to ANPP-36646-EEVB/PGN/98.05 | |
| 05000529/LER-1986-008-01, :on 860423,main Steam Isolation Sys Actuation Occurred in Trains a & B During Plant Protection Sys Monthly Functional Test.Caused by Personnel Failure to Follow Procedure.Technicians Counseled & Disciplined |
- on 860423,main Steam Isolation Sys Actuation Occurred in Trains a & B During Plant Protection Sys Monthly Functional Test.Caused by Personnel Failure to Follow Procedure.Technicians Counseled & Disciplined
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| 05000529/LER-1986-009, :on 860219,during Cold Shutdown,Train B Main Steam Isolation Signal Actuation Occurred,Actuating Esf. Caused by Incorrect Amperage fuse.Eight-amp Fuse Installed in Affected Path |
- on 860219,during Cold Shutdown,Train B Main Steam Isolation Signal Actuation Occurred,Actuating Esf. Caused by Incorrect Amperage fuse.Eight-amp Fuse Installed in Affected Path
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| 05000529/LER-1986-009-01, :on 860219,main Steam Isolation Sys Actuation Occurred.Caused by Application of Incorrect Amperage Fuse. Fuse Replaced.Investigation to Determine Why Wrong Fuse Installed Undertaken |
- on 860219,main Steam Isolation Sys Actuation Occurred.Caused by Application of Incorrect Amperage Fuse. Fuse Replaced.Investigation to Determine Why Wrong Fuse Installed Undertaken
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| 05000528/LER-1986-009, Corrected Ltr Revising Util Tracking Number Forwarding LER 86-009-00 Re Failure to Isolate Waste Gas Holdup Sys | Corrected Ltr Revising Util Tracking Number Forwarding LER 86-009-00 Re Failure to Isolate Waste Gas Holdup Sys | |
| 05000529/LER-1986-010-01, :on 860415,discovered That Local Leak Rate Test Not Performed on Containment Isolation Valve.Caused by Personnel Error.Local Leak Rate Test Performed on 860415 & Valve Declared Operable |
- on 860415,discovered That Local Leak Rate Test Not Performed on Containment Isolation Valve.Caused by Personnel Error.Local Leak Rate Test Performed on 860415 & Valve Declared Operable
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| 05000528/LER-1986-010, :on 860120,results of Surveillance Test Procedure Exceeded Tech Spec Acceptance Criteria.Caused by Licensed Operator Error.Operator Counseled.Shift Supervisors Will Take More Responsibility |
- on 860120,results of Surveillance Test Procedure Exceeded Tech Spec Acceptance Criteria.Caused by Licensed Operator Error.Operator Counseled.Shift Supervisors Will Take More Responsibility
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| 05000528/LER-1986-011, :on 860217,noble Gas Grab Sample for Condenser Air Removal Effluent Monitor Taken Over 4 H Late,In Violation of Tech Spec 3.3.3.9.Caused by Personnel Error. Personnel Counseled & Sample Obtained |
- on 860217,noble Gas Grab Sample for Condenser Air Removal Effluent Monitor Taken Over 4 H Late,In Violation of Tech Spec 3.3.3.9.Caused by Personnel Error. Personnel Counseled & Sample Obtained
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| 05000529/LER-1986-011-01, :on 860429,w/unit in Hot Standby,Both balance- of-plant/ESFAS Trains Determined Inoperable.Caused by Insufficient Length of Pins in ESFAS Module Pin Connectors. Pins Replaced |
- on 860429,w/unit in Hot Standby,Both balance- of-plant/ESFAS Trains Determined Inoperable.Caused by Insufficient Length of Pins in ESFAS Module Pin Connectors. Pins Replaced
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| 05000528/LER-1986-012, :on 860306,discovered That 860304 Surveillance Test 41ST-1ZZ16 Performed Beyond Max Allowable Time for Three Consecutive Tests.Caused by Personnel Error.Dept Guideline Developed |
- on 860306,discovered That 860304 Surveillance Test 41ST-1ZZ16 Performed Beyond Max Allowable Time for Three Consecutive Tests.Caused by Personnel Error.Dept Guideline Developed
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| 05000528/LER-1986-012-01, :on 860321,intercell Resistance Measurement Data Exceeded Tech Specs & Data Misinterpreted as Acceptable.Caused by Personnel Error.Personnel Counseled. Other Surveillance Test Credit Taken Reviewed |
- on 860321,intercell Resistance Measurement Data Exceeded Tech Specs & Data Misinterpreted as Acceptable.Caused by Personnel Error.Personnel Counseled. Other Surveillance Test Credit Taken Reviewed
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| 05000529/LER-1986-013-01, :on 860324,no Initial Surveillance Testing Performed for Two Containment Penetration Conductor Overcurrent Protective Devices.Caused by Personnel Error. Devices Tested |
- on 860324,no Initial Surveillance Testing Performed for Two Containment Penetration Conductor Overcurrent Protective Devices.Caused by Personnel Error. Devices Tested
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| 05000528/LER-1986-013, :on 860221,spurious High Radiation Signal on Spent Fuel Pool Area Radiation Monitor RU-31 Occurred, Resulting in ESF Actuation.Caused by Electrical Noise in Grounding Sys.Design Change Implemented |
- on 860221,spurious High Radiation Signal on Spent Fuel Pool Area Radiation Monitor RU-31 Occurred, Resulting in ESF Actuation.Caused by Electrical Noise in Grounding Sys.Design Change Implemented
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| 05000529/LER-1986-014, :on 860325,during Plant Protection Sys Monthly Functional Test,Main Steam Isolation Sys Actuation on Trains a & B Occurred.Caused by Technicians Not Adhering to Procedural Instructions.Technicians Counseled |
- on 860325,during Plant Protection Sys Monthly Functional Test,Main Steam Isolation Sys Actuation on Trains a & B Occurred.Caused by Technicians Not Adhering to Procedural Instructions.Technicians Counseled
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| 05000528/LER-1986-014-01, :on 860411,two Spurious Actuations of Fuel Bldg Essential Ventilation Sys Occurred.Caused by Dirty/Oxidized Relay Contacts in Feedwater Pump Circuit Breaker Control Circuit.Contacts Cleaned |
- on 860411,two Spurious Actuations of Fuel Bldg Essential Ventilation Sys Occurred.Caused by Dirty/Oxidized Relay Contacts in Feedwater Pump Circuit Breaker Control Circuit.Contacts Cleaned
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| 05000528/LER-1986-014, :on 860411,two Actuations of Fuel Bldg Essential Ventilation Sys Occurred.Cause Undetermined.Low Range Monitor RU-145 Declared Inoperable.Action Statement & Sampling Requirements Initiated |
- on 860411,two Actuations of Fuel Bldg Essential Ventilation Sys Occurred.Cause Undetermined.Low Range Monitor RU-145 Declared Inoperable.Action Statement & Sampling Requirements Initiated
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| 05000529/LER-1986-015-01, :on 860404,automatic Actuation of All Four Channels of Reactor Protection Sys Occurred Due to Low RCS Flow Through Steam Generator 2.Strainer Flushed & Seal Injection Flow Restored |
- on 860404,automatic Actuation of All Four Channels of Reactor Protection Sys Occurred Due to Low RCS Flow Through Steam Generator 2.Strainer Flushed & Seal Injection Flow Restored
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| 05000528/LER-1986-015, :on 860126,after Planned Trip for Load Rejection Test,Required Dose Equivalent Iodine Sample Not Performed.Caused by Technician Failing to Prioritize I-131 Sampling.Required Tech Spec Reading Updated |
- on 860126,after Planned Trip for Load Rejection Test,Required Dose Equivalent Iodine Sample Not Performed.Caused by Technician Failing to Prioritize I-131 Sampling.Required Tech Spec Reading Updated
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| 05000529/LER-1986-016-01, :on 860416,pressurized Heaters Operated in Condition Contrary to Tech Specs.Caused by Personnel & Procedural Error.Improper Amperage Calculation Formula Corrected |
- on 860416,pressurized Heaters Operated in Condition Contrary to Tech Specs.Caused by Personnel & Procedural Error.Improper Amperage Calculation Formula Corrected
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| 05000528/LER-1986-016, :on 860127,operator Failed to Perform High Containment Pressure Surveillance Test within Required Time. Caused by Operator Error.Surveillance Performed.Operator Counseled.Supervisors Reviewed Procedures |
- on 860127,operator Failed to Perform High Containment Pressure Surveillance Test within Required Time. Caused by Operator Error.Surveillance Performed.Operator Counseled.Supervisors Reviewed Procedures
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| 05000529/LER-1986-017-01, :on 860911,actuation of Reactor Protection Sys Initiated Automatic Reactor Trip.Caused by Effects of Reactor Coolant Pump Speed Transient on Core Protection Calculators (Cpc).Cpc Software Updated |
- on 860911,actuation of Reactor Protection Sys Initiated Automatic Reactor Trip.Caused by Effects of Reactor Coolant Pump Speed Transient on Core Protection Calculators (Cpc).Cpc Software Updated
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| 05000528/LER-1986-017, :on 860720,Train a Fuel Bldg Essential Ventilation Actuation Signal Occurred in Response to Signal from Radiation Monitor RU-31.Root Cause Undetermined.Problem Being Evaluated |
- on 860720,Train a Fuel Bldg Essential Ventilation Actuation Signal Occurred in Response to Signal from Radiation Monitor RU-31.Root Cause Undetermined.Problem Being Evaluated
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| 05000529/LER-1986-018-01, :on 860718,Tech Spec 3.0.3 Entered Due to Three Inoperable Charging Pumps.Charging Pumps a & B Taken Out of Svc for Repairs,Causing Pump E Gas Binding.Operations & Preventive Maint Procedures Revised |
- on 860718,Tech Spec 3.0.3 Entered Due to Three Inoperable Charging Pumps.Charging Pumps a & B Taken Out of Svc for Repairs,Causing Pump E Gas Binding.Operations & Preventive Maint Procedures Revised
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| 05000528/LER-1986-018, :on 860307,automatic Reactor Trip Occurred Due to Low Level Condition in Steam Generator 2.Caused by Anomaly in Speed Control Circuitry for Main Feedwater Pump A.Circuit Board Will Be Replaced |
- on 860307,automatic Reactor Trip Occurred Due to Low Level Condition in Steam Generator 2.Caused by Anomaly in Speed Control Circuitry for Main Feedwater Pump A.Circuit Board Will Be Replaced
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| 05000529/LER-1986-018, :on 860718,TS 3.0.3 Entered Due to Three Inoperable Charging Pumps.Replaced Charging Pump a |
- on 860718,TS 3.0.3 Entered Due to Three Inoperable Charging Pumps.Replaced Charging Pump a
| 10 CFR 50.73(a)(2) |
| 05000529/LER-1986-019-02, :on 860729,determined That Gas Grab Samples Not Taken & Analyzed within Required Time Limits Between 860721 & 860728.Caused by Personnel Miscommunication.Concurrent sign-offs Will Be Used |
- on 860729,determined That Gas Grab Samples Not Taken & Analyzed within Required Time Limits Between 860721 & 860728.Caused by Personnel Miscommunication.Concurrent sign-offs Will Be Used
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| 05000529/LER-1986-021-01, :on 860806,discovered That Train B LPSI Pump Header Discharge Throttle Valve Not Adjusted to Proper Setting.Caused by Personnel Error on 860717 Due to Unclear Procedure.Separate Procedures in Effect |
- on 860806,discovered That Train B LPSI Pump Header Discharge Throttle Valve Not Adjusted to Proper Setting.Caused by Personnel Error on 860717 Due to Unclear Procedure.Separate Procedures in Effect
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| 05000529/LER-1986-022-01, :on 860814,discovered That HPSI Valve Declared Operable Based Upon Completion of Superseded Retest Utilizing Incorrect Acceptance Criteria.Caused by Personnel Error.Personnel Counseled |
- on 860814,discovered That HPSI Valve Declared Operable Based Upon Completion of Superseded Retest Utilizing Incorrect Acceptance Criteria.Caused by Personnel Error.Personnel Counseled
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| 05000528/LER-1986-022, :on 860724,Train B Containment Purge Isolation Actuation Signal Initiated.Caused by Personnel Error.Shift Briefings on Overall Necessity for Strict Procedural Adherence Will Be Conducted |
- on 860724,Train B Containment Purge Isolation Actuation Signal Initiated.Caused by Personnel Error.Shift Briefings on Overall Necessity for Strict Procedural Adherence Will Be Conducted
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| 05000529/LER-1986-023-01, :on 861224,reactor Trip Initiated.Caused by Intermittent Ground on 125-volt Dc Bus.Ground Removed & Power Supply Replaced.Further Evaluations to Determine Root Cause of Degraded Voltage Condition Underway |
- on 861224,reactor Trip Initiated.Caused by Intermittent Ground on 125-volt Dc Bus.Ground Removed & Power Supply Replaced.Further Evaluations to Determine Root Cause of Degraded Voltage Condition Underway
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| 05000529/LER-1986-024-01, :on 860514,determined That Several Steam Generator Snubbers Inoperable Since 860310 Due to Lack of Visual Exam.Caused by Personnel Error.Event Reviewed W/ Licensed Operators & Supervisors |
- on 860514,determined That Several Steam Generator Snubbers Inoperable Since 860310 Due to Lack of Visual Exam.Caused by Personnel Error.Event Reviewed W/ Licensed Operators & Supervisors
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| 05000528/LER-1986-024, :on 860207,reactor Trip Occurred Due to Low Level Condition in Steam Generator 1.Caused by Operator Error During Transition from Downcomer to Economizer Feed Paths.Event Reviewed by All Licensed Operators |
- on 860207,reactor Trip Occurred Due to Low Level Condition in Steam Generator 1.Caused by Operator Error During Transition from Downcomer to Economizer Feed Paths.Event Reviewed by All Licensed Operators
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| 05000529/LER-1986-025-02, :on 860525,automatic Reactor Trip Occurred Due to Low Level Condition in Steam Generator.Caused by Personnel Error.Temporary Mod Implemented to Reduce Refill Flow Demand Signal |
- on 860525,automatic Reactor Trip Occurred Due to Low Level Condition in Steam Generator.Caused by Personnel Error.Temporary Mod Implemented to Reduce Refill Flow Demand Signal
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| 05000529/LER-1986-026-01, :on 860825,reactor Trip Occurred,Initiated by Main Turbine Generator Trip.Caused by Loss of Generator Excitation Due to Transducer Calibr at Unnecessarily Low Value.Transducer Recalibr |
- on 860825,reactor Trip Occurred,Initiated by Main Turbine Generator Trip.Caused by Loss of Generator Excitation Due to Transducer Calibr at Unnecessarily Low Value.Transducer Recalibr
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| 05000528/LER-1986-026, :on 860321,invalid Intercell Resistance Measurement Data Recorded During Preoperational Testing. Caused by Personnel Error.Personnel Counseled & 18-month Surveillance Test Completed |
- on 860321,invalid Intercell Resistance Measurement Data Recorded During Preoperational Testing. Caused by Personnel Error.Personnel Counseled & 18-month Surveillance Test Completed
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| 05000529/LER-1986-027-01, :on 860531,turbine Trip Caused Actuation of Reactor Protection Sys,Initiating Reactor Trip.Caused by Personnel Error Due to Inadequate Procedures.Plant Operating Procedures Revised |
- on 860531,turbine Trip Caused Actuation of Reactor Protection Sys,Initiating Reactor Trip.Caused by Personnel Error Due to Inadequate Procedures.Plant Operating Procedures Revised
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