03-22-2016 | On January 26, 2016, at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, the Control Room received a Steam Generator Steam Flow/Feed Flow mismatch alarm. Operators found Steam Generator ( SG) Train C Feedwater Regulating Valve closed and in manual. SG C Feedwater Regulating Valve could not be manually reopened. At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, Operators manually tripped the Unit 1 reactor due to lowering level on SG C. The Auxiliary Feedwater ( AFW) system automatically actuated on a SG low level signal and operators took manual control of AFW at 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />.
The cause of loss of Main Feedwater to SG C was a failure of the Manual 7300 Series Tracking Driver (NTD) circuit card which forced SG C Feedwater Regulating Valve-closed and prevented the operators from taking manual control or switching back to automatic valve control. As a corrective action, the Manual NTD circuit card was replaced. The manual actuation of the Reactor Protection System and subsequent automatic AFW actuation are both reportable under 10 CFR 50.73(a)(2)(iv)(A). The event was of very low risk significance and no radioactive release occurred; therefore, there was no adverse effect on the health and safety of the public. |
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LER-2016-001, Unit 1 Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed ClosedSouth Texas Unit 1 |
Event date: |
01-26-2016 |
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Report date: |
03-22-2016 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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4982016001R00 - NRC Website |
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Category:Letter
MONTHYEARML24318C5082024-11-13013 November 2024 Condition Prohibited by Technical Specifications IR 05000498/20253012024-11-0707 November 2024 Notification of NRC Initial Operator Licensing Examination 05000498/2025301; 05000499/2025301 IR 05000498/20240032024-11-0707 November 2024 Integrated Inspection Report 05000498/2024003 and 05000499/2024003 ML24304B0512024-10-30030 October 2024 Cycle 26 Core Operating Limits Report IR 05000498/20244022024-10-23023 October 2024 Security Baseline Inspection Report 05000498/2024402 and 05000499/2024402 05000499/LER-2024-003, Containment Isolation Valve Inoperable Resulting in Condition Prohibited by Technical Specification and Prevention of Fulfillment of Safety Function2024-10-22022 October 2024 Containment Isolation Valve Inoperable Resulting in Condition Prohibited by Technical Specification and Prevention of Fulfillment of Safety Function ML24295A0772024-10-21021 October 2024 Licensed Operator Positive Fitness-for-Duty Test 05000499/LER-2024-002, Two Control Room Envelope HVAC Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-10-17017 October 2024 Two Control Room Envelope HVAC Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function ML24290A1162024-10-16016 October 2024 Change to South Texas Project Electric Generating Station (STPEGS) Emergency Plan ML24255A0322024-09-30030 September 2024 The Associated Independent Spent Fuel Storage Installation - Notice of Consideration of Approval of Direct Transfer of Licenses and Opportunity to Request a Hearing (EPID L-2024-LLM-0002) - Letter ML24269A1762024-09-25025 September 2024 Tpdes Permit Renewal Application WQ0001 908000 05000498/LER-2024-004, Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps2024-09-19019 September 2024 Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps ML24271A3022024-09-18018 September 2024 STP-2024-09 Post-Exam Comments - Redacted ML24274A0902024-09-16016 September 2024 Written Response - EA-24-026 STP Operator - Redacted ML24250A1882024-09-11011 September 2024 Request for Information for an NRC Post-Approval Site Inspection for License Renewal ML24249A3372024-09-0404 September 2024 Inservice Inspection Summary Report - 2RE23 05000499/LER-2024-001-01, Supplement to Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators2024-08-29029 August 2024 Supplement to Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators ML24234A0912024-08-27027 August 2024 NRC Initial Operator Licensing Examination Approval 05000498/2024301; 05000499/2024301 IR 05000498/20240052024-08-22022 August 2024 Updated Inspection Plan for South Texas Project Electric Generating Station, Units 1 and 2 (Report 05000498/2024005 and 05000499/2024005) IR 05000498/20240022024-08-0909 August 2024 Integrated Inspection Report 05000498/2024002 and 05000499/2024002 IR 05000498/20240102024-08-0808 August 2024 Biennial Problem Identification and Resolution Inspection Report 05000498/2024010 and 05000499/2024010 ML24213A0842024-07-31031 July 2024 Application for Order Consenting to Direct Transfer of Licenses ML24218A1462024-07-26026 July 2024 2. EPA Comments on South Texas Project Exemption Ea/Fonsi ML24207A1782024-07-25025 July 2024 Licensed Operator Positive Fitness-For-Duty Test 05000499/LER-2024-001, Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators2024-07-0202 July 2024 Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators 05000498/LER-2024-003, Condition Prohibited by Technical Specifications and Potential Loss of Safety Function Due to Inoperable Low Head Safety Injection Pump2024-07-0101 July 2024 Condition Prohibited by Technical Specifications and Potential Loss of Safety Function Due to Inoperable Low Head Safety Injection Pump 05000498/LER-2024-002-01, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-06-27027 June 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-003-01, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-06-19019 June 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24136A2872024-05-15015 May 2024 Submittal of 2024 Nrc/Fema Evaluated Exercise Scenario Manual ML24136A2842024-05-15015 May 2024 Independent Spent Fuel Storage Installation Supplement to Request for Exemption from Various Part 72 Regulations Resulting from Fuel Basket Design Control Compliance ML24130A2712024-05-0909 May 2024 Re Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function ML24128A1572024-05-0707 May 2024 Independent Spent Fuel Storage Installation Request for Exemption from Various Part 72 Regulations Resulting from Fuel Basket Design Control Compliance IR 05000498/20240012024-05-0606 May 2024 Integrated Inspection Report 05000498/2024001 & 05000499/2024001 ML24120A3762024-04-29029 April 2024 Annual Dose Report for 2023 05000498/LER-2023-004-01, Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water2024-04-25025 April 2024 Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water ML24116A3032024-04-25025 April 2024 Operations Quality Assurance Plan Condition Adverse to Quality Definition Change Resulting in a Reduction in Commitment ML24116A2282024-04-25025 April 2024 Annual Environmental Operating Report ML24117A1602024-04-24024 April 2024 2023 Radioactive Effluent Release Report ML24102A2452024-04-23023 April 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0046 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24113A3122024-04-22022 April 2024 Cycle 24 Core Operating Limits Report ML24097A0072024-04-0606 April 2024 Relief Request Number RR-ENG-4-07 – Request for an Alternative to ASME Code Case N-729-6 for Reactor Vessel Head Penetration 75 05000498/LER-2024-001, Re Two Steam Generator Power Operated Relief Valves (Porvs) Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-04-0101 April 2024 Re Two Steam Generator Power Operated Relief Valves (Porvs) Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function ML24088A3022024-03-28028 March 2024 Financial Assurance for Decommissioning - 2024 Update NOC-AE-240040, Response to Request for Additional Information for Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2024-03-21021 March 2024 Response to Request for Additional Information for Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML24080A2902024-03-19019 March 2024 Nuclear Liability Certificates of Insurance ML24066A2002024-03-0606 March 2024 10 CFR 50.46 Thirty-Day Report of Significant ECCS Model Changes ML24079A1312024-03-0505 March 2024 Nuclear Insurance Protection IR 05000498/20230062024-02-28028 February 2024 Annual Assessment Letter for South Texas Project Electric Generating Station, Units 1 and 2 (Report 05000498/2023006 and 05000499/2023006) ML24060A1742024-02-28028 February 2024 Submittal of Annual Fitness for Duty Performance Report for 2023 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML24318C5082024-11-13013 November 2024 Condition Prohibited by Technical Specifications 05000499/LER-2024-003, Containment Isolation Valve Inoperable Resulting in Condition Prohibited by Technical Specification and Prevention of Fulfillment of Safety Function2024-10-22022 October 2024 Containment Isolation Valve Inoperable Resulting in Condition Prohibited by Technical Specification and Prevention of Fulfillment of Safety Function 05000499/LER-2024-002, Two Control Room Envelope HVAC Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-10-17017 October 2024 Two Control Room Envelope HVAC Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2024-004, Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps2024-09-19019 September 2024 Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps 05000499/LER-2024-001-01, Supplement to Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators2024-08-29029 August 2024 Supplement to Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators 05000499/LER-2024-001, Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators2024-07-0202 July 2024 Automatic Reactor Trip and Actuation of Two of Three Emergency Diesel Generators 05000498/LER-2024-003, Condition Prohibited by Technical Specifications and Potential Loss of Safety Function Due to Inoperable Low Head Safety Injection Pump2024-07-0101 July 2024 Condition Prohibited by Technical Specifications and Potential Loss of Safety Function Due to Inoperable Low Head Safety Injection Pump 05000498/LER-2024-002-01, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-06-27027 June 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-003-01, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-06-19019 June 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function ML24130A2712024-05-0909 May 2024 Re Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-004-01, Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water2024-04-25025 April 2024 Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water 05000498/LER-2024-001, Re Two Steam Generator Power Operated Relief Valves (Porvs) Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-04-0101 April 2024 Re Two Steam Generator Power Operated Relief Valves (Porvs) Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-004, Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water2024-02-0505 February 2024 Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Chilled Water 05000499/LER-2023-002, Automatic Actuation of Emergency Diesel Generator Due to Lockout of Switchyard Electrical Bus2024-01-30030 January 2024 Automatic Actuation of Emergency Diesel Generator Due to Lockout of Switchyard Electrical Bus 05000499/LER-2023-001, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-01-15015 January 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-003, Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function2024-01-0909 January 2024 Two Essential Chilled Water Trains Inoperable Resulting in a Condition That Could Have Prevented Fulfillment of a Safety Function 05000498/LER-2023-001-01, Supplement to Pressurizer Power Operated Valve Failed to Open2023-07-26026 July 2023 Supplement to Pressurizer Power Operated Valve Failed to Open 05000498/LER-2023-001, Pressurizer Power Operated Relief Valve Failed to Open2023-06-12012 June 2023 Pressurizer Power Operated Relief Valve Failed to Open 05000499/LER-2021-002-01, Supplement to Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Core Cooling System and Containment Spray System2022-07-0505 July 2022 Supplement to Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Core Cooling System and Containment Spray System 05000499/LER-2022-001, From South Texas Project Unit 2, Automatic Actuation of Emergency Diesel Generator Due to Lockout of Switchyard Electrical Bus2022-03-0303 March 2022 From South Texas Project Unit 2, Automatic Actuation of Emergency Diesel Generator Due to Lockout of Switchyard Electrical Bus 05000499/LER-2021-002, Re Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Core Cooling System and Containment Spray System2021-12-21021 December 2021 Re Condition Prohibited by Technical Specifications Due to Inoperable Train of Essential Core Cooling System and Containment Spray System 05000499/LER-2021-001, Condition Prohibited by Technical Specifications Due to Inoperable Containment Isolation Valve2021-09-0909 September 2021 Condition Prohibited by Technical Specifications Due to Inoperable Containment Isolation Valve 05000498/LER-2021-001, Frozen Common Sensing Line Results in Loss of Two Main Feedwater Pumps Leading to Automatic Reactor Protection and Auxiliary Feedwater Systems Actuations Due to Low Steam Generator Level2021-04-15015 April 2021 Frozen Common Sensing Line Results in Loss of Two Main Feedwater Pumps Leading to Automatic Reactor Protection and Auxiliary Feedwater Systems Actuations Due to Low Steam Generator Level 05000498/LER-2020-001, Automatic Actuation of Emergency Diesel Generators Due to Lockout of Switchyard Electrical Bus2020-05-22022 May 2020 Automatic Actuation of Emergency Diesel Generators Due to Lockout of Switchyard Electrical Bus 05000498/LER-2017-0022018-01-22022 January 2018 Unit 1 Condition Prohibited by Technical Specifications Due to Inoperable Control Room Envelope Makeup Filtration System Heating Coil, LER 17-002-00 for South Texas Project, Unit 1, Regarding Condition Prohibited by Technical Specifications Due to Inoperable Control Room Envelope Makeup Filtration System Heating Coil 05000498/LER-2017-0012017-05-11011 May 2017 Unit 1 failure of a timing relay during a Technical Specification surveillance, LER 17-001-00 for South Texas, Unit 1, Regarding Failure of a Timing Relay During a Technical Specification Surveillance 05000498/LER-2016-0022016-06-29029 June 2016 Unit 1 Automatic Reactor Trip and Auxiliary Feedwater System Actuation Following Turbine Trip due to Generator Lockout, LER 16-002-00 for South Texas Project, Unit 1, Regarding Automatic Reactor Trip and Auxiliary Feedwater System Actuation Following Turbine Trip Due to Generator Lockout 05000498/LER-2016-0012016-03-22022 March 2016 Unit 1 Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed, LER 16-001-00 for South Texas Project, Unit 1, Regarding Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed NOC-AE-05001865, LER 05-01-00 South Texas Project Unit 2 Regarding Shutdown of STP Unit 2 Due to Reactor Coolant System Pressure Boundary Leak2005-04-0505 April 2005 LER 05-01-00 South Texas Project Unit 2 Regarding Shutdown of STP Unit 2 Due to Reactor Coolant System Pressure Boundary Leak NOC-AE-04001681, LER 01-03-007 for South Texas, Unit 1 Regarding Failure of Main Steam Power Operated Relief Valves 1B2004-02-18018 February 2004 LER 01-03-007 for South Texas, Unit 1 Regarding Failure of Main Steam Power Operated Relief Valves 1B NOC-AE-00000840, 1,Unauthorized Entry Into Protected Area,Safeguards Event Report2000-05-0404 May 2000 1,Unauthorized Entry Into Protected Area,Safeguards Event Report 2024-09-19
[Table view] |
Reported lessons leamed are incorporated into the licensing process and fed back to industry.
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I. Description of reportable event
A. Reportable event classification
This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) as an event or condition that resulted in a manual actuation of the Reactor Protection System and also as an event or condition that resulted in an automatic actuation of the Auxiliary Feedwater (AFW) {BA} system.
B. Plant operating conditions prior to event
On January 26, 2016, Unit 1 was operating in Mode 1 at 100 percent power.
C. Status of structures, systems, and components (SSCs) that were inoperable at the start of the event and that contributed to the event There were no SSCs that were inoperable at the start of the event that contributed to the event.
D. Narrative summary of the event
On January 26, 2016, at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, STP Unit 1 Control Room received a Steam Generator Steam FlOw/Feed Flow mismatch alarm. C Train Steam Generator (SG) Feedwater Regulating Valve {SJ} failed and could not be manually reopened.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, Operators manually tripped the Unit 1 reactor due to lowering level in SG C which is reportable under 10 CFR 50.73(a)(2)(iv)(A) as a valid manual actuation of the Reactor Protection System.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, all four AFW pumps actuated due to lowering SG C level. This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) as a valid automatic actuation of the AFW system.
At 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />, operators took manual control of AFW.
At 2333 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.877065e-4 months <br />, Operations tripped Steam Generator Feedwater Pumps 11, 12 and 13 and placed Startup Feedwater Pump in service.
At 2355, Main Feedwater was placed in service through the preheater bypass valves and Low Power Feedwater Regulating Valves to feed Steam Generators. The Auxiliary Feedwater Pumps were subsequently secured.
E. Method of discovery
The manual reactor trip and AFW actuation were self-revealing. A Steam Generator Flow/Feed Flow mismatch alarm was received. Operators found SG C Feedwater Regulating Valve closed and in manual. Operators attempted to open the valve both in manual and automatic without success. A manual reactor trip was initiated in response. The AFW system actuated automatically on a SG low level signal.
South Texas Unit 1 05000498
II. Component failures
A. Failure mode, mechanism, and effects of failed component
The component failure applicable to this Licensee Event Report (LER) is related to the Manual 7300 Series Tracking Driver (NTD) circuit card {JB} which controls the SG C Feedwater Regulating Valve.
The cause of the Manual NTD circuit card failure was due to an integrated circuit (IC) chip (W30-2) output pin 8 which failed low. This chip is in the PRIORITY LOWER circuit and with the failed condition it forced the circuit card into the manual mode and drove the output to 0%.
This caused the Manual/Auto (M/A) station to shift to the manual mode and is the reason Operators could not get the Feedwater Regulating Valve to respond when depressing the RAISE button on the M/A station. This condition caused the SG C Feedwater Regulating Valve to close, lowering SG C level, and resulting in Operators manually tripping the reactor.
B. Cause of component failure
The cause of the NTD circuit card failure was attributed to random failure of an electronic component.
C. Systems or secondary functions that were affected by failure of components with multiple functions The SG C Feedwater Regulating Valve does not have multiple functions that affect other systems. The failure of this component contributed to the manual reactor trip.
D. Failed component information (Energy Industry Identification System (EIIS) designators provided in {brackets}) Main Feedwater System {SJ} Feedwater/ Steam Generator Water Level Control System {JB} 7300 Series Tracking Driver NTD card {CBD} Manufacturer: Westinghouse Electric Corporation {W120} Model: 2838A45G01
III. Analysis of the event
A. Safety system responses that occurred
The Reactor Protection System and AFW systems both responded to this event.
B. Duration of safety system inoperability
There were no SSCs that were inoperable at the start of the event that contributed to the event.
C. Safety consequences and implications
No Technical Specification LCOs were entered due to this event. Operators manually tripped the reactor following the loss of Main Feedwater to SG C.
For the Probabilistic Risk Assessment (PRA) analysis, the initiating event is classified as a Partial Loss of Main Feedwater (PLMFW) — the isolation of main feedwater to SG C led to decreasing levels in the SG C which resulted in a reactor trip. The PLMFW event is a modeled initiating event, and no risk significant equipment was confirmed out of service.
The STP PRA was used to estimate the relevant metrics for a reactor trip, Conditional Core Damage Probability (CCDP) and Conditional Large Early Release Probability (CLERP), given that the PLMFW initiating event actually occurred. The CCDP and CLERP were determined to be 6.1E-07 and 3.6E-08 respectively, indicating very low risk significance.
The event was of very low risk significance and no radioactive release occurred; therefore, there was no adverse effect on the health and safety of the public.
IV. Cause of the event
Prior to the manual reactor trip, SG C Feedwater Regulating Valve closed resulting in lowering water level in SG C due to the random failure of the Manual 7300 Series Tracking Driver circuit card. The Manual NTD card failure forced the Feedwater Regulating Valve closed and prevented further operation of the valve. Operators initiated a manual reactor trip due to lowering SG level and the AFW system actuated automatically on a SG low level signal. There were no human performance errors that contributed to the event.
V. Corrective actions
The Manual NTD circuit card was replaced. The circuit card was installed in 2009. The failure of the card is considered an infant mortality failure (i.e.
first documented failure for this type. The Preventive Maintenance replacement frequency for these NTD circuit cards is 15 years.
A review of all Auto and Manual NTD circuit cards installed in the Feedwater Regulating Valve loops in Unit 1 and Unit 2 indicate they were installed 8 to 11 years ago and all have different sequenced serial numbers which indicates they are not manufactured from the same lot.
VI. Previous similar events
An Operating Experience review was conducted as part of the cause evaluation performed for this event.
Five other NTD card failures occurred while in service since 1998. All but one failure caused a minor plant transient requiring operator action. In 2001, a modification was made to the Feedwater Regulating Valve loops to add dual NTD cards (auto and manual) to increase reliability of this single point vulnerability circuit. In 2004, the loop was modified again to add computer points to monitor the 0-10 VDC output signal of both the Auto and Manual NTD cards which provides an annunciation to alert the Control Room Operators of degraded/failed conditions. The last failure occurred in 2009 in Unit 2 after both modifications were installed.
The card failure did not cause a plant transient because the Control Room received an alarm identifying the degraded condition. The 2009 failure occurred after the Manual NTD card was in service for approximately 1 year.
There were no previous STP Licensee Event Reports submitted related to failure of dual tracker (auto and manual) NTD card.
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05000498/LER-2016-001 | Unit 1 Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed LER 16-001-00 for South Texas Project, Unit 1, Regarding Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000498/LER-2016-002 | Unit 1 Automatic Reactor Trip and Auxiliary Feedwater System Actuation Following Turbine Trip due to Generator Lockout LER 16-002-00 for South Texas Project, Unit 1, Regarding Automatic Reactor Trip and Auxiliary Feedwater System Actuation Following Turbine Trip Due to Generator Lockout | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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