05000498/LER-2016-001, Regarding Manual Reactor Trip Due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed
| ML16098A327 | |
| Person / Time | |
|---|---|
| Site: | South Texas |
| Issue date: | 03/22/2016 |
| From: | Gerry Powell South Texas |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| NOC-AE-16003354, STI: 34290779 LER 16-001-00 | |
| Download: ML16098A327 (7) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) |
| 4982016001R00 - NRC Website | |
text
South Texas Project Electric Generating Station P.O. BoK 289 Wadsworth, Texas 77483 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555-0001 South Texas Project Unit 1 March 22, 2016 NOC-AE-16003354 10 CFR 50.73 Docket No. STN 50-498 Licensee Event Report 2016-001-00 Unit 1 Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed Pursuant to 10 CFR 50.73(a)(2)(iv)(A), STP Nuclear Operating Company (STPNOC) hereby submits the attached South Texas Project (STP) Unit 1 Licensee Event Report (LER) 2016-001-00 for a valid manual actuation of the Reactor Protection System and for a valid automatic actuation of the Auxiliary Feedwater System.
The event did not have an adverse effect on the health and safety of the public.
There are no commitments in this letter.
If there are any questions, please contact Robyn Savage at (361) 972-7438 or me at (361) 972-7566.
G. T. Powell Site Vice President rds
Attachment:
Unit 1 LER 2016-001-00 STI: 34290779
cc:
(paper copy)
Regional Administrator, Region IV U.S. Nuclear Regulatory Commission 1600 East Lamar Boulevard Arlington, TX 76011-4511 Lisa M. Regner Senior Project Manager U.S. Nuclear Regulatory Commission One White Flint North (08H04) 11555 Rockville Pike Rockville, MD 20852 NRC Resident Inspector U.S. Nuclear Regulatory Commission P. 0. Box 289, Mail Code: MN116 Wadsworth, TX 77483 (electronic copy)
NOC-AE-16003354 Page 2 of 2 Morgan, Lewis & Bockius LLP Steve Frantz, Esquire U.S. Nuclear Regulatory Commission Lisa M. Regner NRG South Texas LP Chris O'Hara Jim von Suski!
Skip Zahn CPS Energy Kevin Pollo Cris Eugster L. D. Blaylock Crain Caton & James, P.C...,.
Peter Nemeth City of Austin Elaina Ball John Wester Texas Dept. of State Health Services; Richard A. Ratliff Robert Free
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10131/2018 (11-2015)
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. PAGE South Texas Unit 1 05000498 1 OF 5
- 4. TITLE Unit 1 Manual Reactor Trip due to Loss of Main Feedwater to C Train Steam Generator When the Steam Generator Feedwater Regulating Valve Failed Closed
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED YEAR I SEQUENTIAL I REV FACILITY NAME DOCKET NUMBER MONTH DAY YEAR NUMBER NO.
MONTH DAY YEAR N/A N/A FACILITY NAME DOCKET NUMBER 01 26 2016 2016 -
001 - 00 03 22 2016 N/A N/A
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i)
- 50. 73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 1 20.2201(d) 20.2203(a)(3)(ii)
- 50. 73(a)(2)(ii)(B)
- 50. 73(a)(2)(viii)(B) 20.2203(a)(1) 20.2203(a)(4)
- 50. 73(a)(2)(iii)
- 50. 73(a)(2)(ix)(A) 20.2203(a)(2)(i) 50.36(c)( 1 )(i)(A)
...... 50. 73(a)(2)(iv)(A) 50.73(a)(2)(x)
- 10. POWER LEVEL 20.2203(a)(2)(ii) 50.36(c)(1 )(ii)(A)
- 50. 73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iii) 50.36(c}(2)
- 50. 73(a}(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(iv) 50.46(a)(3)(ii)
- 50. 73(a)(2)(v)(C)
- 73. 77(a)(1) 100%
20.2203(a)(2)(v) 50.73(a)(2)(i)(A)
- 50. 73(a)(2)(v)(D) 73.77(a)(2)(i) 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(vii) 73.77(a)(2)(ii)
(;.~~f**a***?<":;*,.* ~*:~;:;,~?!::s'1t::
50.73(a)(2)(i)(C)
OTHER Specify in Abstract below or in summary of the event On January 26, 2016, at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, STP Unit 1 Control Room received a Steam Generator Steam Flow/Feed Flow mismatch alarm. C Train Steam Generator (SG) Feedwater Regulating Valve {SJ} failed and could not be manually reopened.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, Operators manually tripped the Unit 1 reactor due to lowering level in SG C which is reportable under §50.73(a)(2)(iv)(A) as a valid manual actuation of the Reactor Protection System.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, all four AFW pumps actuated due to lowering SG C level. This event is reportable under §50. 73(a)(2)(iv)(A) as a valid automatic actuation of the AFW system.
At 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />, operators took manual control of AFW.
At 2333 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.877065e-4 months <br />, Operations tripped Steam Generator Feedwater Pumps 11, 12 and 13 and placed Startup Feedwater Pump in service.
At 2355, Main Feedwater was placed in service through the preheater bypass valves and Low Power Feedwater Regulating Valves to feed Steam Generators. The Auxiliary Feedwater Pumps were subsequently secured.
E. Method of discovery
The manual reactor trip and AFW actuation were self-revealing. A Steam Generator Flow/Feed Flow mismatch alarm was received. Operators found SG C Feedwater Regulating Valve closed and in manual. Operators attempted to open the valve both in manual and automatic without success. A manual reactor trip was initiated in response. The AFW system actuated automatically on a SG low level signal.
II.
Component failures
A. Failure mode, mechanism, and effects of failed component The component failure applicable to this Licensee Event Report (LER) is related to the Manual 7300 Series Tracking Driver (NTD) circuit card {JB} which controls the SG C Feedwater Regulating Valve.
The cause of the Manual NTD circuit card failure was due to an integrated circuit (IC) chip (W30-2) output pin 8 which failed low. This chip is in the PRIORITY LOWER circuit and with the failed condition it forced the circuit card into the manual mode and drove the output to 0%.
This caused the Manual/Auto (M/A) station to shift to the manual mode and is the reason Operators could not get the Feedwater Regulating Valve to respond when depressing the RAISE button on the M/A station. This condition caused the SG C Feedwater Regulating Valve to close, lowering SG C level, and resulting in Operators manually tripping the reactor.
B. Cause of component failure
The cause of the NTD circuit card failure was attributed to random failure of an electronic component.
- C. Systems or secondary functions that were affected by failure of components with multiple functions The SG C Feedwater Regulating Valve does not have multiple functions that affect other systems. The failure of this component contributed to the manual reactqr trip.
D. Failed component information (Energy Industry Identification System (EllS) designators provided in {brackets})
Main Feedwater System {SJ}
Feedwater/ Steam Generator Water Level Control System {JB}
7300 Series Tracking Driver NTD card {CBD}
Manufacturer: Westinghouse Electric Corporation {W120}
Model: 2838A45G01 Ill.
Analysis of the event
A. Safety system responses that occurred The Reactor Protection System and AFW systems both responded to this event.
B. Duration of safety system inoperability
There were no SSCs that were inoperable at the start of the event that contributed to the event.
2016 001 00
C. Safety consequences and implications
No Technical Specification LCOs were entered due to this event. Operators manually tripped the reactor following the loss of Main Feedwater to SG C.
For the Probabilistic Risk Assessment (PRA) analysis, the initiating event is classified as a Partial Loss of Main Feedwater (PLMFW) - the isolation of main feedwater to SG C led to decreasing levels in the SG C which resulted in a reactor trip. The PLMFW event is a modeled initiating event, and no risk significant equipment was confirmed out of service.
The STP PRA was used to estimate the relevant metrics for a reactor trip, Conditional Core Damage Probability (CCDP) and Conditional Large Early Release Probability (CLERP), given that the PLMFW initiating event actually occurred. The CCDP and CLERP were determined to be 6.1 E-07 and 3.6E-08 respectively, indicating very low risk significance.
The event was of very low risk significance and no radioactive release occurred; therefore, there was no adverse effect on the health and safety of the public.
IV.
Cause of the event
Prior to the manual reactor trip, SG C Feedwater Regulating Valve closed resulting in lowering water level in SG C due to the random failure of the Manual 7300 Series Tracking Driver circuit card. The Manual NTD card failure forced the Feedwater Regulating Valve closed and prevented further operation of the valve. Operators initiated a manual reactor trip due to lowering SG level and the AFW system actuated automatically on a SG low level signal. There were no human performance errors that contributed to the event.
V.
Corrective actions
The Manual NTD circuit card was replaced. The circuit card was installed in 2009. The failure of the card is considered an infant mortality failure (i.e. < 10 years for 7300 circuit cards) and the first documented failure for this type. The Preventive Maintenance replacement frequency for these NTD circuit cards is 15 years.
A review of all Auto and Manual NTD circuit cards installed in the Feedwater Regulating Valve loops in Unit 1 and Unit 2 indicate they were installed 8 to 11 years ago and all have different sequenced serial numbers which indicates they are not manufactured from the same lot.
VI.
Previous similar events
An Operating Experience review was conducted as part of the cause evaluation performed for this event.
Five other NTD card failures occurred while in service since 1998. All but one failure caused a minor plant transient requiring operator action. Jn 2001, a modification was made to the Feedwater Regulating Valve loops to add dual NTD cards (auto and manual) to increase reliability of this single point vulnerability circuit. In 2004, the loop was modified again to add computer points to monitor the O'" 1 O VDC output signal of both the Auto and Manual NTD cards
- which provides an annunciation to alert the Control Room Operators of degraded/failed conditions. The last failure occurred in 2009 in Unit 2 after both modifications were installed.
The card failure did not cause a plant transient because the Control Room receive.d. an alarm identifying the degraded condition. The 2009 failure occurred after the Manual NTQ card was in service for approximately 1 year.
There were no previous STP Licensee Event Reports submitted related to failure of dual tracker (auto and manual) NTD card.
I.
Description of reportable event
A. Reportable event classification
This event is reportable under §50. 73(a)(2)(iv)(A) as an event or condition that resulted in a manual actuation of the Reactor Protection System and also as an event or condition that resulted in an automatic actuation of the Auxiliary Feedwater (AFW) {BA} system.
B. Plant operating conditions prior to event
On January 26, 2016, Unit 1 was operating in Mode 1 at 100 percent power.
C. Status of structures, systems, and components (SSCs) that were inoperable at th.e start of the event and that contributed to the event There were no SSCs that were inoperable at the start of the event that contributed to the event.
D. Narrative summary of the event
On January 26, 2016, at 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, STP Unit 1 Control Room received a Steam Generator Steam Flow/Feed Flow mismatch alarm. C Train Steam Generator (SG) Feedwater Regulating Valve {SJ} failed and could not be manually reopened.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, Operators manually tripped the Unit 1 reactor due to lowering level in SG C which is reportable under §50.73(a)(2)(iv)(A) as a valid manual actuation of the Reactor Protection System.
At 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />, all four AFW pumps actuated due to lowering SG C level. This event is reportable under §50. 73(a)(2)(iv)(A) as a valid automatic actuation of the AFW system.
At 2327 hours0.0269 days <br />0.646 hours <br />0.00385 weeks <br />8.854235e-4 months <br />, operators took manual control of AFW.
At 2333 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.877065e-4 months <br />, Operations tripped Steam Generator Feedwater Pumps 11, 12 and 13 and placed Startup Feedwater Pump in service.
At 2355, Main Feedwater was placed in service through the preheater bypass valves and Low Power Feedwater Regulating Valves to feed Steam Generators. The Auxiliary Feedwater Pumps were subsequently secured.
E. Method of discovery
The manual reactor trip and AFW actuation were self-revealing. A Steam Generator Flow/Feed Flow mismatch alarm was received. Operators found SG C Feedwater Regulating Valve closed and in manual. Operators attempted to open the valve both in manual and automatic without success. A manual reactor trip was initiated in response. The AFW system actuated automatically on a SG low level signal.
II.
Component failures
A. Failure mode, mechanism, and effects of failed component The component failure applicable to this Licensee Event Report (LER) is related to the Manual 7300 Series Tracking Driver (NTD) circuit card {JB} which controls the SG C Feedwater Regulating Valve.
The cause of the Manual NTD circuit card failure was due to an integrated circuit (IC) chip (W30-2) output pin 8 which failed low. This chip is in the PRIORITY LOWER circuit and with the failed condition it forced the circuit card into the manual mode and drove the output to 0%.
This caused the Manual/Auto (M/A) station to shift to the manual mode and is the reason Operators could not get the Feedwater Regulating Valve to respond when depressing the RAISE button on the M/A station. This condition caused the SG C Feedwater Regulating Valve to close, lowering SG C level, and resulting in Operators manually tripping the reactor.
B. Cause of component failure
The cause of the NTD circuit card failure was attributed to random failure of an electronic component.
- C. Systems or secondary functions that were affected by failure of components with multiple functions The SG C Feedwater Regulating Valve does not have multiple functions that affect other systems. The failure of this component contributed to the manual reactqr trip.
D. Failed component information (Energy Industry Identification System (EllS) designators provided in {brackets})
Main Feedwater System {SJ}
Feedwater/ Steam Generator Water Level Control System {JB}
7300 Series Tracking Driver NTD card {CBD}
Manufacturer: Westinghouse Electric Corporation {W120}
Model: 2838A45G01 Ill.
Analysis of the event
A. Safety system responses that occurred The Reactor Protection System and AFW systems both responded to this event.
B. Duration of safety system inoperability
There were no SSCs that were inoperable at the start of the event that contributed to the event.
2016 001 00
C. Safety consequences and implications
No Technical Specification LCOs were entered due to this event. Operators manually tripped the reactor following the loss of Main Feedwater to SG C.
For the Probabilistic Risk Assessment (PRA) analysis, the initiating event is classified as a Partial Loss of Main Feedwater (PLMFW) - the isolation of main feedwater to SG C led to decreasing levels in the SG C which resulted in a reactor trip. The PLMFW event is a modeled initiating event, and no risk significant equipment was confirmed out of service.
The STP PRA was used to estimate the relevant metrics for a reactor trip, Conditional Core Damage Probability (CCDP) and Conditional Large Early Release Probability (CLERP), given that the PLMFW initiating event actually occurred. The CCDP and CLERP were determined to be 6.1 E-07 and 3.6E-08 respectively, indicating very low risk significance.
The event was of very low risk significance and no radioactive release occurred; therefore, there was no adverse effect on the health and safety of the public.
IV.
Cause of the event
Prior to the manual reactor trip, SG C Feedwater Regulating Valve closed resulting in lowering water level in SG C due to the random failure of the Manual 7300 Series Tracking Driver circuit card. The Manual NTD card failure forced the Feedwater Regulating Valve closed and prevented further operation of the valve. Operators initiated a manual reactor trip due to lowering SG level and the AFW system actuated automatically on a SG low level signal. There were no human performance errors that contributed to the event.
V.
Corrective actions
The Manual NTD circuit card was replaced. The circuit card was installed in 2009. The failure of the card is considered an infant mortality failure (i.e. < 10 years for 7300 circuit cards) and the first documented failure for this type. The Preventive Maintenance replacement frequency for these NTD circuit cards is 15 years.
A review of all Auto and Manual NTD circuit cards installed in the Feedwater Regulating Valve loops in Unit 1 and Unit 2 indicate they were installed 8 to 11 years ago and all have different sequenced serial numbers which indicates they are not manufactured from the same lot.
VI.
Previous similar events
An Operating Experience review was conducted as part of the cause evaluation performed for this event.
Five other NTD card failures occurred while in service since 1998. All but one failure caused a minor plant transient requiring operator action. Jn 2001, a modification was made to the Feedwater Regulating Valve loops to add dual NTD cards (auto and manual) to increase reliability of this single point vulnerability circuit. In 2004, the loop was modified again to add computer points to monitor the O'" 1 O VDC output signal of both the Auto and Manual NTD cards
- which provides an annunciation to alert the Control Room Operators of degraded/failed conditions. The last failure occurred in 2009 in Unit 2 after both modifications were installed.
The card failure did not cause a plant transient because the Control Room receive.d. an alarm identifying the degraded condition. The 2009 failure occurred after the Manual NTQ card was in service for approximately 1 year.
There were no previous STP Licensee Event Reports submitted related to failure of dual tracker (auto and manual) NTD card.