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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
05000499/LER-1998-004-01, :on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced1999-01-26026 January 1999
- on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced
05000498/LER-1998-010, :on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With1998-11-19019 November 1998
- on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With
05000499/LER-1998-003-01, :on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With1998-11-12012 November 1998
- on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With
05000499/LER-1998-002-01, :on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress1998-10-15015 October 1998
- on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress
ML20237A1201998-08-0505 August 1998 LER 98-S01-00:on 980707,loss of Power Supply to Security Sys Occurred.Caused by Inverter Switching to Alternate Power Source Due to Intermittent Failure of Static Switch Board. Static Switch Board Replaced,Per 10CFR73.71 05000498/LER-1997-013, :on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures1998-04-16016 April 1998
- on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures
05000498/LER-1997-006, :on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases1998-04-0909 April 1998
- on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases
05000498/LER-1998-002, :on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs1998-03-0505 March 1998
- on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs
05000498/LER-1998-001-01, :on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided1998-02-23023 February 1998
- on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided
05000499/LER-1997-007-01, :on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced1997-12-18018 December 1997
- on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced
05000498/LER-1997-013, :on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised1997-12-11011 December 1997
- on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised
05000498/LER-1997-010, :on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment1997-10-16016 October 1997
- on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment
ST-HL-AE-5762, LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel1997-10-0303 October 1997 LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel 05000498/LER-1997-009, :on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves1997-10-0202 October 1997
- on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves
05000498/LER-1997-008, :on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable1997-09-10010 September 1997
- on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable
ST-HL-AE-5721, LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted1997-08-20020 August 1997 LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted 05000498/LER-1997-007, :on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps1997-07-21021 July 1997
- on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps
05000498/LER-1997-006-01, :on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure1997-06-10010 June 1997
- on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure
05000499/LER-1997-006, :on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily1997-05-29029 May 1997
- on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily
05000498/LER-1997-005-01, :on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances1997-05-0101 May 1997
- on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances
05000499/LER-1997-005, :on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances1997-04-24024 April 1997
- on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances
05000499/LER-1997-004-01, :on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced1997-04-17017 April 1997
- on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced
05000498/LER-1997-004, :on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested1997-04-17017 April 1997
- on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested
05000499/LER-1997-002-01, :on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators1997-03-13013 March 1997
- on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators
05000499/LER-1997-001-01, :on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted1997-03-0606 March 1997
- on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted
ST-HL-AE-5591, LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan1997-02-27027 February 1997 LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan 05000498/LER-1997-003, :on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service1997-02-24024 February 1997
- on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service
05000498/LER-1997-001, :on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated1997-02-13013 February 1997
- on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated
05000498/LER-1997-002, :on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested1997-02-13013 February 1997
- on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested
05000498/LER-1996-005, :on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed1997-01-13013 January 1997
- on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed
05000498/LER-1996-004, :on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures1996-12-18018 December 1996
- on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures
05000498/LER-1995-013, :on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised1996-10-0303 October 1996
- on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised
05000499/LER-1996-003, :on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed1996-09-25025 September 1996
- on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed
05000498/LER-1996-009, :on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp1996-07-17017 July 1996
- on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp
05000498/LER-1996-002-01, :on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved1996-06-0606 June 1996
- on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved
05000498/LER-1996-001-01, :on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents1996-06-0303 June 1996
- on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents
05000499/LER-1996-002, :on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue1996-04-24024 April 1996
- on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue
05000499/LER-1996-001, :on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications1996-02-19019 February 1996
- on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications
05000498/LER-1995-012, :on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced1996-01-0909 January 1996
- on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced
1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) 05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With 05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
ML20212C2811999-09-13013 September 1999 Safety Evaluation Supporting Amends 116 & 104 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P9001999-09-0202 September 1999 Safety Evaluation Supporting Amends 115 & 103 to Licenses NPF-76 & NPF-80,respectively ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20211F3651999-08-19019 August 1999 Safety Evaluation Supporting Amends 114 & 102 to Licenses NPF-76 & NPF-80,respectively ML20210K4881999-08-0303 August 1999 Safety Evaluation Supporting Amends 113 & 101 to Licenses NPF-76 & NPF-80,respectively ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 ML20196K7091999-07-0202 July 1999 Safety Evaluation Supporting Amend 100 to License NPF-80 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20212J0031999-06-23023 June 1999 Safety Evaluation Supporting Amends 112 & 99 to Licenses NPF-76 & NPF-80,respectively ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U7731999-05-20020 May 1999 Safety Evaluation Supporting Amends 110 & 97 to Licenses NPF-76 & NPF-80,respectively ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20207A1101999-05-17017 May 1999 Safety Evaluation Supporting Amends 109 & 96 to Licenses NPF-76 & NPF-80,respectively ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with 05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
ML20206A3611999-04-19019 April 1999 Safety Evaluation Supporting Amends 108 & 95 to Licenses NPF-76 & NPF-80,respectively ML20206A1411999-04-19019 April 1999 Safety Evaluation Supporting Amends 107 & 94 to Licenses NPF-76 & NPF-80,respectively ML20205Q6771999-04-16016 April 1999 Safety Evaluation Supporting Amends 105 & 92 to Licenses NPF-76 & NPF-80,respectively ML20205Q7321999-04-16016 April 1999 Safety Evaluation Supporting Amends 106 & 93 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan 1999-09-09
[Table view] |
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The Light c o mp a ny S uth Texas Project Elcctric Generating Station P. O. Box 289 Wadsworth, Texas 77483 Houston Lighting & Power February 7,1994 ST-HL-AE-4692 File No.: G26 10CFR50.73 U. S. Nuclear Regulatory Conunission Attention: Document Control Desk Washington, DC 20555 South Texas Project Unit 1 Docket No. STN 50-498 Licensee Event Report 94-001 Regarding Small Gaps in the Reactor Containment Building Emergency Sumps Screens Pursuant to 10CFR50.73, Houston Lighting & Power submits the attached Unit 1 Licensee Event Report 94-001 regarding small gaps in the Reactor Containment Building (RCB) emergency sumps screens. This event did not have an adverse effect on the health and safety of the public.
If you should have any questions on this matter, please contact Mr. J. M. Pinzon at (512) 972-8027 or me at (512) 972-8787.
IILl J TWC 1
T. H. Cloninger Vice President, Nuclear Engineering JMP/eg Attachment: LER 94-001 (South Texas, Unit 1) 9402180160 940207 PDR ADOCK 05000498 Ig 2.2 S
PDR Project Manager on Behalf of the Participants in the South Texas Project If/
L,94035RO.U1 02/07/94 (6 28pm) 1
9 ST-HL-AE-4692 Houston Lighting & Power Company File'No.:
G26 South Texas Project Electric Generating Station Page 2 4
C:
i 1
I Regional Administrator, Region IV
_Rufus S.
Scott U.
S. Nuclear' Regulatory Commission Associate General Counsel 611 Ryan Plaza Drive, Suite 400 Houston Lighting & Power Company Arlington, TX 76011 P.
O.
Box 61867
)
Houston, TX 77208 l
Lawrence E.
Kokajko Institute of Nuclear Power l
~ Project Manager Operations - Records-Center
- - U.
S. Nuclear Regulatory Commission 700 Galleria Parkway Washington, DC 20555 13H15 Atlanta, GA 30339-5957 David P.
Loveless Dr. Joseph M.
Hendrie Sr. Resident Inspector 50 Bellport Lane l
c/o U.S. Nuclear Regulatory Comm.
Bellport, NY 11713 P.
O.
Box 910 Bay' City, TX 77404-910 J.
R.
Newman, Esquire D.
K.
Lacker Newman & Holtzinger, P.C.,
STE 1000 Bureau of Radiation' Control 1615 L Street, N.W.
Texas Department of Health Washington, DC 20036 1100 West 49th Street Austin, TX 78756-3189 K.
J. Fiedler/M.
T.
Hardt U.
S. Nuclear Regulatory Comm.
City Public Service Attn:
Document Control Desk' P._O.
Box 1771 Washington, D.C.
20555
- - San Antonio,,TX 78296 J. C.-Lanier/M.
B.
Lee
' City of Austin Electric Utility Department 721 Barton Springs Road Austin, TX 78704 G.
E.
Vaughn/T. M.
Puckett
' Central Power and Light Company P.'O.
Box 2121
- - Corpus Christi, TX 78403 f
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South Texas Unit 1 05000 498 1 OF 10 TITLE v4) Small Gaps in the Reactor Containment Building limergency Sumps Screens EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
IA FOUENTIAL REVIS!CN MONTH DAY YEAR SOUTil TEXAS, UNIT 2 05000 499 MONTH CAY YEAP YEAR bW NUMBEP FACILITY hAME DOCKET NUMBER 01 05 94 94 001 --
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NAME TElEPHJhE NUMBEF (include Area Code)
Jairo Pinzon - Senior Engineer (512) 972-8027 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) f E
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On January 5,1994, Unit I was in Mode 5 at 0% power and Unit 2 was defueled while in a refueling outage.
During an inspection of the emergency sumps in the Unit i Reactor Containment Building by the NRC Resident inspectors, openings in the sump screen structures were found that exceeded the designed 1/4" diameter perforations. At each emergency sump screen the frame plate at the floor was warped creating a clearance up to approximately 5/8", and near the solid cover plate at each of the six angle iron supports, cut-out holes approximately 1.5" x 3.5" remained. Some additional gaps, larger than 1/4", were found in the l
area of the screen seams. Similar conditions were identified in Unit 2. The gaps remained from initial construction fabrication, welding and installation of the screen. The apparent cause of this event is the less than adequate attention to detail during the original design, fabrication, and installation, as well as various surveillance inspections subsequent to original construction. A plant change was issued providing the repair disposition and repairs were implemented. Engineering performed an assessment of the deficiencies and concluded there is no safety significance with regard to these deficiencies.
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DESCRIPTION OF EVENT
On January 5,1994, Unit I was ic Mode 5 at 0% power and Unit 2 was defueled while in a refueling outage. During an inspection of the emergency sumps in the Unit 1 Reactor Containment Building (RCB) by the NRC Resident Inspectors, openings in the sump screens were found that exceeded the designed 1/4" perforations. At each emergency sump screen the frame plate at the floor was warped providing a clearance up to approximately 5/8", and near the solid cover plate at each of the six angle iron supports, cut-out holes of approximately 1.5" x 3.5" remained. Engineering and maintenance personnel investigated j
the extent of the gaps and proposed a resolution. Some additional gaps, larger than 1/4", were found in the area of the screen seams. These gaps remained from initial fabrication, welding and installation of the j
screen. A plant change was issued providing the repair disposition and repairs were implemented. Similar i
deficiencies were identiGed for Unit 2.
On Januaiy 6. IW4 the NRC was notified that this event was reportable.
As a result of the investigation of the sump screen deficiencies, on January 20,1994, the NRC was also j
notified that the surveillance procedure for the containment sump inspection was inadequate to fully meet the requirements for Technical Specification 4.5.2.d in that it did not require the inspector to physically enter the sump to search for debris. The surveillance was last determined to be performed adequately on March 22,1991. In August 1993, Unit I entered Mode 3 without an adequate surveillance to ensure compliance with Technical Specification 4.5.2.d. This constituted a period of approximately 29 months since the last adequate performance of the containment sump surveillance and entry into Mode 3. This is beyond the 18 months (plus grace period) allowed by Technical SpeciGeations. Therefore, Unit 1 entry j
into Mode 3 in August 1993, constituted an operation prohibited by Technical Specification 3.5.2.
CAUSE OF EVENT
The apparent cause of the screen deficiencies is the less than adequate attention to detail during original construction design, fabrication, installation.
The design drawing should have included an additional note limiting the size of fit-up gaps to less than normal installation tolerances.
- The fabricator, installer and t,aality control acceptance should have questioned the cutouts in the screen around the angle iron frames in addition to the other gaps / holes following initial installation.
There have been several NRC communications issued to the industry addressing sump screen blockage and debris intrusion into pump suctions. Most of this correspondence, with the exception of information Notice (IN) 89-77, addressed types of debris and their effect on sump suction blockage. IN 89-77 addressed both debris and inadequate sump screens. The South Texas Project Electric Generating Station 7 9ew m 02/07/94 (6:2% W
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South Texas, Unit 1 05000 498 3 OF 10 94-
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CAUSE OF EVENT
(Cont'd) review of this IN was focused primarily on cleanliness and removal of debris present in the Reactor Containment Building and did not consider sump screen integrity.
Subsequent surveillance inspections did not identify the screen deficiencies since the surveillance procedure did not have guidance to prompt plant personnel to identify holes and gaps during the various surveillance inspections of the emergency sump.
The cause of the inadequate surveillance was the lack of detailed inspection instructions. Regulatory Guide 1.82 does not provide specific inspection criteria. The cause for the operation prohibited by Technical Specifications was as a result of the inadequate surveillance procedure.
ANALYSIS OF EVENT
The small gaps in the Unit I and Unit 2 sump screens created the potential for injected debris to compromise the ability of the containment spray and injection systems to perform their design functions.
Therefore this event is considered to be reportable pursuant to 10CFR50.73(a)(2)(ii)(B) as a condition outside the design basis of the plant and 10CFR50.73(a)(2)(v) as a condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident for Unit I and Unit 2. The inadequate surveillance procedure is reportable i
for both Units pursuant to 10CFR50.73(a)(2)(i)(B) as an operation prohibited by Technical Specification.
The surveillance procedure was inadequate to meet the requirements of Technical Specification 4.5.2.d. In addition, Unit 1 operated in Mode 3 without a surveillance being adequately performed within the time limits established by the Technical Specifications.
The following provides the safety analysis of this event:
- 1. GENERATION OF DEBRIS Debris generated from the jet impingement of a loss of coolant accident (LOCA) is the most likely source of material that could bypass the sump screens via the identified deficiencies. RCB walkdowns, in accordance with OPSP03-XC-0002, provide reasonable assurance that the Containment is clean and free of other foreign material which could migrate to the emergency sumps.
Insulation has traditionally ten considered one of the major contributors to post-LOCA debris. Mirror and NUKON insulation ari utilized predominantly in the RCBs at STP. Topical Report i
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I SEQUDTTIAL REVISION gp South Texas, Unit 1 05000 498 4 OF 10 94
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ANALYSIS OF EVENT
(Cont'd)
OCF-1 concludes that NUKON will not deteriorate or lose its mechanical integrity in a post-LOCA environment. Similarly, mirror insulation, if dislodged in a LOCA, would settle in relatively large pieces and would not be a factor adverse to emergency core cooling system (ECCS) recirculation.
- 2. TRANSPORTATION OF DEBRIS The six 1.5" x 3.5" holes near the top of the structure do not significantly degrade the integrity of the screen because of the arrangement of the screen design and the normal flow configuration. A 4" x 4" structural angle on the outer edge of the screen structure directs the normal Dow path below the 1.5" x 3.5" openings and entrained matter is caught on the 1/4" perforated screen as intended. See Figure 1.
The potential impact of the remaining holes and gaps is twofold. The 5/8" and 3/8" gaps and holes provide potential paths for an increase in particulate size over the 1/4" design criteria and increase the total available flow area through which suspended particulate matter may pass.
l From the aspect of increased particulate size, there is little impact because of low design Gow velocities.
The approach velocity at the first screen is 0.12 ft/sec, which is well below the recommended design velocity of 0.2 ft/sec in Regulatory Guide (RG) 1.82. Since the flow upstream of the screens would be less than or equal to 0.12 ft/see, particulate matter with a speciOc gravity of 1.05 or greater would settle j
out on the containment Door and would not migrate to the screens.
]
1 From the aspect of an increase in total now area, the gaps and holes have been conservatively estimated i
to represent a total maximum increase of 1.36% in the current available sump screen Dow area. This 1
increase is considered insignificant compared with the total flow area.
Due to the low flow velocities, the concentrated area of potential debris that would be available for i
ingestion to the sump is extremely small. Given the location and geometry of the emergency sumps, it is highly unlikely that remote debris would propagate to the emergency sumps. With the exception of the aforementioned deficiencies, the emergency sumps meet the intent of the RG 1.82.
- 3. IMPACT ON EMERGENCY CORE COOLING AND CONTAINMENT SPRAY SYSTEM (ECCS &
CS) PUMPS The ECCS & CS pump design and fabrication requirements specifically address pump operation during recirculation of Containment sump water. The pump manufacturer was required to allow cm m w m mw.,
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SEQUENTIAL REVISION YMR South Texas, Unit 1 05000 498 5 OF 10 94
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ANALYSIS OF EVENT
(Cont'd) for sump water to contain solid particles of concrete, insulation and paint flakes which could pass through the screen and into the suction of the pumps. This was satisfactorily demonstrated by a thermal transient test with injection of suspended particles (less than 1/4 inch). The pump performance variation between pre and post transient test was minimal and well within specifications. The head curve deviated less than 1% between tests and vibration levels were unchanged. Additionally, the seal area showed no sign of leakage before, during, or after the transient. Any entrained particle must enter the outer barrel and make a 180" flow direction change prior to entering the first stage impeller. A dense particle (unlikely to be transported to the screen or migrate from the sump) would be forced against the bottom of the outer barrel. Light objects would enter the first stage impeller and pass through the pump.
i Although transport of debris in excess of design is unlikely, the suspended particle pump performance tests and inherent geometry substantiate that there would be no adverse impact on the ability of the ECCS and CS pumps to perform their design functions.
- 4. NO SIGNIFICANT 11AZARDS (CONTAINMENT HEAT REMOVAL, RADIOLOGICAL OR CORE COOLING)
(i)
CONTAINMENT HEAT REMOVAL One of the functions of the Containment Spray System (CSS) is heat removal from Containment following a design basis accident (DBA). Per UFSAR Section 6.2.1, the Containment DBA is a double-ended pump suction guillotine rupture (LOCA 2). The energy inventory for this accident is depicted in Figure 2 (UFSAR Fig. 6.2.1.1-1 A) and the Containment vapor and sump temperatures for this accident are depicted in Figure 3 (FSAR Fig. 6.2.1.1-1 1 ).
At the assumed time of initiation of recirculation with suction from the Containment sumps (1216 seconds), the Containment sump temperature is significantly higher than Containment vapor temperature and heat removal by Containment spray begins to decrease (and is essentially zero at 8000 sec) as shown in Figure 2.
.1 i
A loss of Containment spray capability by total blockage of the spray header nozzles at the initiation of recirculation flow will not have a negative impact on energy removal capability following a DBA and is, therefore, not a safety concern.
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SEQUENTIAL REVISICN YEAR South Texas, Unit 1 05000 498 6 OF 10 94
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ANALYSIS OF EVENT
(Cont'd)
(ii) RADIOLOGICAL in addition to reducing the pressure and temperature in ti,e Containment following a postulated LOCA, the CSS also provides a mechanism to scrub iodine from the Containment atmosphere.
The recirculation phase of the LOCA begins after approximately 20 minutes. It is at this time that any degradation of the CSS due to loss of sump screen integrity might begin to potentially impact the design basis dose calculation.
An examination of the dose calculations performed for the LOCA reveals that spray removal of elemental iodine ends at 16.8 minutes after the accident. Spray removal of particulate iodine ends at 6.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The sprays are not assumed to remove organic iodine from the Containment atmosphere. Therefore, the impact of potentially reduced CSS flow would be limited to a decrease in the removal rate for particulate iodine. Since approximately 42% of the offsite thyroid dose is due to elemental iodine and 54% due to organic iodine, the impact of reduced CSS flow on the offsite doses is small.
Calculation NE-CE-94-01-00 indicates that a reduction of two-train CSS flow (during the recirculation phase) of up to 75% may be tolerated without exceeding 10CFR100 limits. In the bounding hypothetical case considering the two train CSS flow reduced to zero, the offsite dose would only increase by approximately 15%. The control room and Technical Support Center (TSC) thyroid doses would increase by only 11%. The offsite and control room doses would not exceed 10CFR100 dose limits. Additionally, the thyroid dose to TSC personnel would exceed 10CFR100 limit of 30 rem by only approximately 3 rem.
(iii) CORE COOLING The amdysis of a large break LOCA is divided into three phases; blowdown, refill and reflood.
Blowdown is the time between full power operation until zero break flow is first calculated; refill is from the end of blowdown to the time the ECCS fills the vessel lower plenum; and reflood begins when water starts moving into the core and continues until the end of the transient.
Depending on the specific accident assumptions, the core reflood ends at 100 to 280 seconds (UFSAR Table 6.2.1.1 - 10). At this time, the transient has ended and long term core cooling has been established. Continued operation of the ECCS pumps supplies water during long-term i
cooling. Core temperatures have been reduced to long-term steady-state levels associated with dissipation of residual heat generation. The recirculation phase of a LOCA begins at approximately 20 minutes (1200 seconds) after the accident. After the water level l
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NRC FCRM 366A U.S. NUCLEAR REGULATORY COMMISSIODi' LPPROVED BY OMR NO. 3150 0100 EXPIRES 5/31/95 (5-92) -
ESTIMATED BURDEN PEN RESPONSE TO COMPLY WITH THIS
+
LICENSEE EVENT REPORT (LER) ccxor"SwN
TEXT CONTINUATION 5$$$arcYi,s.ne pgggARooot7a;gmy Tnpyggg UniU4% MW WWA& nr %"i?
FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (5)
PAGE (3)
SEQUENTIAL FEVISION yg South Texas, Unit 1 05000 498 7 OF 10 94
-- 001 --
00 TEXT ITf more space le ro Tr i rsu:I u w +11ttfonal revien of hRr Form 1 MAS (11)
ANALYSIS OF EVENT
(Cont'd) of the RWST reaches a minimum allowable value, coolant for long-term cooling of the core is obtained by automatically switching to the cold leg recirculation phase of operation in which spilled borated water is drawn from the Containment emergency sumps by the low-head and high-head safety injection pumps and returned to the RCS cold legs. The main objective of the ECCS now is to keep the core covered. The recirculation phase of a LOCA begins when the ECCS suction is switched from the RWST to the containment sumps. The identified sump screen defects would not prevent the low-head l
and high-head safety injection from performing the long-term cooling functions, i.e.,the core would I
remain flooded.
(5) CONCI.USION The low flow velocities and design conservatism would inhibit the propagation of debris to the emergency sumps and preclude debris from entering into the ECCS/CS suction piping.
(
In the highly unlikely event of a 75% loss of the two-train CSS design flow due to blockage, there are no negative consequences to containment pressure / temperature mitigation or core cooling and only minimal impact on the available design margin for control room, TSC, and offsite doses.
Therefore, the gaps found in the Unit I and Unit 2 cmergency sumps have no adverse effect on the operation of the plant.
I
CORRECTIVE ACTIONS
The followinf., corrective actions have been or will be taken as a result of ibis event:
1 1.
Repair dispositions were initiated to correct the noted deficiencies in the ECCS sump as well as the design drawings. The repairs on Unit I are complete and the Unit 2 repairs will be completed prior to entry into Mode 4 from the current refueling outage.
2.
The emergency sump inspection surveillance procedure has been corrected to require sump entry and has been enhanced to include quantitative inspection criteria for gaps and holes in the screen structure.
ADDITIONAL INFORM ATION Unit i LER 88-063 was previously submitted regarding the failure to install vortex breakers in the containment emergency sumps. The cause of this event was the failure to clearly establish responsibility and accountability for the installation of the vortex breakers during initial installation.
02/07/94 (6 2a,m)
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NRC FOPM 386A U.S.
NUCLEAR REGULATORY COMMISSION APPROVED BY ON3 Ho. 3150-0104 EXPIRES 5/31/95 (5-92)
ESTIMATED BURDEN FER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION R EQUE.sT:
50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE LICENSEE EVENT REPORT (LER)
INFORMATION AND RECCRDS MANAGEMENT BRANCH (MNBB 7714),
U.S.
NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION wASnINGTON, De 20sss-ooot, AND TO TuE PAeERwCRx REDUCTION PROJECT (3150-0104).
OFFICE OF MANAGEMENT AND BUDr,FT. WASHINGTON, DC 20503, FACILITY NAME (1)
W KET NUMBER (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVISION ypg NUMBER NUMBCR South Texas, Unit 1 05000 498 8 OF 10 94
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EXPIRES 5/31/95 j
+
ESTIMATED tlURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS.
i FOHWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE LIC$NSEE EVENT REPORT (LER)
INFORMATION AND RECORDS MANAGEMENT URANCH (MNBB 7714),
U.S.
NUCLEAR REGULATORY COMMIGSION, TEXT CONTINUATION WASHINGTON, DC 20$55-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104),
OFFICE OF I
MANAGEMENT AND PJ1DGET. WA9HINGTON, DC 20501.
FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER f6)
PAGE (3)
SEQUENTIAL REVISION R
NUMBER NUMBER South Texas, Unit 1 05000 498 9 OF.10 94
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50.0 HRS.
l FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE
~ LIddNSEE EVENT REPORT (LER)
INFORMATION AMD RECORDS MANAGEMENT BRANCH (MNBB TEXT CONTINUATION EN!sGTo"N',"be ES5^5001"*EN5' THE' ElIEU8"A REDUCTION PROJECT (3150-0104),
OFFICE OF MANAGEMENT AND PUDGET, WASHINGTON, DC 2050).
FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3) b IOIC YEAR N'JMBER NUMBER South Texas, Unit 1 05000 498 10 OF 10 94
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05000499/LER-1994-001-01, :on 940301,SDG 21 Experienced Inadvertent Start.Caused by Weakened Transistor in non-1E Fiber Optic Start Circuits & Faulty Power Supply (PS-2).Fiber Optic Boards G,C & J & PS-2 Power Supply Replaced |
- on 940301,SDG 21 Experienced Inadvertent Start.Caused by Weakened Transistor in non-1E Fiber Optic Start Circuits & Faulty Power Supply (PS-2).Fiber Optic Boards G,C & J & PS-2 Power Supply Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1994-001, :on 940105,discovered Small Gaps in Reactor Containment Bldg Emergency Sumps Screens.Caused by Less than Adequate Attention to Detail.Repair Dispositions Initiated to Correct Noted Deficiencies in Sump |
- on 940105,discovered Small Gaps in Reactor Containment Bldg Emergency Sumps Screens.Caused by Less than Adequate Attention to Detail.Repair Dispositions Initiated to Correct Noted Deficiencies in Sump
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000498/LER-1994-002, :on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution Statements |
- on 940115,centrifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to Requirements of TS 3.1.2.3.Caused by hydro-pneumatic Transient.Valves Labeled W/Caution Statements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1994-002-02, :on 940302,Piston 4R Was Discovered Damaged During Insp Due to Piston Failure Foreign Material or Trapped Wear Particles Between Piston & Liner.Piston & Cylinder Liner for Cylinder 4R Were Replaced |
- on 940302,Piston 4R Was Discovered Damaged During Insp Due to Piston Failure Foreign Material or Trapped Wear Particles Between Piston & Liner.Piston & Cylinder Liner for Cylinder 4R Were Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1994-002-01, :on 940115,centifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to TS 3.1.2.3 Requirements.Caused by hydro-pneumatic Transient. MOV Database Searched |
- on 940115,centifugal Charging Pump 1A Discharge Bypass Valve Found in Open Position Contrary to TS 3.1.2.3 Requirements.Caused by hydro-pneumatic Transient. MOV Database Searched
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1994-003-01, :on 940429,inadvertent Test Mode Start of Standby DG 21 & 22 Occurred Due to fiber-optic Board Susceptibility to Noise in Conjunction W/Transient DC Spikes.Maint for Boards Initiated |
- on 940429,inadvertent Test Mode Start of Standby DG 21 & 22 Occurred Due to fiber-optic Board Susceptibility to Noise in Conjunction W/Transient DC Spikes.Maint for Boards Initiated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1994-004, :on 940119,determined Surveillance Performed to Comply W/Sr 4.4.4.1.b for Rvs Needed to Be Enhanced Because PORVs Not Tested from Mcb.Procedure 1(2)PSP03-RC-0010 Replaced w/OPSP03-RC-0010 |
- on 940119,determined Surveillance Performed to Comply W/Sr 4.4.4.1.b for Rvs Needed to Be Enhanced Because PORVs Not Tested from Mcb.Procedure 1(2)PSP03-RC-0010 Replaced w/OPSP03-RC-0010
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1994-004-01, :on 940512,SG hi-hi Level (P-14) Signal Generated While Performing RTD Cross Calibrs Due to Filling SG to Approx 90% Full.Crew Briefings Discussing Event Conducted |
- on 940512,SG hi-hi Level (P-14) Signal Generated While Performing RTD Cross Calibrs Due to Filling SG to Approx 90% Full.Crew Briefings Discussing Event Conducted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) | 05000499/LER-1994-005, :on 940607,standby DG 22 Received an Unexpected test-mode Start Signal.Caused by Voltage Spike Generated by an Emergency Fuel Oil Solenoid Deenergizing.Noise Suppression Devices Installed |
- on 940607,standby DG 22 Received an Unexpected test-mode Start Signal.Caused by Voltage Spike Generated by an Emergency Fuel Oil Solenoid Deenergizing.Noise Suppression Devices Installed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(s)(2) | 05000499/LER-1994-005-02, :on 940607,standby Diesel Generator 22 Had Received Unexpected Test Mode Start Signal.Caused by Voltage Spike Generated by Emergency Fuel Oil Solenoid Deenergizing. Replaced Parts Found to Be Weak |
- on 940607,standby Diesel Generator 22 Had Received Unexpected Test Mode Start Signal.Caused by Voltage Spike Generated by Emergency Fuel Oil Solenoid Deenergizing. Replaced Parts Found to Be Weak
| | 05000498/LER-1994-005, :on 940201,determined Control Room make-up & Fuel Handling Building Exhaust Dampers Inoperable Due to Depleted Lithium Battery back-up Power Supplies.Performed Evaluation on Control Room HVAC Sys |
- on 940201,determined Control Room make-up & Fuel Handling Building Exhaust Dampers Inoperable Due to Depleted Lithium Battery back-up Power Supplies.Performed Evaluation on Control Room HVAC Sys
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000499/LER-1994-006-01, :on 940711,discovered That Sp Used to Verify Operability of Accident Monitoring Instrumentation & Remote Shutdown Monitoring Instrumentation Inadequate.Sp Revised.W/ |
- on 940711,discovered That Sp Used to Verify Operability of Accident Monitoring Instrumentation & Remote Shutdown Monitoring Instrumentation Inadequate.Sp Revised.W/
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000498/LER-1994-006, :on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design Configuration |
- on 940214,reactor Manually Tripped Following Unanticipated Test Results.Caused by Mod Which Failed post- Mod Test.Test Terminated & Solid State Rod Control Sys Returned to Original Design Configuration
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1994-007, :on 940224,Reactor Trip Bypass Breaker Did Not Properly Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program & Basis Document Developed |
- on 940224,Reactor Trip Bypass Breaker Did Not Properly Satisfy Ts.Caused by Inadequate Procedure Preparation & Review.Surveillance Procedure Enhancement Program & Basis Document Developed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1994-007-02, :on 940625,main Transformer Lockout Relay Actuated.Caused by Failure of Capacitor within Pilot Wire Relay.Annunciator Response Procedures Have Been Revised & Faulty Pilot Wire Relay Was Replaced |
- on 940625,main Transformer Lockout Relay Actuated.Caused by Failure of Capacitor within Pilot Wire Relay.Annunciator Response Procedures Have Been Revised & Faulty Pilot Wire Relay Was Replaced
| | 05000498/LER-1994-008, :on 940224,reactor Trip Breaker Surveillance Not Performed within TS Staggered Test Interval.Caused by Inadequate Methods & Training.Training Conducted for Responsible Surveillance Coordinators |
- on 940224,reactor Trip Breaker Surveillance Not Performed within TS Staggered Test Interval.Caused by Inadequate Methods & Training.Training Conducted for Responsible Surveillance Coordinators
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(e)(2)(x) 10 CFR 50.73(e)(2) | 05000498/LER-1994-009, :on 940228,manual Reactor Trip Occurred Due to Malfunctioning Main Feedwater Regulating Valve.Caused by Failed Transformer Coil in Torque Motor to Pneumatic Converter.Converter Replaced |
- on 940228,manual Reactor Trip Occurred Due to Malfunctioning Main Feedwater Regulating Valve.Caused by Failed Transformer Coil in Torque Motor to Pneumatic Converter.Converter Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(e)(2)(iii) | 05000498/LER-1994-010, :on 940719,Unit 1 Failed to Fully Meet Surveillance Requirements of TS 4.7.4, Essential Cooling Water Sys. Caused by Misuse of Equipment Procedures. Revised Procedure Was re-performed for Unit 1 |
- on 940719,Unit 1 Failed to Fully Meet Surveillance Requirements of TS 4.7.4, Essential Cooling Water Sys. Caused by Misuse of Equipment Procedures. Revised Procedure Was re-performed for Unit 1
| | 05000498/LER-1994-011, :on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from Watchbill |
- on 940310,safety Injection Actuation Was Received on Trains A,B & C.Cause Was Failure to Adhere to Procedure.Corrective Actions:Restored Cooling Shutdown & Removed Personnel from Watchbill
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1994-012, :on 940311,failure to Meet TS Requirements Occurred Due to Standby Diesel Generator 11 Technically Inoperable as Result of Intermittent Failure of K1 Contactor for Voltage Regulator/Field Flash Circuit |
- on 940311,failure to Meet TS Requirements Occurred Due to Standby Diesel Generator 11 Technically Inoperable as Result of Intermittent Failure of K1 Contactor for Voltage Regulator/Field Flash Circuit
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1994-013, :on 940804,identified Two Cases of NUMARC 87-00 Criterion Not Being Satisfied.Caused by Failure to Confirm Validity of Blackout Program.Severe Weather Guidelines Revised |
- on 940804,identified Two Cases of NUMARC 87-00 Criterion Not Being Satisfied.Caused by Failure to Confirm Validity of Blackout Program.Severe Weather Guidelines Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | 05000498/LER-1994-014, :on 940810,determined That Sdg Starting Air Receiver Inlet Check Valves Not Being Surveillance Tested Due to Inadequate Review of Function of Subj Valves When IST Initially Developed.Affected Valves Tested |
- on 940810,determined That Sdg Starting Air Receiver Inlet Check Valves Not Being Surveillance Tested Due to Inadequate Review of Function of Subj Valves When IST Initially Developed.Affected Valves Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1994-015, :on 940920,unit 1 Experienced Reactor Trip on low-low Steam Generator Level for Approx Four Minutes After Loss of Steam Generator Feedwater Pump.Caused by Expected Response Instead of Actual Conditions |
- on 940920,unit 1 Experienced Reactor Trip on low-low Steam Generator Level for Approx Four Minutes After Loss of Steam Generator Feedwater Pump.Caused by Expected Response Instead of Actual Conditions
| | 05000498/LER-1994-016, :on 940923,failure to Fully Meet Requirements of TS Due to Not Placing CR Envelope HVAC Sys in Required Mode.Toxic Gas Analyzers Repaired & Mod Implemented |
- on 940923,failure to Fully Meet Requirements of TS Due to Not Placing CR Envelope HVAC Sys in Required Mode.Toxic Gas Analyzers Repaired & Mod Implemented
| | 05000498/LER-1994-017, :on 941011,gaseous Effluent Monitor Setpoints Had Not Been Calculated in Accordance W/Offsite Dose Calculation Methodology.Caused by Failure to Revise Related Change Documents.Monitors Verified Operable |
- on 941011,gaseous Effluent Monitor Setpoints Had Not Been Calculated in Accordance W/Offsite Dose Calculation Methodology.Caused by Failure to Revise Related Change Documents.Monitors Verified Operable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1994-018-01, :on 941102,failure to Fully Meet Requirements of TS Re CR Envelope HVAC Sys Boundary.Caused by Less than Adequate Surveillance Test Procedure.Development of Detailed Testing Method Initiated |
- on 941102,failure to Fully Meet Requirements of TS Re CR Envelope HVAC Sys Boundary.Caused by Less than Adequate Surveillance Test Procedure.Development of Detailed Testing Method Initiated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000498/LER-1994-018, :on 941102,required 0.125 Inches Water Gauge Could Not Be Demonstrated on Trains of CR Envelope HVAC Due to Less than Adequate Surveillance Test Procedure.Electrical Auxiliary Bldg HVAC Airflows Adjusted |
- on 941102,required 0.125 Inches Water Gauge Could Not Be Demonstrated on Trains of CR Envelope HVAC Due to Less than Adequate Surveillance Test Procedure.Electrical Auxiliary Bldg HVAC Airflows Adjusted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1994-019, :on 941109,failure to Fully Meet Requirement of TS for Response Testing of Reactor Containment Fan Cooler,Cr Envelope & Fuel Handling Bldg HVAC Sys.Caused by Inadequate Preparation,Review & Rev |
- on 941109,failure to Fully Meet Requirement of TS for Response Testing of Reactor Containment Fan Cooler,Cr Envelope & Fuel Handling Bldg HVAC Sys.Caused by Inadequate Preparation,Review & Rev
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000498/LER-1994-020, :on 941209,determination Made That Combined Total of 66 Breakers Potentially Out of Tolerance.Caused by Misinterpretation of Acceptance Criteria.Molded Case Circuit Breaker Tests Procedure Revised |
- on 941209,determination Made That Combined Total of 66 Breakers Potentially Out of Tolerance.Caused by Misinterpretation of Acceptance Criteria.Molded Case Circuit Breaker Tests Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) |
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