05000445/FIN-2015003-01
From kanterella
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Failure to Take Appropriate Maintenance Rule Corrective Actions for the Instrument Air System |
Description | The inspectors identified a non-cited violation of 10 CFR Part 50.65(a)(1) for the failure to take appropriate corrective actions for a system that did not meet established goals. Specifically, the Unit 1 instrument air system had been in maintenance rule (a)(1) status since 2011 due to dryer component failures. In 2014, the instrument air system experienced additional failures that resulted in water accumulating in air operated valve actuators on Unit 1. The water intrusion resulted in abnormal operation of the air operated valves in the Unit 1 main feedwater system. These failures were determined to be due to inadequate maintenance on the instrument air dryers unrelated to the 2011 failures. However, the licensee failed to revise their corrective actions to address the causes of the water intrusion. The licensee entered these issues into corrective action program as Condition Report CR-2015-009077. The licensees failure to take appropriate corrective actions for a system that did not meet established goals was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it affected the equipment performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the failure to take appropriate corrective actions adversely affected the reliability of a system scoped in the plants maintenance rule program. Using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, and Appendix A, The Significance Determination Process (SDP) for Findings AtPower, Exhibit 1, Initiating Events Screening Questions, dated June 19, 2012, the finding was determined to be of very low safety significance (Green) because the finding affected a support system initiator but did not involve the loss of a support system that contributed to the likelihood of an initiating event and affected mitigation equipment. The finding has a problem identification and resolution cross-cutting aspect associated with evaluation, in that, the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes. Specifically, the licensee performed an inadequate cause evaluation and failed to identify the cause of the water intrusion [P.2]. |
Site: | Comanche Peak |
---|---|
Report | IR 05000445/2015003 Section 1R12 |
Date counted | Sep 30, 2015 (2015Q3) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.12 |
Inspectors (proximate) | J Drake J Groom J Josey J Reynoso R Kumana |
Violation of: | 10 CFR 50.65(a)(1) 10 CFR 50.65 |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
' | |
Finding - Comanche Peak - IR 05000445/2015003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Comanche Peak) @ 2015Q3
Self-Identified List (Comanche Peak)
| ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||