05000410/LER-2013-001, Regarding Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure

From kanterella
(Redirected from 05000410/LER-2013-001)
Jump to navigation Jump to search

Regarding Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure
ML13091A370
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 03/25/2013
From: Philippon M
Constellation Energy Group, EDF Group, Nine Mile Point
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 13-001-00
Download: ML13091A370 (8)


LER-2013-001, Regarding Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
4102013001R00 - NRC Website

text

Michel A. Philippon P.O. Box 63 Plant General Manager Lycoming, New York 13093 315.349.5205 315.349.1321 Fax CENG.

a joint venture of 0

Constellation EnerwgeD NINE MILE POINT NUCLEAR STATION March 25, 2013 U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 ATTENTION:

Document Control Desk

SUBJECT:

Nine Mile Point Nuclear Station Unit No. 2; Docket No. 50-410 Licensee Event Report 2013-001, Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure In accordance with 10 CFR 50.73, please find attached Licensee Event Report 2013-001, Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure.

There are no regulatory commitments in this submittal.

Should you have questions regarding the information in this submittal, please contact John J. Dosa, Director-Licensing, at (315) 349-5219.

Very truly yours, MAP/BTV

Attachment:

Licensee Event Report 2013-001, Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure cc:

NRC Project Manager NRC Resident Inspector NRC Regional Administrator

ATTACHMENT LICENSEE EVENT REPORT 2013-001 REACTOR CORE ISOLATION COOLING SYSTEM ISOLATION DUE TO A TEMPERATURE SWITCH UNIT FAILURE Nine Mile Point Nuclear Station, LLC March 25, 2013

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010)

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Nine Mile Point Unit 2 05000410 1 of 6
4. TITLE Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED 1FACILIT NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH DAY YEAR NUMBER NO.I tFACILITY NAME DOCKET NUMBER 01 23 2013 2013 001 0

03 25 2013

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

[o 20.2201(b)

[I 20.2203(a)(3)(i)

El 50.73(a)(2)(i)(C)

[I 50.73(a)(2)(vii)

El 20.2201(d)

[I 20.2203(a)(3)(ii)

El 50.73(a)(2)(ii)(A)

El 50.73(a)(2)(viii)(A)

[I 20.2203(a)(1)

El 20.2203(a)(4)

[I 50.73(a)(2)(ii)(B)

El 50.73(a)(2)(viii)(B)

10. POWER LEVEL E] 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

El 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

El 20.2203(a)(2)(ii)

El 50.36(c)(1)(ii)(A)

Z 50.73(a)(2)(iv)(A)

El 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

[I 50.36(c)(2)

ED 50.73(a)(2)(v)(A)

El 73.71(a)(4) 100 El 20.2203(a)(2)(iv)

El 50.46(a)(3)(ii)

[I 50.73(a)(2)(v)(B)

El 73.71(a)(5)

El 20.2203(a)(2)(v)

El 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

El OTHER El 20.2203(a)(2)(vi)

El 50.73(a)(2)(i)(B) 0 50.73(a)(2)(v)(D)

Specify in Abstract below or in

D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES

January 23, 2013 15:16 Operators received a high temperature alarm for reactor building general area temperature.

An isolation signal is generated by 2RHS*TS85A and sent to Group 5 and 10 isolation valves.

RCIC system is declared inoperable. TS 3.5.3 Conditions A and B and TS 3.5.1 Conditions B and D are entered for RCIC and IHPCS inoperable.

2RHS*TS85A is declared inoperable. TS 3.3.6.1 Condition A is entered for 2RHS*TS85A inoperable.

15:50 HPCS system is declared operable following completion of surveillance testing and filling and venting of the system. TS 3.5.1 Conditions B and D are exited. TS 3.5.3 Condition B is exited.

23:04 Replacement of 2RHS*TS85A is complete.

23:59 2RHS*TS85A is declared operable. TS 3.3.6.1 Condition A is exited.

January 24, 2013 01:17 RCIC system is declared operable after reopening the steam supply isolation valve. TS 3.5.3 Condition A is exited.

E. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED

No other systems or functions were affected.

F. METHOD OF DISCOVERY

On January 23, 2013 at 15:16, Operators received a high temperature alarm for reactor building general area temperature.

G. MAJOR OPERATOR ACTION:

RCIC system was declared inoperable.

TS 3.5.3 Conditions A and B were entered for RCIC and HPCS systems inoperable.

TS 3.5.1 Conditions B and D were entered for RCIC and HPCS systems inoperable.

2RHS*TS85A was declared inoperable.

TS 3.3.6.1 was entered for 2RHS*TS85A inoperable.

H. SAFETY SYSTEM RESPONSES:

No operational conditions requiring the response of safety systems occurred as a result of this event.

II. CAUSE OF THE EVENT

The cause of the temperature switch unit failure was age-related capacitor degradation. The apparent cause of the event is insufficient use of the corrective action program to fully implement a periodic capacitor replacement program for the Riley temperature switches.

Condition reports written in 1997 and 2002 were initiated in response to temperature switch failures and calibration drift respectively. As part of the corrective actions for these CRs, the capacitors were replaced. In 2002, Preventative Maintenance Change Requests (PMCRs) were developed to periodically replace the capacitors in the Riley temperature switches; however, these PM tasks were never implemented, and subsequent capacitor replacements were not performed.

This event was entered into the Nine Mile Point Nuclear Station, LLC (NMPNS) corrective action program as condition report CR-2013-00634.

III. ANALYSIS OF THE EVENT

This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an automatic actuation of containment isolation valves in more than one system. Containment isolation valves in the RCIC and RHR systems received an isolation signal as a result of the temperature switch unit failure. The event is also reportable in accordance with 10 CFR 50.73(a)(2)(v), as an event that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition, and (D) Mitigate the consequences of an accident.

There were no actual safety consequences from this event. The event was caused by the failure of temperature switch unit 2RHS*TS85A, resulting in the generation of an isolation signal which was sent to containment isolation valves in the Reactor Core Isolation Cooling (RCIC) system (Group 10) and the Residual Heat Removal (RHR) system (Group 5). This caused the RCIC system to isolate from the reactor vessel. The Group 5 containment isolation valves were already closed, which is their normal position during power operation. The isolation signal was generated due to the failure of the temperature trip unit. Operators verified the temperature indicated by the thermocouple was below the trip setpoint, and the isolation signal was determined to be invalid.

The failure of the temperature switch unit occurred concurrently with the HPCS system inoperable for planned surveillance testing. When the steam supply isolation valve to the RCIC turbine (21CS*MOV121) closed due to the temperature switch failure, the RCIC system became inoperable. With both the RCIC and HPCS systems inoperable, high pressure makeup capability to the reactor core was lost.

The HPCS system is an Emergency Core Cooling System (ECCS) designed to pump water into the reactor vessel over a wide range of pressures. For a small break Loss of Coolant Accident (LOCA) that does not result in rapid reactor depressurization, the system maintains reactor water level and coolant inventory. For large breaks, the HPCS system cools the core by a spray. The RCIC system is not part of the ECCS. It is designed to assure that sufficient reactor water inventory is maintained in the reactor vessel to permit adequate core cooling in the event that the reactor is isolated from the main condenser. The RCIC system, like the HPCS system, can operate over a large pressure range (165 - 1215 psia). During an accident with the RPV at high pressure, either the HPCS system or the RCIC system can be used to provide makeup flow to the reactor. If the HPCS system was to fail, and RCIC capacity is insufficient to maintain reactor vessel level, the Automatic Depressurization System (ADS) automatically initiates depressurization of the reactor to permit low-pressure ECCS to provide

makeup coolant. When the low-pressure ECCS operates in conjunction with the ADS, the effective core cooling capability of the low-pressure ECCS is extended to all break sizes. The low-pressure ECCS consists of the Low-Pressure Core Spray (LPCS) system and the Low-Pressure Coolant Injection (LPCI) system.

The ADS and both the LPCS and the LPCI systems were operable during the event. Based on the above considerations, it has been concluded that the safety significance of this event is low, and the event did not pose a threat to the health and safety of the public or plant personnel.

This event affects the NRC Reactor Oversight Process (ROP) Performance Indicators (PIs) for Unit 2 for Mitigating System Performance Index (MSPI) Heat Removal System and Safety System Functional Failures (SSFF). The unplanned unavailability experienced as a result of the temperature switch unit failure will result in an increase in the MSPI Heat Removal System PI by 0.2E-08, from -1.8E-08 to -1.6E-08, and remains green.

The green to white threshold for the MSPI Heat Removal System PI is 1.OE-06. The SSFF PI will increase by 1, from I to 2, and remains green. The green to white threshold for this PI is 6.

IV. CORRECTIVE ACTIONS

A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

1. Temperature switch unit 2RHS*TS85A was replaced.

B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

1. Develop and implement a maintenance strategy for Riley temperature switch units that will implement new preventative maintenance requirements.
2.

Refurbish all temperature switch units of the same model type as the failed unit.

3.

NMPNS has implemented Department Corrective Action Review Teams (DCARTs) and a Correct Action Completion Evaluation (CACE) committee to provide reinforcement and oversight of corrective action standards.

V. ADDITIONAL INFORMATION

A. FAILED COMPONENTS:

Reactor Building General Area temperature switch unit 2RHS*TS85A.

Manufacturer: Riley - Beaird, Inc \\ US Riley Corp Model: 86BPTEF-E B. PREVIOUS LERs ON SIMILAR EVENTS:

There are no previous LERs that are similar to this event. There are two 60-day telephone notifications that were made for temperature switch unit failures, as described below.

Event Number: 48570 On October 12, 2012, NMP2 received a Division I primary containment isolation signal which resulted in the closure of Group 5, 6, and 10 primary containment isolation valves (PCIVs). The Division I isolation signal was generated due to the failure of a temperature switch unit. The Division I and II temperature switch units were both reading within limits when the Division I unit failed. Since the isolation signal was not initiated in response to actual plant conditions or parameters satisfying the requirements for initiation, the isolation signal was determined to be invalid.

Event Number: 47547 On November 7, 2011, NMP2 received a Division II reactor building pipe chase high ambient temperature isolation signal, which resulted in closure of isolation valves in the reactor water cleanup (RWCU) system, the reactor core isolation cooling (RCIC) system, and the residual heat removal (RHR) system (isolation valve Groups 5, 6, 7, and 10). The isolation signal was generated by a new NUS/Scientech ambient temperature indicating switch that had recently been installed as a replacement for the original Riley temperature switch.

Operations personnel confirmed that conditions requiring isolation of the RWCU, RCIC, and RHR systems did not exist, based on a check of the Division 1 reactor building pipe chase high ambient temperature channel and area radiation monitors. Therefore, the isolation signal was determined to be invalid.

C. THE ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) COMPONENT FUNCTION IDENTIFIER AND SYSTEM NAME OF EACH COMPONENT OR SYSTEM REFERRED TO IN THIS LER:

COMPONENT Temperature Switch Reactor Pressure Vessel Capacitor Isolation Valve High-Pressure Coolant Injection System Reactor Core Isolation Cooling System Residual Heat Removal System Low-Pressure Coolant Injection System Low-Pressure Core Spray System IEEE 803 COMPONENT IDENTIFIER TS RPV CAP ISV N/A N/A N/A N/A N/A IEEE 805 SYSTEM IDENTIFICATION IJ N/A N/A N/A BJ BN BO BO BM D. SPECIAL COMMENTS:

None