10-22-2009 | On August 23, 2009, at 0915 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.481575e-4 months <br />, the Nine Mile Point Unit 2 (NMP2) control room received a High Pressure Core Spray ( HPCS) Inoperable annunciator and a Division 3 Diesel Direct Current Control Power Failure annunciator for one second, after which both annunciators cleared. An operator was immediately dispatched to the Division 3 switchgear room, but did not find any obvious failure.
During troubleshooting, a degraded connection was found between the removable and stationary parts of the HPCS breaker CLOSE fuse block. The contact gap for one of the receiver connections internal to the stationary section of the CLOSE fuse block was wider than the other 3 receiver connections. At that point, HPCS was declared inoperable per Technical Specification 3.5.1. The degraded receiver connection was adjusted and the CLOSE fuse block was reassembled. The HPCS pump was run and subsequently declared operable at 2046 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.78503e-4 months <br />.
Throughout the event, NMP2 continued to operate at 100% power. There were no other inoperable components impacting this event.
The apparent cause of this event was failure to incorporate a GE Service Advisory Letter (SAL) 322.1 recommendation for checking the fuse block contact wipe or contact gap settings as part of the 4.16 kV breaker Preventive Maintenance (PM).
To prevent reoccurrence, the procedures for the 4.16kV and 13.8 kV breaker PMs will be revised to include the fuse block contact gap adjustment. |
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LER-2009-001, Momentary Loss of Control Power to High Pressure Core Spray, Pump Due to Degraded Fuse Block ConnectionDocket Number |
Event date: |
08-23-2009 |
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Report date: |
10-22-2009 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident |
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4102009001R00 - NRC Website |
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I. DESCRIPTION OF EVENT
A. PRE-EVENT PLANT CONDITIONS:
Prior to and throughout this event Nine Mile Point Unit 2 (NMP2) was stable at 100% power with no other inoperable systems affecting this event.
B. EVENT:
At 0915 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.481575e-4 months <br /> on August 23, 2009, with (NMP2) operating at 100% power, the control room received an unexpected annunciator for High Pressure Core Spray (HPCS) Inoperable and a Division 3 Diesel Direct Current Control Power Failure annunciator. Both annunciators cleared one second later. An operator was dispatched to the HPCS (Division 3) switchgear room to investigate. It was determined that the two annunciators were indicative of a DC control power failure in the breaker circuit for the HPCS pump. A review of the prints showed that if the circuit monitoring relay for the HPCS breaker changed state, both annunciators would activate. The relay is normally energized and would only de-energize if the relay failed or power was lost to the circuit. Loss of control power to the HPCS pump breaker would prevent the HPCS pump from starting if high pressure injection were required.
During troubleshooting, a degraded connection was found between the removable and stationary parts of the HPCS breaker CLOSE fuse block. The contact gap for one of the receiver connections internal to the stationary section of the CLOSE fuse block was wider than the other 3 receiver connections. At 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br />, HPCS was declared inoperable and Technical Specification 3.5.1, Condition B, was entered. Condition B requires NMP2 to immediately verify by administrative means that the Reactor Core Isolation Cooling (RCIC) system is operable when RCIC is required to be operable AND restore the HPCS system to operable status within 14 days. In accordance with Condition B, the RCIC system was verified to be operable. The HPCS circuit was taken out of service and the fuse block connection repaired by readjusting the receiver connection. The circuit was re-energized and the HPCS pump was run. No further annunciators were received and the HPCS system was declared operable at 2046 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.78503e-4 months <br /> on August 23, 2009.
This event involved the potential loss of safety function of the NMP2 HPCS system for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, 31 minutes and 1 second. This includes the duration the annunciator was in alarm and the time it took for troubleshooting from 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br /> to 2046 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.78503e-4 months <br /> on August 23, 2009. The 8-hour Emergency Notification System notification required by 10 CFR 50.72 (b)(3)(v)(D) was completed on August 23, 2009, at 2152 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.18836e-4 months <br />.
Throughout the event, NMP2 continued to operate at 100% power. The only equipment affected by the degraded fuse connection was the HPCS pump and its associated breaker. The Division 3 Emergency Switchgear and associated Division 3 Emergency Diesel Generator were unaffected by this failure and were available throughout the event.
There was no impact on Nine Mile Point Unit 1 (NMP1) from this event.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO
THE EVENT:
There were with no other inoperable components that impacted this event.
D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
August, 23, 2009:
0915 HPCS loss of power annunciators were received in the control room:
091525 HPCS System INOP 091525 BKR102-2 DN/NO CONT PWR ALARM 091526 HPCS System ALMCLR 091526 BKR102-2 DN/NO CONT PWR ALMCLR 1715 Troubleshooting revealed that the contact gap for one of the receiver connections internal to the stationary section of the CLOSE fuse block was wider than the other 3 receiver connections. The HPCS system was declared inoperable per Technical Specification 3.5.1.
2043 The fuse block connection was repaired by readjusting the receiver connection. HPCS was returned to standby and the HPCS pump was declared inoperable, but available.
2046 The HPCS pump was run and then restored to operable status.
E.OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None.
F.METHOD OF DISCOVERY:
The fuse connection degradation was first suspected in the control room due to the two HPCS annunciators activating for 1 second.
G.MAJOR OPERATOR ACTION:
An operator was dispatched to the Division 3 switchgear room to investigate the cause of the alarms. After repairs were completed, the HPCS pump was run to verify operability.
H.SAFETY SYSTEM RESPONSES:
There were no safety system responses during this event and none were required.
II. CAUSE OF EVENT:
The cause of this event is omission of relevant information from maintenance procedures.
In February, 1978, General Electric issued a Service Advisory Letter (SAL), SAL 322.1, "Type NEC Fuse Holders 30 Amp and 60 Amp," in order to address the potential for loose fuse holders. NMP1 does not use this type of fuse holder, but NMP2 uses them in the 4.16 kV and 13.8 kV switchgear. The SAL was reviewed by Condition Report (CR) 1998-0790, but one recommendation was not incorporated into the maintenance procedures for high voltage switchgear breakers.
Repeated removal and installation of the close fuses for the HPCS breaker resulted in the contact gap of one of the receiver connections within the stationary fuse block to be wider than it should have been. This caused the removable portion of the fuse block connection to not engage the stationary side properly. Had the adjustments recommended in the SAL been incorporated into the maintenance procedure for the HPCS breaker, the contact gap would have been adjusted at the last performed preventive maintenance evolution.
NMP CR 2009-005044 applies to this LER.
III. ANALYSIS OF THE EVENT:
This event is reportable in accordance with 10 CFR 50.73(a)(2)(v)(D) which states that any event or condition that could have prevented the fulfillment of the safety system function of structures or systems that are needed to mitigate the consequences of an accident is reportable.
The HPCS system circuit issue revealed itself at 0915 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.481575e-4 months <br /> when the annunciators in the control room activated for one second. The HPCS system was declared inoperable 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> later at 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br /> when it was determined that the HPCS fuse connection was degraded. The system was declared inoperable, but available, at 2043 when the circuit was re-energized. The HPCS pump was run with no further alarms and at 2046 the HPCS system was declared operable. The HPCS system was inoperable for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 31 minutes.
There were no other systems inoperable and no other system failures related to this event. There were no actual safety consequences for this event. HPCS is designed to provide a high pressure injection source to the reactor when required, including a LOCA (Loss of Coolant Accident). Throughout this event, the reactor was stable at 100% power. Had a LOCA occurred, RCIC (Reactor Core Isolation Cooling) was available as well as all other Emergency Core Cooling Systems (ECCS). Under this scenario, adequate core cooling is ensured by the operability of the redundant and diverse low pressure ECCS injection/spray subsystems in conjunction with the ADS (Automatic Depressurization System). Also the RCIC system would automatically provide makeup water at most reactor operating pressures.
This event resulted in a reduction in the Regulatory Oversight Process (ROP) Mitigating System Performance Index (MSPI) for the High Pressure Core Spray System from -1.8E-07 to -1.7E-07 compared to the Green-to- White threshold value of >1.0E-06. This reduction would not result in entry into the "Increased Regulatory (White) Response Band.
IV. CORRECTIVE ACTIONS:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
The CLOSE fuse block stationary and removable connections were adjusted and verified to fit tightly into each other.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
To prevent reoccurrence, the procedures for the 4.16kV and 13.8 kV breaker PMs will be revised to include the fuse block contact gap adjustment.
V. ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
The CLOSE fuse block stationary contact for HPCS pump breaker was the only failed component and it was repaired.
B. PREVIOUS LERs ON SIMILAR EVENTS:
There have been no previous LERs similar to this event.
C. THE ENERGY INDUSTRY IDENTIFICATION SYSTEM (EllS) COMPONENT FUNCTION IDENTIFIER
AND SYSTEM NAME OF EACH COMPONENT OR SYSTEM REFERRED TO IN THIS LER:
�COMPONENT IEEE 803 � IEEE 805 � PART
COMPONENT IDENTIFIER SYSTEM IDENTIFICATION NUMBER
Fuse Block� FUB� BG 0132A1578001 High Pressure Core Spray Pump� P� BG Division 3 Switchgear� SWGR� BG HPCS Breaker� BKR� BG Diesel Generator� DG� EK RCIC System� N/A� BN ADS System� N/A� N/A ECCS� N/A� BO D.SPECIAL COMMENTS:
None.
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| | Reporting criterion |
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05000410/LER-2009-001 | Momentary Loss of Control Power to High Pressure Core Spray, Pump Due to Degraded Fuse Block Connection | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000266/LER-2009-001 | Component Coolina Water PumD Inoperable In Excess of Technical Specification Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2009-001 | Containment Overpressure Not Ensured in the Appendix R Analysis | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000250/LER-2009-001 | Procedure Inadequacy Causes Control Room Ventilation Isolation Technical Specification Noncompliance | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2009-001 | Common Mode Failure of Reactor Building Isolation Dampers | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000530/LER-2009-001 | Manual Reactor Trip Due to a Loss of Instrument Air to the Containment Building | | 05000457/LER-2009-001 | Reactor Trip on Over Temperature Delta Temperature due to a Signal Spike on One Channel With Another Channel Placed in the Tripped Condition for Surveillance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000413/LER-2009-001 | Both Trains of Chemical and Volume Control, Auxiliary Feedwater and Containment Spray Systems were Inoperable due to a Component Failure | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000412/LER-2009-001 | Equipment Operability for Steam Generator Tube Rupture Safety Analysis Not Met | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vi) | 05000461/LER-2009-001 | Safety Function Lost Due to Capacitor Failure on Circuit Card | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000382/LER-2009-001 | Waterford 3 Steam Electric Station 05000382 1 OF 3 | | 05000370/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2009-001 | Containment Air Cooler Fans Inoperable Due to Misapplication of Potter and Brumfield Rotary Relays | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2009-001 | Reactor Trip Due to High Pressurizer Pressure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000281/LER-2009-001 | Manual Reactor Trip Initiated to Replace a Rod Control Data Logging Card | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000261/LER-2009-001 | Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2009-001 | Failure to Implement Required Technical Specification Actions Associated with Failed Surveillance Test | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000389/LER-2009-001 | Unit 2 Main Feedwater Isolation Valves Stroke Time Potentially Affected by Temperature | 10 CFR 50.73(a)(2)(I)(B) | 05000321/LER-2009-001 | Pump Suction Swap for HPCI and RCIC Non-Conservative With Respect To Technical Specification Requirements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2009-001 | Surveillance Test Inadvertently Violates Technical Specification 3.6.1 for Containment Operability | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2009-001 | III Duke Energy® BRUCE H HAMILTON Vice President McGuire Nuclear Station Duke Energy Corporation MGO1VP / 12700 Hagers Ferry Road Huntersville, NC 28078 704-875-5333 704-875-4809 fax bhhamilton@duke-energy.com June 24, 2009
U.S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, D.C. 20555
Subject: Duke Energy Carolinas, LLC
McGuire Nuclear Station, Units 1 and 2
Docket Nos. 50-369, 50-370
Licensee Event Report 369/2009-01, Revision 0
Problem Investigation Process (PIP) M-09-02216
Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached
is Licensee Event Report 369/2009-01, Revision 0, regarding
the past inoperability of the Nuclear Service Water System
"A" Trains due to potential for strainer fouling.
This report is being submitted in accordance. with 10 CFR
50.73 (a) (2) (i)- (B), an Operation Prohibited by Technical
Specifications, and 10 CFR 50.73 (a) (2) (v) (B), any Event.
or Condition That Could Have Prevented Fulfillment of the
Safety Function.
This event is considered to be of no significance with
respect to the health and safety of the public. There are
no regulatory commitments contained in this LER.
If questions arise regarding this LER, contact Rick Abbott
at 980-875-4685.
Very truly yours,
Bruce H. Hamilton
Attachment
www.duke-energy.corn m U.S. Nuclear Regulatory Commission
Date
Page 2
CC: L. A. Reyes, Regional Administrator •U.S. Nuclear Regulatory Commission, Region.II
Sam Nunn Atlanta Federal Center
•61 Forsyth Street, SW, Suite 23T85
Atlanta, GA 30303
J. H. Thompson, Jr. (Addressee Only)
Senior Project Manager (McGuire)
U.S. Nuclear Regulatory Commission
Mail Stop 0-8G9A
Washington, DC 20555
J. B. Brady
Senior Resident Inspector
U.S. Nucle'ar Regulatory Commission-
McGuire Nuclear Station
B. 0. Hall, Section Chief
Radiation Protection Section
1645 Mall Service Center.
Raleigh, NC 27699
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104t EXPIRES: 08/31/2010
(9-2007) Estimated burden per response to comply with this mandatory collection request: 50 hours. Repoded
lessons learned are incorporated into the licensing process and fed back to industry. Send comments
regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information (See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or digits/characters for each block) sponsor, and a person is not required to respond to, the information collection. LICENSEE EVENT REPORT (LER) 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE _McGuire Nuclear Station, . 0369 8 Unit 1 05000- OF 4. TITLE Nuclear Service Water System (NSWS)d
"A" Trains Past Inoperable when aligned
to the Standby Nuclear Service Water Pond due to'corrosion.
(SNSWP) | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000456/LER-2009-001 | Steam Generator Tube Exceeding Plugging Criteria Remained In Service During Previous Cycle | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000395/LER-2009-001 | Inadequate Procedure Results In EDG Not Obtaining Maximum Load Required By Technical Specification | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2009-002 | Reactor Coolant System Pressure Boundary Leakage | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000373/LER-2009-002 | Loss of Shutdown Cooling Due to Spurious Closure of the Shutdown Cooling Suction Isolation Valve | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000382/LER-2009-002 | Waterford 3 Steam Electric Station 05000382 10OF 4 | | 05000278/LER-2009-002 | Inoperable 'A' Wide Range Neutron Monitor Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000287/LER-2009-002 | Unit 3 Trip Due to Generator Phase Differential Lockout | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000263/LER-2009-002 | | | 05000412/LER-2009-002 | Unacceptable Indications Identified During Reactor Vessel Head Inspection | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000354/LER-2009-002 | As Found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000346/LER-2009-002 | Vibration Induced Failure of Temperature Instrument Results in Operation above Licensed Power Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2009-002 | Failure to Complete Technical Specifications Required Action Within the Allowed Completion Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2009-002 | Feedwater Isolation Initiates Auxiliary Feedwater System During Refueling Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000254/LER-2009-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 OF 5 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000305/LER-2009-002 | Steam Exclusion Door Blocked Open During Maintenance Activities | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000250/LER-2009-002 | Turkey Point Unit 3 05000250 1 of 10 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000220/LER-2009-002 | High Pressure Coolant Injection System Initiation Following a Manual Turbine Trip Due to High Turbine Bearing Vibrations | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2009-002 | Manual Scram On Low Water Level Caused By Turbine Trip From Hydraulic Fluid Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2009-003 | Containment Spray Pump A Inoperable At Degraded Voltage Protection Setpoint | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000395/LER-2009-003 | ..Potential Loss of Residual Heat Removal System Safety Function In Mode 4 Due To An Unanalyzed Condition0 | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000389/LER-2009-003 | RCP 2B2 Lower Seal Cavity Line Leak | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000323/LER-2009-003 | Containment Sump Recirculation Valve Position Interlock Failure Due to Inadequate Testing | | 05000263/LER-2009-003 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000261/LER-2009-003 | Manual Reactor Trip Due to Failure of 'A' Steam Generator Level Module | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2009-003 | Reactor Recirculation Pump Failure Results in Manual Reactor Protection System Actuation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000361/LER-2009-003 | Pressurizer Auxiliary Spray Failed Inservice Test | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000457/LER-2009-003 | Drain Procedure for ECCS Suction Line Creates an Unanalyzed Condition Due to Inadequate Configuration Requirements | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000237/LER-2009-003 | Emergency Diesel Generator Oil Leak | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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