03-16-2012 | On December 9, 2011, at 0908, Nine Mile Point Unit 2 (NMP2) was operating at 100 percent of rated thermal power when alert alarms were received for containment monitoring particulate channels. These alarms were accompanied by a rise in unidentified drywell leakage and drywell pressure. At 1046, a manual shutdown of Unit 2 was initiated due to exceeding the Technical Specification (TS) Limiting Condition for Operation for unidentified leakage in the drywell. TS 3.4.5 requires action to be taken if unidentified leakage increases > 2 gpm within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period while in Mode 1. Peak drywell floor drain leakage was 3.7 gpm. Entry into the drywell revealed a packing leak from the Reactor Coolant System ( RCS) "A" blocking valve 2RCS*MOV18A.
The valve stem packing leak occurred due to a score in the packing material created by a burr on the valve stem. The burr was created during packing replacement in August 2011 when the plant was shutdown due to high unidentified drywell leakage from the packing of this same valve.
The root cause of this event was that Nine Mile Point leadership did not exhibit a questioning attitude toward potential error likely situations. Leadership did not appropriately identify situations where precursors, such as lack of adequate procedure details and environmental conditions, were challenges to workmanship. |
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LER-2012-001, Forced Shutdown Due to an Increase in Drywell Leakage in Excess of Technical Specifications LimitDocket Number |
Event date: |
12-09-2011 |
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Report date: |
03-16-2012 |
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Reporting criterion: |
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
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4102012001R01 - NRC Website |
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I. DESCRIPTION OF EVENT
A. PRE-EVENT PLANT CONDITIONS:
Prior to this event, Nine Mile Point Unit 2 (NMP2) was operating at 100 percent rated thermal power with no inoperable systems affecting this event.
B. EVENT:
On December 9, 2011, at 0908, NMP2 was operating at 100 percent of rated thermal power when alert alarms were received for containment monitoring particulate channels. These alarms were accompanied by a rise in unidentified drywell leakage and drywell pressure. At 1046, a manual shutdown of Unit 2 was initiated due to exceeding the Technical Specifications (TS) Limiting Condition for Operation (LCO) for unidentified leakage in the drywell. TS 3.4.5 requires action to be taken if unidentified leakage increases > 2 gpm within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period while in Mode 1.
There was no impact on Nine Mile Point Unit 1 (NMP1) from this event.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE
EVENT:
There were no inoperable components or systems that contributed to this event.
D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES (note: all times are on December 9, 2011, unless otherwise noted):
0903 - Identified rising unidentified drywell leakage rate and a corresponding rise in drywell pressure.
0905 - Identified rising trend on particulate monitor 2CMS*CAB10A-2.
0908 - 2CMS*CAB10A-2 in alert.
0911 - 2CMS*CAB10B-2 in alert.
0915 - Reactor Coolant System (RCS) unidentified leakage is 2.35 gpm, entered TS 3.4.5 Condition B, which requires the unidentified leakage increase to be reduced to within limit within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or the source of the unidentified leakage increase to be identified within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
0918 - The shift manager directed unit shutdown.
1046 - Power reduction commenced.
1315 - Entered TS 3.4.5 Condition C, which requires the plant to be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />, due to not meeting TS 3.4.5 Condition B.
2237 - All Control Rods are fully inserted.
2317 - Mode Switch placed in Shutdown. Plant in Mode 3, Hot Shutdown.
12/10/2011 - 1813 - Reactor Operation is Mode 4, Cold Shutdown.
E. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None
F. METHOD OF DISCOVERY:
On December 9, 2011, at 0908, Operations noted that the containment particulate radiation monitors went into alarm and that RCS unidentified leakage was increasing.
G. MAJOR OPERATOR ACTION:
At 0915, TS 3.4.5 Condition B was entered for RCS unidentified leakage rate increase > 2 gpm within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. At 1046, a manual shutdown of NMP2 was initiated.
H. SAFETY SYSTEM RESPONSES:
None. No operational conditions requiring the response of safety systems occurred as a result of this event.
II. CAUSE OF THE EVENT:
The direct cause of this event is failed packing on Reactor Coolant Pump "A" discharge blocking valve 2RCS*MOV18A. This caused the RCS unidentified leakage rate to exceed the TS 3.4.5 limit. The valve stem packing leak occurred due to a score in the packing material created by a burr on the valve stem. The burr was created during packing replacement in August 2011 when the plant was shutdown due to high unidentified drywell leakage from the packing of this same valve. In August 2011, while removing the failed packing set, destructive removal of the packing set's carbon bushing was performed. The carbon bushing is designed to be removed using a packing puller and the pre-drilled and tapped holes in the top of the carbon bushing. Due to valve stem mis-alignment, the bushing was pinched in the stuffing box and could not be removed in this manner.
Hardened tools, including a machinist's punch and hammer, were used to break apart and remove the bushing.
The physical arrangement of the stuffing box and packing set's carbon bushing allowed the punch to be at such an angle to allow a direct strike to the stem. It is believed at this point the burr was created on the valve stem.
The root cause of this event was that Nine Mile Point leadership did not exhibit a questioning attitude toward potential error likely situations. Leadership did not appropriately identify situations where precursors, such as lack of adequate procedure details and environmental conditions, were challenges to workmanship.
This event was entered into the NMPNS corrective action program (Condition Report CR-2011-010906).
III. ANALYSIS OF THE EVENT:
This event is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(A), "The completion of any nuclear plant shutdown required by the plant's Technical Specifications.
There were no systems inoperable and no system failures related to this event. There were no actual safety consequences from this event. The leakage was from the blocking valve packing and was not indicative of RCS component wear. The leakage was contained within the drywell. The maximum leakage rate noted during this event was 3.7 gpm, which is within the TS limit of 5 gpm. Even if the packing had catastrophically failed, the leakage would still have been contained within the drywell and the plant would have been capable of reaching a safe shutdown condition. There were no system failures that prevented the safe shutdown of the plant. It is therefore concluded that even if a design basis accident had occurred concurrent with this event, all safety systems would have operated to safely mitigate the event. Based on the above considerations, the safety significance of this event is low, and the event did not pose a threat to the health and safety of the public or plant personnel.
This event does not affect the NRC Regulatory Oversight Process (ROP) Index for Unplanned Scrams because the shutdown did not involve a scram. This event increases the ROP Index for Unplanned Power Changes per 7000 Critical Hours from 1.6 to 2.5.
IV. CORRECTIVE ACTIONS:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
1. Removed burr and polished all high spots on the stem of 2RCS*MOV18A to improve the condition of the sealing surface.
2. Installed modified packing on 2RCS*MOV18A and torqued.
3. Installed modified packing on 2RCS*MOV18B and torqued, as a precautionary measure.
4. The packing for similar RCS pump suction blocking valves 2RCS*MOV10A and 2RCS*MOV10B were re-torqued.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
1. Revise the appropriate procedures to include required tools and precautions for proper removal of valve packing.
2. Develop and implement a case study of this event to highlight the elements of an engaged thinking workforce necessary to overcome conditions that are not conducive to completing high quality maintenance. The expected outcome will be improved behaviors in terms of supervisory intervention to mitigate error-likely situations.
3. Revise training for Mechanical Maintenance personnel to include human performance and safety dynamic learning activity course material during initial and continuing training that incorporates the lessons learned from this event.
V. ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None
B. PREVIOUS LERs ON SIMILAR EVENTS:
There are three similar LERs:
1. NMP2 LER 2011-002. On August 6, 2011, NMPNS identified drywell floor drain leakage exceeding the maximum limits of TS 3.4.5 for unidentified drywell leakage. The cause of the unidentified leakage was determined to be failed packing in a reactor coolant system discharge blocking valve, 2RCS*MOV18A.
The corrective actions included repacking the valve to stop the leakage and re-torquing the packing for the remaining similar valves in the RCS to protect against leakage. The primary cause of the packing failure was determined to be vibration and flow turbulence. This caused the packing to relax and fail on 2RCS*MOV18A.
2. NMP2 LER 2001-007. On December 15, 2001, NMPNS identified drywell floor drain leakage approaching the maximum limits of TS 3.4.5 for unidentified drywell leakage. The cause of the unidentified leakage was determined to be failed packing in a reactor coolant system discharge blocking valve, 2RCS*MOV18A. The corrective actions included installing modified packing to stop the leakage and re-torquing the packing for the remaining similar valves in the RCS to protect against leakage. The primary cause of the packing failure was determined to be packing ring extrusion into the leak-off port.
3. NMP1 LER 2006-001. On June 11, 2006, NMPNS commenced a planned downpower to perform a drywell entry to determine the cause of increased drywell leakage. The source of the increased leakage was determined to be the reactor coolant system drain valve packing. The cause of the packing leak was installation of incorrect packing in March 1997. The packing that was installed did not have the same diameter as the inside diameter of the stuffing box. During the shutdown, NMPNS replaced the packing in the leaking RCS pump drain valve.
C. THE ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) COMPONENT FUNCTION
IDENTIFIER AND SYSTEM NAME OF EACH COMPONENT OR SYSTEM REFERRED TO IN THIS
LER:
COMPONENT IEEE 803 IEEE 805
COMPONENT IDENTIFIER SYSTEM IDENTIFICATION
Reactor Coolant Blocking Valves V AD Reactor Protection System NA JC
None
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| | Reporting criterion |
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05000413/LER-2012-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2012-001 | Unanalyzed Condition Affecting Essential Raw Cooling Water System due to External Flooding | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000388/LER-2012-001 | Two Control Room Floor Cooling Systems Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000395/LER-2012-001 | Vice President, Nuclear Operations 803.345.4342 August 3, 2012SCE~r .so A SCANA COMPANY Document Control Desk U. S. Nuclear Regulatory Commission
Washington, DC 20555
Dear Sir / Madam: Subject:VVIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50-395 OPERATING LICENSE NO. NPF-12 LICENSEE EVENT REPORT (LER 2012-001-01) CORE EXIT THERMOCOUPLES & REACTOR WATER LEVEL INDICATION SYSTEM INOPERABLE DUE TO AN INADEQUATE MAINTENANCE PROCEDURE Attached is Licensee Event Report (LER) No. 2012-001-01 for the Virgil C. Summer Nuclear Station Unit 1. This revised report describes a condition where Core Exit Thermocouples and Reactor Water Level Indication System would not be operable for accident monitoring. This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B). This letter and attached LER contain no new commitments and no revisions to existing
commitments.
Should you have any questions, please call Bruce Thompson at (803) 931-5042. Very truly yours, Dal Thomas D. Gatlin TS/TDG/jw
Attachment
c: K. B. Marsh P. Ledbetter S. A. Byrne J. C. Mellette J. B. Archie EPIX Coordinator N. S. Carps K. M. Sutton J. H. Hamilton INPO Records Center R. J. White Marsh USA, Inc. W. M. Cherry R. J. Schwartz V. M. McCree NSRC R. E. Martin RTS (CR-11-01807) NRC Resident Inspector FileV(818.07) M. N. Browne PRSF (RC-12-0116) V fALVirgil C. Summer Station • Post Office Box 88 .Jenkinsville, SC • 29065 • F (803) 345-5209 1 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours.0Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocollects.resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management andLICENSEE EVENT REPORT (LER) Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Virgil C. Summer Nuclear Station Unit 1 05000 395 1 OF 5 4. TITLE Core Exit Thermocouples & Reactor Water Level Indication System Inoperable due to Inadequate Maintenance Procedure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000397/LER-2012-001 | DG-3 Inoperable for Longer than Allowed by TS Due to Failed Governor 05000 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-001 | Forced Shutdown Due to an Increase in Drywell Leakage in Excess of Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000289/LER-2012-001 | Single Condition Making Independent Trains Inoperable | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2012-001 | Common Cause Inoperability of Both Trains of Motor Driven Auxiliary Feedwater (AFW) Pumps Due to Inability to Control AFW Regulating Valves After Isolation of Nitrogen Backup | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000265/LER-2012-001 | Main Steam Isolation Valve Local Leak Rate Test Exceeds Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2012-001 | Two Main Steam Safety Valves Failed Pre-outage Setpoint Testing Due to Abnormal Spring Geometry | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-001 | Technical Specification Required Plant Shutdown Due to Missed Surveillance and Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000483/LER-2012-001 | Modification Implementation Error Adversely Impacted the Containment Cooling System | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2012-001 | Containment Concrete Thickness At Spalled Patch Does Not Meet Technical Specification Design Value | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000414/LER-2012-001 | Carolinas Duke Energy Carolinas, LLC 4800 Concord Rd. York, SC 29745 803-701-4251 December 20, 2012 U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
Subject:�Duke Energy Carolinas, LLC (Duke Energy)
Catawba Nuclear Station, Units 1 and 2
Docket Nos. 50-413 and 50-414
Licensee Event Report 414/2012-001
Pursuant to 10 CFR 50.73(a)(1) and (d), attached is Licensee Event Report 414/2012-001,
Revision 0 entitled, "Diesel Generator (DG) 2B Was Unknowingly inoperable from 09/28/12 to
10/23/12 Due to Failed Tachometer Relay Power Supply".
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B), 10 CFR
50.73(a)(2)(ii)(B), and 10 CFR 50.73(a)(2)(v)(A)-(D).
There are no regulatory commitments contained in this letter or its attachment. This event is considered to be of no significance with respect to the health and safety of the
public.
If there are any questions on this report, please contact L.J. Rudy at (803) 701-3084. Kelvin Henderson LJR/s Attachment www. duke-energy. corn Document Control Desk Page 2 December 20, 2012 xc (with attachment): V.M. McCree Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, GA 30303-1257 J.H. Thompson (addressee only) NRC Project Manager U.S. Nuclear Regulatory Commission Mail Stop 8-G9A 11555 Rockville Pike Rockville, MD 20852-2738 G.A. Hutto, III NRC Senior Resident Inspector Catawba Nuclear Station INPO Records Center 700 Galleria Place Atlanta, GA 30339-5957 Document Control Desk Page 3 December 20, 2012 bxc (electronic copy)(with attachment): INPO L.E. Harmon C.S. Kamilaris R.D. Hart G.Y. Helton S.F. Hatley (ICES) M.K. Green R.T. Simril, Jr. B.C. Carroll M.C. Nolan W.J. Pritchett, Jr. T.L. Patterson K.R. Alter H.D. Brewer R.E. Abbott, Jr. B.J. Horsley S.L. Western bxc (hard copy)(with attachment): D.B. Alexander L.S. Nichols L.J. Rudy ELL Master File CN-801.01 LER File RGC Date File NCMPA-1 NCEMC PMPA ICES Lee.Harmon@NRC.gov NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013
(10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported
lessons learned are incorporated into the licensing process and fed back to industry. Send commentsLICENSEE EVENT REPORT (LER) regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.resource@nrclov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used(See reverse for required number of to impose an information collection does not display a currently valid OMB control number, the NRCdigits/characters for each block) may not conduct or sponsor, and a person is not required to respond to, the information collection. r1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 05000414 10OF •4. TITLE Diesel Generator (DG) 2B Was Unknowingly Inoperable from 09/28/12 to 10/23/12 Due to Failed Tachometer
Relay Power Supply | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000247/LER-2012-001 | Technical Specification (TS) Prohibited Condition Caused by an Inoperable 23 Emergency Diesel Generator Fuel Oil Storage Tank Due to Fuel Oil Below TS Limit | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2012-001 | Unanalyzed Conditions Exist for Standby Shutdown Facility Mitizated Events | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000445/LER-2012-002 | COMANCHE PEAK 05000445 10OF06 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000413/LER-2012-002 | Discovery of Inadequacy in Surveillance Testing of Solid State Protection System | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-002 | Unplanned LCO 3.5.4 Entry Due to RWST alignment to Purification | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-002 | Loss of Isolation Function on RHR Shutdown Cooling Suction Line due to Breaker Trip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000482/LER-2012-002 | . One Train of Automatic Safety Infection Blocked During Entry Into Mode 3 Due To Procedural Weakness | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2012-002 | Emergency Diesel Generator Vibration Trip Not Bypassed For Non-Accident Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000346/LER-2012-002 | Leak from Reactor Coolant Pump Seal Piping Socket Weld due to High Cycle Fatigue | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000333/LER-2012-002 | High Pressure Coolant Injection Pressure Control Valve Failure | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2012-002 | Unit 2 Emergency Diesel Generators Inoperable Due To Missing Flood Control Barrier Seal | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000250/LER-2012-002 | Non-compliance with TS 3.4.9.3 due to Manual Isolation Valve Found in Incorrect TS Configuration | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000278/LER-2012-002 | Failure of Primary Containment Isolation Valve due to Foreign Material Results in Condition Prohibited by TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2012-002 | Unit 2 Reactor Trip from Generator Trip Due to Incorrect Relay Setting | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2012-002 | Unplanned Actuation of 121 Motor Driven Cooling Water Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-002 | Improper Rotor Installation Causes Failure of Diesel Generator to Start | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2012-002 | Technical Specification (TS) Prohibited Condition Caused by New Fuel Assemblies Stored in a Configuration Prohibited by the TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2012-002 | Inlet Steam Drain Pot Drain Line Leaks Result in HPCI Inoperabilities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2012-003 | Reactor Building Doors Opened Simultaneously Causes Loss of Safety Function | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000410/LER-2012-003 | Suppression Pool Level Below Technical Specification Limit During Mode Change | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-003 | Plant Modification Interfered with the Operation of Containment Wide Range Level Indicator | | 05000298/LER-2012-004 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000410/LER-2012-004 | Manual Reactor Scram due to a Loss of Main Turbine Gland Sealing Steam Resulting in Lowering Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2012-004 | Essential Chiller Oil Leak Creates Unanalyzed Past Operability Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000265/LER-2012-004 | Drywell Radiation Monitor Failed Downscale | | 05000261/LER-2012-004 | Reactor Tripped Due to a Turbine Trip Caused by a Feedwater Isolation Signal from Steam Generator 'B' High Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000454/LER-2012-004 | Reactor Pressure Vessel Head Control Rod Drive Mechanism Penetration Nozzle Weld Repair Surface Indications | | 05000254/LER-2012-004 | Breech in Secondary Containment | | 05000482/LER-2012-004 | Two Charging Pumps Capable of Injecting into the RCS Due to Inadequate Definition of Centrifugal Charging Pump in LCO 3.4.12 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-005 | Automatic Diesel Actuation Due to the Loss of a 115 kV Offsite Power Source | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-005 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000298/LER-2012-006 | Missing Vent Plug Results in Technical Specifications Prohibited Condition | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2012-007 | High Pressure Coolant Injection System Logic Actuation Following an Automatic Turbine Trip Signal Due to High Reactor Water Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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