On March 31, 2016 at approximately 06:03, while performing lineups for Local Leak Rate Testing ( LLRT), the Control Room received a Division two (2) Primary Containment Isolation System ( PCIS) alarm along with a Division two (2) Heating Ventilation Air Conditioning ( HVAC) isolation, and Standby Gas Treatment ( SBGT) and Control Room Emergency Outside Air Supply System ( CREOASS) initiation. This was shortly followed by the Division one (1) Primary Containment Isolation System ( PCIS) alarm along with a Division one (1) Heating Ventilation Air Conditioning ( HVAC) isolation, and Standby Gas Treatment ( SBGT) and Control Room Emergency Outside Air Supply System ( CREOASS) initiation.
The valid actuation signal was the result of the performance of four (4) LLRT procedures concurrently for four (4) separate drywell pressure instruments. These instruments are divisional with each powered by a different channel.
Placing each in "TEST" mode, resulted in bringing both the Division one (1) and Division two (2) isolation logic. The cause of the valid actuation signal was less than adequate procedure use and adherence by Operations staff members. Corrective action included coaching and remediation of an individual involved in confirming the position of the test switch, communication to the Operations organization and revision to the LLRT procedures.
There was no operational impact as a result of this this event due to the plant being in Mode 5. This event resulted in a eight (8) hour Emergency Notification System (ENS) communication pursuant to 10 CFR 50.72(b)(3)(iv)(A).
This Licensee Event Report (LER) is being communicated pursuant to 10 CFR 50.73(a)(2)(iv)(A). |
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Category:Letter
MONTHYEARML24289A1252024-10-22022 October 2024 – Authorized Alternative to Requirements of the ASME OM Code PLA-8145, Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-81452024-10-21021 October 2024 Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-8145 ML24291A1562024-10-16016 October 2024 Missed Annual Inventory Required by 40 CFR 266, Subpart in PLE 0026645 PLA-8148, Registration for the Use of Spent Fuel Storage Casks 311, 308, and 3102024-10-15015 October 2024 Registration for the Use of Spent Fuel Storage Casks 311, 308, and 310 PLA-8141, Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-81412024-09-18018 September 2024 Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-8141 PLA-8142, Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-81422024-09-18018 September 2024 Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-8142 ML24260A2312024-09-17017 September 2024 Senior Reactor and Reactor Operator Initial License Examinations 05000387/LER-2024-002, B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor2024-09-16016 September 2024 B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24233A2192024-09-0303 September 2024 – Authorized Alternative to Requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code IR 05000387/20240052024-08-29029 August 2024 Updated Inspection Plan for Susquehanna Steam Electric Station, Units 1 and 2 (Report 05000387/2024005 and 05000388/2024005) 05000387/LER-2023-004-01, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-08-26026 August 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum 05000387/LER-2024-001-01, Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear2024-08-21021 August 2024 Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear IR 05000387/20240022024-08-12012 August 2024 Integrated Inspection Report 05000387/2024002 and 05000388/2024002 ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification PLA-8117, 23rd Refueling Outage Owners Activity Report (PLA-8117)2024-07-23023 July 2024 23rd Refueling Outage Owners Activity Report (PLA-8117) ML24197A0982024-07-15015 July 2024 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000387/2024010 and 05000388/2024010 PLA-8126, Response to Request for Confirmation of Information Regarding Relief Request 1RR062024-05-29029 May 2024 Response to Request for Confirmation of Information Regarding Relief Request 1RR06 ML24127A2262024-05-29029 May 2024 Issuance of Amendment Nos. 288 and 272 Adoption of TSTF-563 PLA-8122, Annual Radiological Environmental Operating Report (PLA-8122)2024-05-28028 May 2024 Annual Radiological Environmental Operating Report (PLA-8122) 05000387/LER-2024-001, Main Steam Isolation Valve Leakage2024-05-23023 May 2024 Main Steam Isolation Valve Leakage PLA-8115, Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115)2024-05-23023 May 2024 Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115) IR 05000387/20240012024-05-13013 May 2024 Integrated Inspection Report 05000387/2024001 and 05000388/2024001 IR 05000387/20244042024-05-0707 May 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000387/2024404 and 05000388/2024404 PLA-8095, 2023 Annual Radiological Environmental Operating Report (PLA-8095)2024-04-22022 April 2024 2023 Annual Radiological Environmental Operating Report (PLA-8095) PLA-8094, Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-80942024-04-22022 April 2024 Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-8094 PLA-8101, Re 2023 Annual Report of Radiation Exposure2024-04-22022 April 2024 Re 2023 Annual Report of Radiation Exposure ML24082A1372024-04-22022 April 2024 Issuance of Amendment Nos. 287 and 271 Adoption of TSTF-568, Revision 2 and Associated Technical Specification Changes PLA-8102, Annual Environmental Operating Report (Nonradiological) PLA-81022024-04-11011 April 2024 Annual Environmental Operating Report (Nonradiological) PLA-8102 PLA-8113, Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113)2024-04-11011 April 2024 Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113) PLA-8112, Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-81122024-04-0909 April 2024 Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-8112 PLA-8110, Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110)2024-04-0404 April 2024 Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110) PLA-8100, Property Insurance Program (PLA-8100)2024-04-0101 April 2024 Property Insurance Program (PLA-8100) ML24092A4022024-04-0101 April 2024 Annual Financial Report (PLA-8098) PLA-8109, Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109)2024-03-21021 March 2024 Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109) PLA-8107, Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance2024-03-19019 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance ML24067A2512024-03-19019 March 2024 Authorized Alternative to Requirements of the ASME Code ML24044A2532024-03-14014 March 2024 Associated Independent Spent Fuel Storage Installation – Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0077 (Security Notifications, Reports, and Recordkeeping & Suspicious Activity Reporting)) IR 05000387/20240112024-02-29029 February 2024 Commercial Grade Dedication Inspection Report 05000387/2024011 and 05000388/2024011 IR 05000387/20230062024-02-28028 February 2024 Annual Assessment Letter for Susquehanna Steam Electric Station, Units 1 and 2 (Reports 05000387/2023006 and 05000388/2023006) ML24039A1882024-02-27027 February 2024 Issuance of Amendment Nos. 286 and 270 Changes to Technical Specifications for Control Rods ML24037A3072024-02-22022 February 2024 Summary of Regulatory Audit in Support of Relief Request 5RR-02 PLA-8099, Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099)2024-02-13013 February 2024 Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099) IR 05000387/20230042024-02-0707 February 2024 Integrated Inspection Report 05000387/2023004 and 05000388/2023004 05000387/LER-2023-004, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-01-0909 January 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum PLA-8096, Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval2024-01-0404 January 2024 Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval PLA-8077, Emergency Plan Revision 67 (PLA-8077)2023-12-27027 December 2023 Emergency Plan Revision 67 (PLA-8077) IR 05000387/20230102023-12-11011 December 2023 Fire Protection Team Inspection Report 05000387/2023010 and 05000388/2023010 PLA-8088, Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088)2023-12-0505 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088) 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000387/LER-2024-002, B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor2024-09-16016 September 2024 B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor 05000387/LER-2023-004-01, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-08-26026 August 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum 05000387/LER-2024-001-01, Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear2024-08-21021 August 2024 Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear 05000387/LER-2024-001, Main Steam Isolation Valve Leakage2024-05-23023 May 2024 Main Steam Isolation Valve Leakage 05000387/LER-2023-004, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-01-0909 January 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum 05000387/LER-2023-003, D Diesel Generator Inoperable Due to Clogged Fuel Injectors2023-11-0909 November 2023 D Diesel Generator Inoperable Due to Clogged Fuel Injectors 05000387/LER-2023-002, Unplanned Lnoperability of the High Pressure Coolant Injection (HPCI) System Due Failure of the HPCI Turbine Stop Valve to Fully Close, Most Likely Due to Internal Corrosion and2023-06-0606 June 2023 Unplanned Lnoperability of the High Pressure Coolant Injection (HPCI) System Due Failure of the HPCI Turbine Stop Valve to Fully Close, Most Likely Due to Internal Corrosion And. 05000388/LER-2023-001, Secondary Containment Bypass Leakage Limit Exceeded Due Inadequate Procedure Guidance Resulting in Failure of the Inboard Containment Isolation Valve to Close and Pressurize2023-05-25025 May 2023 Secondary Containment Bypass Leakage Limit Exceeded Due Inadequate Procedure Guidance Resulting in Failure of the Inboard Containment Isolation Valve to Close and Pressurize 05000387/LER-2023-001, Inadvertent Contact Between Relay Cover and Relay Trip Contacts Resulted in Automatic Actuation of the ‘B’ Emergency Diesel Generator2023-05-22022 May 2023 Inadvertent Contact Between Relay Cover and Relay Trip Contacts Resulted in Automatic Actuation of the ‘B’ Emergency Diesel Generator 05000387/LER-2022-003, Inoperable 13.8kV Startup Transformer Due to Misaligned Load Tap Charger Local/Remote Control Switch2022-12-19019 December 2022 Inoperable 13.8kV Startup Transformer Due to Misaligned Load Tap Charger Local/Remote Control Switch 05000387/LER-2022-002-01, Automatic Reactor Scram Due to Reactor Protection System Actuation on High Reactor Vessel Pressure Signal Following Inadvertent Closure of Inboard Main Steam Isolation Valve2022-12-0505 December 2022 Automatic Reactor Scram Due to Reactor Protection System Actuation on High Reactor Vessel Pressure Signal Following Inadvertent Closure of Inboard Main Steam Isolation Valve 05000388/LER-2022-001, Re Inadequate Performance of Loss of Safety Determination Resulting in Both Divisions of Core Spray Being Inoperable2022-11-23023 November 2022 Re Inadequate Performance of Loss of Safety Determination Resulting in Both Divisions of Core Spray Being Inoperable 05000388/LER-2021-004-01, From Susquehanna Steam Electric Station, Unit 2 Main Turbine Pressure Regulator Inoperable for Longer than Allowed by Technical Specifications Due to Inadequate Valve Modification2022-11-0303 November 2022 From Susquehanna Steam Electric Station, Unit 2 Main Turbine Pressure Regulator Inoperable for Longer than Allowed by Technical Specifications Due to Inadequate Valve Modification 05000387/LER-2022-001-01, From Susquehanna Steam Electric Station Unit 1 - Main Steam Line Isolation Valve Leakage Due to Seating Surfaces Wear and Material Deposits2022-08-10010 August 2022 From Susquehanna Steam Electric Station Unit 1 - Main Steam Line Isolation Valve Leakage Due to Seating Surfaces Wear and Material Deposits 05000387/LER-2022-002, Automatic Reactor Scram Due to High Reactor Vessel Pressure Following Inadvertent Closure of Inboard Main Steam Isolation Valve2022-07-21021 July 2022 Automatic Reactor Scram Due to High Reactor Vessel Pressure Following Inadvertent Closure of Inboard Main Steam Isolation Valve 05000387/LER-2022-001, Main Steam Isolation Valve Leakage2022-06-0101 June 2022 Main Steam Isolation Valve Leakage 05000388/LER-2021-005-01, Condition Prohibited by Technical Specification Due to Setpoint Drift Attributed to Age Related Degradation2022-04-11011 April 2022 Condition Prohibited by Technical Specification Due to Setpoint Drift Attributed to Age Related Degradation 05000387/LER-2021-005-01, Automatic Reactor Scram Due to Turbine Control Valve Fast Closure2022-03-30030 March 2022 Automatic Reactor Scram Due to Turbine Control Valve Fast Closure 05000388/LER-2021-003-01, Automatic Reactor Scram Due to Main Turbine Trip Caused by Inadvertent Trip of the Main Generator Output Breakers2022-03-24024 March 2022 Automatic Reactor Scram Due to Main Turbine Trip Caused by Inadvertent Trip of the Main Generator Output Breakers 05000387/LER-2021-004-01, Loss of 1B RHRSW Pump Due to Cable Damage During Excavation Activities2022-03-21021 March 2022 Loss of 1B RHRSW Pump Due to Cable Damage During Excavation Activities 05000388/LER-2021-001-01, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switch2022-03-21021 March 2022 Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switch 05000388/LER-2021-005, Condition Prohibited by Technical Specification Due to Setpoint Drift2022-02-11011 February 2022 Condition Prohibited by Technical Specification Due to Setpoint Drift 05000388/LER-2021-002-01, Loss of Secondary Containment Due to Failed Differential Pressure Transmitter2022-02-0808 February 2022 Loss of Secondary Containment Due to Failed Differential Pressure Transmitter 05000387/LER-2021-005, Automatic Reactor Scram Due to Turbine Control Valve Fast Closure2022-01-26026 January 2022 Automatic Reactor Scram Due to Turbine Control Valve Fast Closure PLA-7977, Main Turbine Pressure Regulator Inoperable for Longer than Allowed by Technical Specifications2021-12-0909 December 2021 Main Turbine Pressure Regulator Inoperable for Longer than Allowed by Technical Specifications PLA-7976, Automatic Reactor Scram Due to Main Turbine Trip2021-12-0909 December 2021 Automatic Reactor Scram Due to Main Turbine Trip 05000387/LER-2021-004, Loss of 1B RHRSW Pump Due to Cable Damage During Excavation Activities2021-12-0101 December 2021 Loss of 1B RHRSW Pump Due to Cable Damage During Excavation Activities 05000387/LER-2021-003-01, Automatic Reactor Scram Due to Main Turbine Trip Caused by a C Isophase Bus Ground Fault2021-11-11011 November 2021 Automatic Reactor Scram Due to Main Turbine Trip Caused by a C Isophase Bus Ground Fault 05000388/LER-2021-002, Re Loss of Secondary Containment2021-10-28028 October 2021 Re Loss of Secondary Containment 05000387/LER-2021-003, Automatic Reactor Scram Due to Main Turbine Trip2021-09-16016 September 2021 Automatic Reactor Scram Due to Main Turbine Trip 05000388/LER-2021-001, Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switch2021-09-0101 September 2021 Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switch 05000388/LER-2017-0102018-02-0202 February 2018 Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches, LER 17-010-00 for Susquehanna, Unit 2 Regarding Condition Prohibited by Technical Specifications Due to Drift of Reactor Pressure Switches 05000387/LER-2017-0072017-10-0909 October 2017 Secondary Containment Declared Inoperable Due to the opening of a plenum., LER 17-007-00 for Susquehanna Steam Electric Station Regarding Secondary Containment Declared Inoperable Due to Supply Air Flow 05000387/LER-2017-0052017-10-0404 October 2017 Automatic Reactor Protection System Trip on High Neutron Flux, LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux 05000388/LER-2017-0082017-09-18018 September 2017 1 OF 3, LER 17-008-00 for Susquehanna, Unit 2, Regarding Condition Prohibited by Technical Specifications Due to a Loose Terminal Block Associated with a Primary Containment Isolation Valve 05000387/LER-2017-0062017-09-0606 September 2017 Control Room Envelope In-leakage Exceeded the Technical Specification Limit, LER 17-006-00 for Susquehanna, Unit 2, Regarding Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan 05000387/LER-2017-0042017-08-0404 August 2017 Secondary Containment Declared Inoperable Due to Failure of an Exhaust Fan Breaker., LER 17-004-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Failure of an Exhaust Fan Breaker 05000387/LER-2017-0012017-05-0505 May 2017 Secondary Containment Breach Due to Simultaneous Opening of Airlock Doors, LER 17-001-00 for Susquehanna, Unit 2, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Sticking Door Latch 05000388/LER-2017-0022017-05-0505 May 2017 Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 during Unit 2 Refueling, LER 17-002-00 for Susquehanna, Unit 2, Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 During Unit 2 Refueling 05000387/LER-2017-0032017-05-0505 May 2017 Susquehanna Steam Electric Station Unit 1 05000387, LER 17-003-00 for Susquehanna, Units 1 and 2, Regarding Loss of Secondary Containment Zone 3 Due to Fan Trip 05000387/LER-2017-0022017-04-12012 April 2017 Secondary Containment Breach due to Simultaneous Opening of Airlock Doors, LER 17-002-00 for Susquehanna, Unit 1, Regarding Secondary Containment Breach due to Simultaneous Opening of Airlock Doors 05000388/LER-2016-0052016-07-12012 July 2016 Unit 2 HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient, LER 16-005-00 for Susquehanna, Unit 2, Regarding HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient 05000387/LER-2016-0152016-06-15015 June 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error, LER 16-015-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error 05000387/LER-2016-0132016-06-0909 June 2016 Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors, LER 16-013-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors 05000387/LER-2016-0142016-06-0909 June 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error, LER 16-014-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error 05000387/LER-2016-0102016-05-31031 May 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency, LER 16-010-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency 05000387/LER-2016-0092016-05-26026 May 2016 Valid Primary Containment Isolation Actuation during Local Leak Rate Testing due to Human Performance Error, LER 16-009-00 for Susquehanna, Unit 1, Regarding Valid Primary Containment Isolation Actuation During Local Leak Rate Testing Due to Human Performance Error 05000387/LER-2016-0082016-05-19019 May 2016 Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing, LER 16-008-00 for Susquehanna, Unit 1, Regarding Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing 05000387/LER-2016-0052016-05-16016 May 2016 Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error, LER 16-005-00 for Susquehanna, Units 1 and 2, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error 05000387/LER-2016-0112016-05-16016 May 2016 Valve inoperability for a period longer than allowed by Technical Specifications, LER 16-011-00 for Susquehanna, Unit 1, Regarding Valve Inoperability for a Period Longer Than Allowed by Technical Specifications 2024-09-16
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
CONDITIONS PRIOR TO EVENT
Unit 1 - Mode 5, 0 percent Rated Thermal Power Unit 2- Mode 1, 100 percent Rated Thermal Power There were no systems, structures or components that were inoperable at the start of the event and contributed to the event.
EVENT DESCRIPTION
On March 31, 2016 at approximately 06:03, while performing lineups for Local Leak Rate Testing (LLRT), the Control Room received a Division two (2) Primary Containment Isolation System (PCIS) [EIIS System Identifier: JM] alarm along with a Division two (2) Heating Ventilation Air Conditioning (HVAC) [EIIS System Identifier: VA] isolation, and Standby Gas Treatment (SBGT)[EIIS System Identifier: BH] and Control Room Emergency Outside Air Supply System (CREOASS) initiation [EIIS System Identifier: VI]. This was shortly followed by the Division one (1) Primary Containment Isolation System (PCIS) alarm along with a Division one (1) Heating Ventilation Air Conditioning (HVAC) isolation, and Standby Gas Treatment (SBGT) and Control Room Emergency Outside Air Supply System (CREOASS) initiation. The following timeline summarizes the events prior to the PCIS isolation:
3/25/16: LLRT PCO (Plant Control Operator) requested Operations Supervision release LLRT procedure SE-159-123 (B channel) and LLRT procedure SE-159-125 (D channel). The Senior Reactor Operator (SRO) reviewed the procedures and outage schedule. There were no issues with performing the LLRTs noted and the work was released.
3/31/16: 0550: LLRT PCO began system alignment for LLRT procedure SE-159-122 (A channel) and LLRT procedure SE-159-124 (C channel). The Residual Heat Removal (RHR) to Radwaste (RW) Inboard Valve, F040, Isolation Logic Test Switch, B21H-S22A and RHR to RW Outboard Valve, F049, Isolation Logic Test Switch [EIIS Component identifier: HS], B21H-S22C were placed in the "TEST" position. These switches are located in the Upper Relay Room. These LLRT procedures were not released by Operations Supervision at the time of performance.
3/31/16: 0603: LLRT PCO began system alignment for LLRT procedures SE-159-123 (B Channel) and SE- 159-125 (D Channel). The RHR to RW Outboard Valve, F049, Isolation Logic Test Switch, B21H-S22D and the RHR to RW Inboard Valve, F040, Isolation Logic Test Switch, B21H-S22B were placed in the "TEST" position. These switches are located in the Lower Relay Room [EIIS System Code: NA].
At this time, the Control Room received Division 2 PCIS alarm (AR-112-G03), along with Division 2 HVAC isolation and SBGT and CREOASS initiations. Approximately 1 minute later, the Division 1 PCIS alarm, HVAC isolation and SBGT and CREOASS actuations occurred.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3/31/16: 0830: Due to the loss of Zone 3 HVAC, Operations backed- out of LLRT procedure SE-159-122, SE-159-123, SE-159-124, and SE-159-125. The associated test switches, B21H-S22A, B21H-S22C, B21H-S22B and B21H-S22D were restored to the "NORMAL" position.
The valid actuation signal was the result of performing the four (4) LLRT procedures concurrently for four (4) separate drywell pressure instruments, PSH-1N002A/B/C/D [EIIS Component Code: PS]. These instruments are divisional with each powered by a different channel. When placed in the "TEST" mode, the S22 (A/B/C/D) contacts open and de- energize (actuate) portions of the PCIS logic. By placing all four Nuclear Steam Supply Shutoff System (NSSSS) channels to "TEST" at the same time, both divisions of the isolation logic were made up and all corresponding valves and dampers received an isolation signal.
Based on the plant being in Refueling Mode (Mode 5) with Residual Heat Removal (RHR) Shutdown Cooling (SDC) out of service [EIIS System Code: BO], there was no operational consequence to this event.
All equipment functioned as expected, including the initiation of Standby Gas Treatment and Control Room Emergency Outside Air Supply System.
Based on investigation, only two of the four test procedures were released by Shift Supervision at the time of the event. LLRT procedure SE-159-123 (B Channel) and LLRT procedure SE-159-125 (D Channel) were released on 3/25/16. The LLRT procedure SE-159-122 (A Channel) and SE-159-124 (C Channel) were not signed and released to be performed. The LLRT Plant Control Operator (PCO) believed all four tests were signed and ready to be performed.
In addition to the utilizing procedures that were not released, each procedure contains a step as part of the "As Found Test Prerequisites" requiring verification that the all test switches, B21H-S22A, B, C, D, are in the "NORMAL" position prior to beginning the test.
This event resulted in an eight (8) hour NRC Emergency Notification System (ENS) noffication pursuant to 10 CFR 50.72(b)(3)(iv)(A) for a valid actuation of the primary containment isolation system. The ENS notification (#51838) was on 3/31/2016 at 12:45. This Licensee Event Report (LER) is pursuant to 10 CFR 50.73(a)(2)(iv)(A).
CAUSE OF EVENT
The cause of this event was less than adequate procedure use and adherence with respect to confirmation that Operations Shift Supervision approval was obtained prior to performance of each LLRT test and with respect to confirmation that the S22A/B/C/D switches were in the normal position prior to beginning the LLRT.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by interne( e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
ANALYSIS/SAFETY SIGNIFICANCE
There was no actual safety consequence as a result of this event. The primary containment isolation system operated as designed upon receipt of a valid isolation signal. Additionally, the Zone 3 HVAC isolation and subsequent actuation of both trains of the SBGT and CREOASS responded as expected. The response of these systems would ensure that fission product release and control room habitability are not affected in an actual event requiring PCIS isolation.
As discussed, the Unit was in Refueling Mode, with RHR Shutdown Cooling (SDC) out of service at the time of the event. While the RHR SDC Suction Inboard Isolation Valve, HV151F009, stroked closed as a result of the PCIS signal, the system was not in service at the time, and therefore did not impact system operation.
If RHR SDC was in service at the time of the event, the inboard isolation valve, HV151F009, breaker would have been open, and the outboard isolation valve, HV151F008, and the test switch, B21H-S22D, would have been protected equipment, which would have prevented the system isolation.
CORRECTIVE ACTIONS
The following corrective actions have been completed or are in progress to address this event:
1. Revise the LLRT procedures, SE-159-122 thru 126 and corresponding Unit 2 LLRT procedure, SE-259- 122 thru 126, to add a note in the "As Found Test Prerequisites" section that these procedures cannot be performed concurrently.
2. The individual involved in confirming that test switch B21H-S22A/B/C/D was in the NORMAL position, as required by the procedure, was coached and remediated.
3. An Operations department communication with respect to required authorization prior to commencement of work and review of 0I-AD-046, Operations Conduct of Outages, was issued.
PREVIOUS SIMILAR EVENTS
No other similar events were identified.
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05000387/LER-2016-010 | Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency LER 16-010-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Medical Emergency | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-001 | Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence LER 16-001-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-011 | Valve inoperability for a period longer than allowed by Technical Specifications LER 16-011-00 for Susquehanna, Unit 1, Regarding Valve Inoperability for a Period Longer Than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000388/LER-2016-001 | Secondary Containment Breach due to Simultaneous Opening of Airlock Doors Due to Degraded Latch Mechanism | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2016-002 | Secondary Containment Breach due to Simultaneous Opening of Airlock Doors Due to Degraded Latch Mechanism | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-012 | Secondary Containment declared inoperable due to loss of differential pressure as a result of a solenoid failure. | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-002 | Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence LER 16-002-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to an Airlock Doors Open Due to Random Occurrence | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-013 | Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors LER 16-013-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Simultaneous Opening of Double Airlock Doors | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2016-003 | Secondary Containment Inoperability due to Failure to Meet Surveillance Requirement 3.6.4.1.1 | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-003 | Unit 2 Zone 3 HVAC unable to maintain Zone 3 differential pressure greater than 0.25 in wg LER 16-003-00 for Susquehanna, Unit 1, Regarding Unit 2 Zone 3 HVAC Unable to Maintain Zone 3 Differential Pressure Greater Than 0.25 in wg | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000387/LER-2016-014 | Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error LER 16-014-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2016-004 | Unit 2 experienced an electrical transient resulting in a manual SCRAM | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-004 | Momentary Loss of Secondary Containment due to Both Airlock Doors on Elevation 779 of the Unit 2 Reactor Building being Opened at the Same Time LER 16-004-00 for Susquehanna, Unit 1, Regarding Momentary Loss of Secondary Containment Due to Both Airlock Doors on Elevation 779 of the Unit 2 Reactor Building Being Opened at the Same Time | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-015 | Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error LER 16-015-00 for Susquehanna, Unit 1, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to a Human Performance Error | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000387/LER-2016-005 | Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error LER 16-005-00 for Susquehanna, Units 1 and 2, Regarding Secondary Containment Declared Inoperable Due to Airlock Doors Open Due to Human Performance Error | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material | 05000388/LER-2016-005 | Unit 2 HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient LER 16-005-00 for Susquehanna, Unit 2, Regarding HPCI Manually Overridden Prior to a Manual Scram During a Plant Transient | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000387/LER-2016-006 | Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 LER 16-006-00 for Susquehanna, Unit 1, Regarding Implementation of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2016-007 | Inoperability of Swing Bus Transfer Switch Due to Deformed Bolt on Linkage LER 16-007-00 for Susquehanna, Unit 1, Regarding Inoperability of Swing Bus Transfer Switch Due to Deformed Bolt on Linkage | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2016-008 | Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing LER 16-008-00 for Susquehanna, Unit 1, Regarding Inoperability of Diesel Generator Due to Misalignment of MOC Switch Contacts Due to Inadequate Post Maintenance Testing | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000387/LER-2016-009 | Valid Primary Containment Isolation Actuation during Local Leak Rate Testing due to Human Performance Error LER 16-009-00 for Susquehanna, Unit 1, Regarding Valid Primary Containment Isolation Actuation During Local Leak Rate Testing Due to Human Performance Error | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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