05000324/FIN-2013003-05
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Finding | |
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Title | Inadequate Design Control for Allowable Jacket Water Leak Rate |
Description | An NRC-identified Green NCV of 10 CFR 50, Appendix B, Criterion III, Design Control, was identified for the failure of the licensee to verify the adequacy of the design acceptance criteria for jacket water leakage to ensure EDG 3 could meet the design basis mission time of seven days. The licensees corrective actions include developing a plan to fill the EDG jacket water system to ensure operation of the EDG for seven days. The licensee entered this issue into the CAP as NCR 615491. The inspectors determined that the failure to ensure sufficient jacket water to the EDGs, with a jacket water leak, for the seven-day mission time, was a performance deficiency. The violation is more than minor because it is associated with the design control attribute of the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the calculational error assuming a fourday mission time versus a seven-day mission time results in a condition where there was reasonable doubt on the capability of an EDG when a jacket water leak exists. Using IMC 0609, Appendix A, issued June 19, 2012, the SDP for Findings At-Power, the inspectors determined the finding screened to a detailed risk evaluation because the finding represented an actual loss of function of at least a single Train of EDG for greater than the TS Allowed Outage time. The regional SRA performed a Phase 3 analysis on the finding. The time to failure of the EDG due to the leak precluded any internal risk impact, since it exceeded 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to failure. A screening calculation was performed to estimate the impact the finding would have on an extended loss of offsite power from seismic or external flooding. The low likelihood of the seismic or external flood event occurring, combined with the short time the deficiency existed, resulted in a finding of very low safety significance (Green). The finding does not have a cross-cutting aspect since the performance deficiency is not indicative of current plant performance. Engineering evaluation was performed on July 7, 2004. |
Site: | Brunswick |
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Report | IR 05000324/2013003 Section 1R15 |
Date counted | Jun 30, 2013 (2013Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.15 |
Inspectors (proximate) | M Catts M Schwieg R Taylor G Hopper J Dodson |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control Technical Specification |
INPO aspect | |
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Finding - Brunswick - IR 05000324/2013003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Brunswick) @ 2013Q2
Self-Identified List (Brunswick)
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