05000324/FIN-2013002-01
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Finding | |
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| Title | Failure to Follow Procedure for Variable Frequency Drive Reactor Recirculation Pump Design Modification |
| Description | An NRC-identified Green finding was identified for the failure of the licensee to follow Procedure EGR-NGGC-0005, Engineering Change (EC), when performing the variable frequency drive (VFD) modification for the reactor recirculation pumps (RRPs). Specifically, between April 4, 2010 and the present, the licensee inappropriately used a Rapid Field Release (RFR) to revise the power supplies for the relays in the VFD system without re-evaluating the EC, the 10 CFR 50.59 Screen/Evaluation, and the Failure Modes and Effects Analysis (FMEA). This resulted in a new failure mode on a loss of the power supply causing a RRP runback and placing the plant in a flow transient, and a loss of cooling to the RRP seals. The licensee entered this issue into the corrective action program (CAP) as nuclear condition report (NCR) 581202. The performance deficiency associated with this finding was the failure of the licensee to follow Procedure EGR-NGGC-0005, Engineering Change (EC), when performing the VFD modification for the RRPs. The finding was more than minor because it was associated with the design control attribute of the Initiating Events Cornerstone and affects the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the VFD modification inappropriately causes a RRP runback on a loss of 480 VAC and core flow instability, and a loss of cooling to the RRP seals. Using IMC 0609, Appendix A, issued June 19, 2012, The SDP for Findings At-Power, the inspectors determined the finding was of very low safety significance because as a transient initiator due to the RRP runback, the finding did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. The inspectors determined the finding was also of very low safety significance because as a loss of coolant accident (LOCA) initiator, after a reasonable assessment of degradation, the finding would not result in exceeding the reactor coolant system leak rate for a small break LOCA or likely affect other systems used to mitigate a LOCA resulting in a total loss of their function. The finding has a cross-cutting aspect in the area of human performance associated with the work control attribute because the licensee did not appropriately coordinate work activities by incorporating actions to address the impact of changes to the work scope, associated with the VFD modification, on the plant. |
| Site: | Brunswick |
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| Report | IR 05000324/2013002 Section 1R18 |
| Date counted | Mar 31, 2013 (2013Q1) |
| Type: | Finding: Green |
| cornerstone | Initiating Events |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.18 |
| Inspectors (proximate) | A Nielsen C Dykes J Worosilo L Lake M Catts M Schwieg R Musser W Pursley |
| CCA | H.5, Work Management |
| INPO aspect | WP.1 |
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Finding - Brunswick - IR 05000324/2013002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Brunswick) @ 2013Q1
Self-Identified List (Brunswick)
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