0-0-1007 | On May 11, 2005, Pilgrim Station was notified that three Target Rock relief valve pilot assemblies exceeded the Technical Specification (TS) tolerance limit of 1115 psig ± 11 psi (± 1%) during routine testing at the Wyle Laboratories test facility. Certified replacement relief valve pilot assemblies were installed in the plant at the time of the notification.
The most probable cause of the as-found initial popping pressures exceeding the TS tolerance limit was corrosion bonding of the pilot valve assembly disk and seat. The corrosion bonding most likely developed while the pilot valve assemblies were in service. Poor fitting insulation was also identified as a contributing cause.
Corrective action taken includes replacing the pilot valves with certified tested replacements.
Engineering is evaluating options for resolving the high popping pressure reliability concern.
The condition posed no threat to public health and safety. |
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� FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) �
BACKGROUND
The Pilgrim Station Pressure Relief System (PRS) is designed to prevent over-pressurization of the ASME Boiler and Pressure Vessel Code qualified nuclear steam supply system. The PRS consists of two safety valves and four two-stage relief valves. These valves are installed in the main steam system piping upstream of the main steam isolation valves and are located within the Drywell. The safety valves are self-actuating, provide over-pressure protection, and discharge directly into the Drywell atmosphere when actuated. The relief valves augment the safety valves and are sized to prevent unnecessary actuation of the safety valves. The relief valves are self-actuating and discharge into the suppression pool through discharge piping connected to the valves. Each two-stage relief valve consists of a pilot assembly and main stage. The pilot assembly provides the pressure sensing function and the main stage provides the pressure relieving function. The relief valves are also part of the Automatic Depressurization System (ADS). As part of the ADS, the relief valves are designed to automatically actuate as a result of a depressurization permissive signal, and can also be manually actuated from the control room for depressurization.
Technical Specification (TS) 3.6.D.1 specifies that the nominal setpoint of the relief valves shall be selected between 1095 and 1115 psig and that all relief valves shall be set at this nominal set point ± 11 psi. The valves' nameplate setpoint is 1115 psig. Therefore, based on the tolerance limit of 11 psi (±1%), a maximum pressure of 1126 psig and a minimum pressure of 1104 psig are allowed. The established TS limit is stricter than the standard allowable relief valve setpoint drift range of ± 3% given in Section XI of the ASME Boiler and Pressure Vessel Code.
The main steam relief valves were manufactured by Target Rock Corporation, model #7567F.
Since the early 1980s, increased initial lift pressure (or upward setpoint drift) has been an industry concern applicable to the two—stage relief valves found in BWRs. Industry investigation of relief valve reliability problems revealed the primary cause of upward setpoint drift in the two-stage relief valves was corrosion bonding of the pilot valve disk to its seat. Three different design modifications were found to reduce or counteract the corrosion bounding: 1) installation of ion beam implanted platinum pilot valve disks, 2) the installation of Stellite-21 pilot valve disks, and 3) the installation of additional pressure actuation switches. PNPS implemented changes to install the Stellite-21 pilot valve disk design in the mid 1980 timeframe.
NRC review of upward setpoint drift is documented in NRC Regulatory Issue Summary 2000-12, Resolution of Generic Safety Issue B-55, "Improved Reliability of Target Rock Safety Relief Valves," and Generic Issue 165, "Spring Actuated Safety and Relief Valve Reliability." In the review, the NRC staff found that the industry has significantly improved valve performance and is continuing efforts to evaluate and improve performance, as necessary. Therefore, the staff found no new requirements were necessary and that existing quality assurance, maintenance rule, and code testing requirements were adequate to ensure reliable valve performance in the future.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) All four pilot assemblies for main steam relief valves RV-203-3A, 3B, 3C and 3D were removed during the May 2005 Refueling Outage (RFO-15). RV-203-3C had experienced steam leakage problems while installed during the operating cycle (Cycle 15) and was the subject of License Amendment No.
208 which was issued on December 23, 2004. This amendment allowed for continued operation with the steam leakage provided that certain conditions were satisfied.
EVENT DESCRIPTION
On May 11, 2005 Pilgrim Station was notified that three of four pilot valve assemblies previously installed had as-found popping pressures that exceeded the maximum TS tolerance limit of 1126 psig.
The as-found popping pressures were 1161 psig (serial number 1046), 1139 psig (serial number was 1124 psig. These test results were received when the plant was shutdown, during the 2005 refueling outage.
CAUSE
The probable cause of the as-found popping pressures exceeding the TS tolerance limit was setpoint drift resulting from corrosion bonding of the pilot valve disk to its seat. The corrosion bonding most likely occurred while the pilots were installed and in-service.
CORRECTIVE ACTION
The following corrective actions were taken. Four spare pilot valve assemblies were installed to replace the pilot valve assemblies that were removed during RFO-15. The spare pilot valve assemblies that were installed were tested and certified to be within 1% of the nominal set point required by technical specifications. New insulation was installed on the SRVs which may inhibit corrosion bonding of the seat and disk assembly while the valve is in-service.
The following corrective actions are planned. Engineering is working with industry representatives to evaluate actions and potential modifications to reduce or mitigate set-point drift.
These actions are within the scope of the corrective action program.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) � PILGRIM NUCLEAR POWER STATION 05000-293 2005 003 00 Loss of Coolant Accident (LOCA) — Fuel Peak Clad Temperature:
Following a small break LOCA and vessel isolation, reactor pressure will remain high and is controlled by cycling (opening and closing) relief valves. The small break analysis for Pilgrim Station assumes both HPCI and RCIC are unavailable. Core cooling is provided by the Automatic Depressurization System (ADS) in combination with low-pressure Core Standby Cooling Systems (CSCS). Until ADS initiation, the loss of inventory from the vessel is a function of break area and reactor pressure as controlled by cycling relief valves. After the initial discharge of stored energy from the reactor vessel to the suppression pool by multiple relief valves, a single relief valve is capable of removing decay heat.
Since the lowest as-found popping pressure of the four relief valve pilot assemblies was 1124 psig (serial number 1208), the analysis of record is bounding with respect to reactor pressure and inventory loss from the vessel prior to depressurization by ADS. Therefore, the existing LOCA analysis provides a bounding prediction of core uncovery time, fuel clad heatup, and peak clad temperatures.
Anticipated Transient Without Scram (ATWS):
Beginning in Cycle 15, the licensed thermal power level for PNPS was increased from 1998 MWth to 2028 MWth. Each of the four main steam relief valves was modified to increase the throat diameter, which provides a 7.5% increase in steam flow capacity per valve. During the licensing phase of the power uprate, a revised ATWS analysis was performed. These analyses resulted in a peak vessel pressure of 1495 psig. An evaluation of the as-found condition indicates that in the worst case, the peak vessel pressure resulting from the as-found popping pressures is estimated to be slightly greater than 1500 psig for approximately 30 seconds, well below the stress analysis limit of 1875 psig for faulted conditions (i.e., conditions associated with extremely low probability postulated events which may impair the integrity and operability of the nuclear system to the point where public safety is involved). It also should be noted that the estimated peak vessel pressure does not exceed the hydrostatic test pressure (125% of design pressure or 1560 psig) required by the ASME code to verify Reactor Coolant System integrity prior to initial plant startup. Therefore, given an ATWS event considering the as-found relief valve opening pressures, the estimated peak vessel pressure did not increase significantly and based on engineering judgment, system integrity would not have been impaired.
FACILITY NAME (1)� DOCKET NUMBER (2) I � LER NUMBER (6)� PAGE (3)
REPORTABILITY
This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B) because it was conservatively assumed that the as-found popping pressures could have been the pressures at which the relief valves would have operated if a high reactor pressure condition had occurred while the pilot assemblies were installed. The condition is assumed to have existed for a period greater than the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> limiting condition for operation specified in Technical Specification 3.6.D.2 for the relief valves.
SIMILARITY TO PREVIOUS EVENTS
A review was conducted of Pilgrim Station LERs. The review focused on LERs related to relief valve tests submitted since 2001. The review identified LER 2001-004-000, LER 2004-001-00 and LER 2004-03-00.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:
COMPONENTS� CODES Valve, Relief �
RV
SYSTEMS� CODES Main Steam� SB
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05000328/LER-2005-001 | Unit 2 Reactor Trip Following Closure of Main Feedwater Upon Inadvertent Opening of Control Breakers | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000388/LER-2005-001 | DDegradation of Primary Coolant Pressure Boundary due to Recirculation Pump Discharge Valve Bonnet Vent Connection Weld Flaw | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000423/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000455/LER-2005-001 | Unit 2 Automatic Reactor Trip Due to Low Steam Generator Level resulting from a Software Fault on the Turbine Control Power Runback Feature | | 05000370/LER-2005-001 | Automatic Actuation of Motor Driven Auxiliary Feedwater Pumps During Outage | | 05000244/LER-2005-001 | Failure of ADFCS Power Supplies Results in Plant Trip | | 05000247/LER-2005-001 | 0Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by an Inoperable Auxiliary Component Cooling Water Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000529/LER-2005-001 | REACTOR HEAD VENT AXIAL INDICATIONS CAUSED BY DEGRADED ALLOY 600 COMPONENT | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000336/LER-2005-001 | | | 05000266/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000269/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000289/LER-2005-001 | | | 05000293/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2005-001 | Reactor Scram due to Reactor Level Transient and Inadvertent Rendering of High Pressure Coolant Injection Inoperable | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000331/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000315/LER-2005-001 | Reactor Trip Following Intermediate Range High Flux Signal | | 05000316/LER-2005-001 | Reactor Trip from RCP Bus Undervoltage Signal Complicated by Diesel Generator Output Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000317/LER-2005-001 | Main Feedwater Isolation Valve Inoperability Due to Handswitch Wiring | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000323/LER-2005-001 | TS 3.4.10 Not Met During Pressurizer Safety Valve Surveillance Testing Due to Random Lift Spread | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000333/LER-2005-001 | Inoperable Offsite Circuit In Excess of Technical Specifications Allowed Out of Service Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2005-001 | Loss Of Licensed Material In The Form Of A Radiation Detector Calibration Source | | 05000353/LER-2005-001 | Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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