Similar Documents at Salem |
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LER-1978-073, Forwards LER 78-073/01X-1.Detailed Event Analysis Encl |
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f PS~G Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 Mr. Boyce H. Grier Director of USNRC March 25, 1981 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
Dear Mr. Grier:
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-73/0lX-l SUPPLEMENTAL REPORT Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting supple-mental Licensee Event Report for,Reportable Occurrence 78-73/0lX-l.
Sincerely yours,
/!1//1~/*
R. A. Uderit:z General Manager -
Nuclear Production CC:
Director, Office of Inspection and Enforcement (30 copies)
Director, Office of Management Information and Program Control (J)_l'L_G<::::>
( 3 copies)
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Report Date:
Occurrence Date:
Facility:
78-73/0lX-l March 25, 1981 11/27/78 Salem Generating Station -
Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Loss of lB Vital Instrument Bus CONDITIONS PRIOR TO OCCURRENCE:
Operational Mode 1, Reactor Power 100%
DESCRIPTION OF OCCURRENCE:
At 0445 hours0.00515 days <br />0.124 hours <br />7.357804e-4 weeks <br />1.693225e-4 months <br /> on November 27, 1978, loss of lB Vital Instrument Bus initiated a Reactor Coolant Loop Low Flow above PS reactor trip.
The Action Statement for Technical Specification 3.8.2.l was imple-mented.
Nos. 12 and 13 Auxiliary Feed Pumps did not start with low steam generator level.
No. 12 was manually started by the control room operator.
Recovery from the reactor trip was in prog-ress when a High Steam Flow -
Low Tave inadvertent safety injection occurred at 0502 hours0.00581 days <br />0.139 hours <br />8.300265e-4 weeks <br />1.91011e-4 months <br />.
The loss of lB Vital Instrument Bus resulted in inputs from each Stearn Generator Hi Stearn Flow logic to the Safety Injection logic.
During recovery from the trip, Tave decreased to less than 543°F causing the proper coincident logic for Safety Injection.
The safety injection was reset three minutes later.
The Safeguards Equipment Control System (SEC) was activated by the safety injection signal, however, lB Diesel, No. 11 Charging Pump and No. 12 RHR Pump failed to start.
The Action Statements for Technical Specifications 3.5.2 and 3.8.1.1.b were implemented.
No. 11 RHR Pump started from SEC and was secured after the safety injection.
An attempt was made to restart No. 11 RHR Pump at 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> but the breaker would not close.
Investigation of the bus failure showed that the inverter had failed and the bus was re-energized from the emergency supply solatron transformer.
The surveillance requirement for Technical Specification 3.8.1.1.2.a.2 was satisfactorily completed by 0756 hours0.00875 days <br />0.21 hours <br />0.00125 weeks <br />2.87658e-4 months <br /> and lB Diesel was declared operable at 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> upon completion of a one hour run.
Boration commenced at 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br /> to bring the RCS to Xenon free cold shutdown condition.
At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br />, the plant started cooldown and entered Hot Shutdown Mode 4 at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />.
RHR was initiated at 2240 hours0.0259 days <br />0.622 hours <br />0.0037 weeks <br />8.5232e-4 months <br /> and cooldown continued.
All Technical Specification Action Statements were terminated prior to reaching cold shutdown.
ECCS Actuation Report for Reportable Occurrence 78-74/990 was submitted on January 26, 1979, as required by Technical Specification 6.9.2.a.
March9s, 1981 LER 78-73/0lX-l 2 -
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The loss of lB Vital Instrument Bus was traced to the failure of the output transformer and two regulating resistors in the supply inverter.
The loss of the bus de-energized the "12 RCP Breaker Open" input relays to the Solid State Protection System.
This erroneous indication of a tripped RCP caused the low flow reactor trip logic to initiate the reactor trip.
The failure of lB Diesel, No. 11 Charging Pump and No. 12 RHR Pump to start with the initiation of safety injection is due to none of this equipment receiving an actuating signal from the lB SEC cabinet which was de-energized by the lB Vital Instrument Bus failure.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.8.2.1 for on-site power distribution systems requires 115 volt vital instrument buses and inverters operable for lA, lB and lC buses.
The Action Statement requires that with less than the above complement of AC buses operable, restore the inoperable bus to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least Hot Standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
The lB Vital Instrument Bus was re-energized from the emergency supply solatron transformer and the inverter was returned to service within 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br />.
The RCS was borated to Xenon free cold shutdown condition and entered Hot Shutdown 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> after the reactor trip.
Cooldown continued until all Technical Specification limiting conditions were terminated.
The failure of Noo lB Diesel, No. 11 Charging Pump and No. 12 RHR Pump to start at the time of safety injection is predictable under the circumstances and has been accounted for in the overall plant design of the safety systems.
The failure of No. 13 Auxiliary Feed Pump to start appears to be a random failure.
Operational testing has been done which shows the pump to be fully operational.
CORRECTIVE ACTION
The failed output transformer and regulating resistors in the lB Instrument Bus inverter were replaced and tests were run to verify operability.
The overspeed trip reset latch mechanism on No. 13 Auxiliary Feed Pump was readjusted to provide more positive latch operation.
No. 11 RHR Pump breaker was replaced and tested satisfactory.
No further corrective action is necessary.
FAILURE DATA:
Garrett Static Power Conditioning - Static Inverter -
Model Series 1 Transformer/Regulating Mode 5 kva Manufacturer:
Airesearch Manufacturing Company Prepared By W. J. Steele SORC Meeting No.
81-19
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| 05000272/LER-1978-022, Forwards LER 78-022/01T-0 | Forwards LER 78-022/01T-0 | | | 05000272/LER-1978-022-01, /01T-0 on 780404:Fischer & Porter 10B2496 Transmitters for Coolant Low Flow Monitoring Had High Output Deviation During Seismic Test.Caused by Vibration of Mounting Plate.Design Change Initiated | /01T-0 on 780404:Fischer & Porter 10B2496 Transmitters for Coolant Low Flow Monitoring Had High Output Deviation During Seismic Test.Caused by Vibration of Mounting Plate.Design Change Initiated | | | 05000272/LER-1978-029, Forwards LER 78-029/01X-1 | Forwards LER 78-029/01X-1 | | | 05000272/LER-1978-029-01, /01X-1 on 780610:during Training Startups,Two Power Range Channels Found Inoperable.Caused by Personnel Error in Which Wrong Leads Were Disconnected from Reactivity Computer.Procedures Revised | /01X-1 on 780610:during Training Startups,Two Power Range Channels Found Inoperable.Caused by Personnel Error in Which Wrong Leads Were Disconnected from Reactivity Computer.Procedures Revised | | | 05000272/LER-1978-035-03, /03L-0:on 780630,gas Starting Turbine Relay Operation Caused Loss of Power to Station Power Transformer. Caused by Personnel Error in Preparing Unit for Svc.Operator Reinstructed on Proper Breaker Operation | /03L-0:on 780630,gas Starting Turbine Relay Operation Caused Loss of Power to Station Power Transformer. Caused by Personnel Error in Preparing Unit for Svc.Operator Reinstructed on Proper Breaker Operation | | | 05000272/LER-1978-035, Forwards LER 78-035/03L-0 | Forwards LER 78-035/03L-0 | | | 05000272/LER-1978-043-03, /03L-0 on 780808:during Normal Oper,After 45% Pwr Reduction to Less than 50% for Maint,Reactor Pwr Increased to 51%.Deviation Alarm Would Not Clear & QPTR Was 1.03%.QPTR Was Not Discovered Sooner Because of Alarm Indications | /03L-0 on 780808:during Normal Oper,After 45% Pwr Reduction to Less than 50% for Maint,Reactor Pwr Increased to 51%.Deviation Alarm Would Not Clear & QPTR Was 1.03%.QPTR Was Not Discovered Sooner Because of Alarm Indications | | | 05000272/LER-1978-043, Forwards LER 78-043/03L-0 | Forwards LER 78-043/03L-0 | | | 05000272/LER-1978-046, :Number Not Used |
- Number Not Used
| | | 05000272/LER-1978-061, Forwards LER 78-061/01X-2 | Forwards LER 78-061/01X-2 | | | 05000272/LER-1978-061-01, /01X-2 on 780907:noted Defect in Protection Sys Which Could Allow Airborne Activity to Be Released to Outside Atmosphere.Caused by Design Deficiency.Design Change Installed in Protection Sys | /01X-2 on 780907:noted Defect in Protection Sys Which Could Allow Airborne Activity to Be Released to Outside Atmosphere.Caused by Design Deficiency.Design Change Installed in Protection Sys | | | 05000272/LER-1978-062, Forwards LER 78-062/03L | Forwards LER 78-062/03L | | | 05000272/LER-1978-062-03, /03L-0 on 780913:during Normal Oper the 12 Reactor Coolant Flow Channel 2 Was Not Indicating Due to Failure of a Hagan Controls Signal Isolator | /03L-0 on 780913:during Normal Oper the 12 Reactor Coolant Flow Channel 2 Was Not Indicating Due to Failure of a Hagan Controls Signal Isolator | | | 05000272/LER-1978-063-03, /03X-1 on 780910:containment Fan Cooling Unit 13 Inoperable. Caused by Flow Control Transmitter Failure Due to Silt Buildup in Low Pressure Sensing Line.Transmitter Cleaned & Sensing Line Blown Out | /03X-1 on 780910:containment Fan Cooling Unit 13 Inoperable. Caused by Flow Control Transmitter Failure Due to Silt Buildup in Low Pressure Sensing Line.Transmitter Cleaned & Sensing Line Blown Out | | | 05000272/LER-1978-063, Forwards LER 78-063/03X-1 | Forwards LER 78-063/03X-1 | | | 05000272/LER-1978-064-03, /03L-0 on 780912:reactor Trip Setpoint Greater than T/S Limit During Check of Pressure Protec Channel 2. Caused by Unstable Output from Comparator Feeding Trip Bistable.Comparator Replaced | /03L-0 on 780912:reactor Trip Setpoint Greater than T/S Limit During Check of Pressure Protec Channel 2. Caused by Unstable Output from Comparator Feeding Trip Bistable.Comparator Replaced | | | 05000272/LER-1978-064, Forwards LER 78-064/03L-0 | Forwards LER 78-064/03L-0 | | | 05000272/LER-1978-067, Forwards LER 78-067/03X-1 | Forwards LER 78-067/03X-1 | | | 05000272/LER-1978-067-03, /03X-1 on 780929:during Normal Operation,Resident NRC Inspector Noted Missing Fire Barrier in Cable Penetration.Caused by Failure of Administrative Controls. Penetration Immediately Sealed | /03X-1 on 780929:during Normal Operation,Resident NRC Inspector Noted Missing Fire Barrier in Cable Penetration.Caused by Failure of Administrative Controls. Penetration Immediately Sealed | | | 05000272/LER-1978-069-03, /03L-0:on 781011,while Investigating Diesel 1B Alarm,Heater Leaking Chromated Water Into pre-lube Pump Motor Discovered.Caused by Corrosion of Element Sheath in Two of Three Heater Elements | /03L-0:on 781011,while Investigating Diesel 1B Alarm,Heater Leaking Chromated Water Into pre-lube Pump Motor Discovered.Caused by Corrosion of Element Sheath in Two of Three Heater Elements | | | 05000272/LER-1978-069, Forwards LER 78-069/03L-0 | Forwards LER 78-069/03L-0 | | | 05000272/LER-1978-070, Supplemental LER 78-070/01X-1:on 781021,during Mode 4 Operation,While Heating Up to Enter Mode 3,high Flow Through RCP Seals & Other Alarms Indicating RCS Leakage Were Observed.Cause Undetermined.Instructions Have Been Revised | Supplemental LER 78-070/01X-1:on 781021,during Mode 4 Operation,While Heating Up to Enter Mode 3,high Flow Through RCP Seals & Other Alarms Indicating RCS Leakage Were Observed.Cause Undetermined.Instructions Have Been Revised | | | 05000272/LER-1978-070-01, /01T-0:on 781021,during Mode 4 Operation,While Heating Up to Enter Mode 3,high Flow Through RCP Seals Noted & Alarms Went Off Indicating RCS Leakage.Cause Unknown | /01T-0:on 781021,during Mode 4 Operation,While Heating Up to Enter Mode 3,high Flow Through RCP Seals Noted & Alarms Went Off Indicating RCS Leakage.Cause Unknown | | | 05000272/LER-1978-071, Forwards LER 78-071/01T-0 | Forwards LER 78-071/01T-0 | | | 05000272/LER-1978-071-01, /01T-0:on 781023:during Mode 5,fire Pumps 1 & 2 Put in Manual Due to Low Air Pressure Causing Actuation of air-operated Deluge Valves.Station Air Compressors Could Not Be Started Due to Low Cooling Water Flow | /01T-0:on 781023:during Mode 5,fire Pumps 1 & 2 Put in Manual Due to Low Air Pressure Causing Actuation of air-operated Deluge Valves.Station Air Compressors Could Not Be Started Due to Low Cooling Water Flow | | | 05000272/LER-1978-072-01, /01X-1:on 781107,svc Water Isolation Valves to All Five Containment Fan Coil Units Found Tripped Closed.Caused by Design Deficiency in Installation of RMS Detectors for Containment Fan Coil Unit Svc Water.Detectors Shielded | /01X-1:on 781107,svc Water Isolation Valves to All Five Containment Fan Coil Units Found Tripped Closed.Caused by Design Deficiency in Installation of RMS Detectors for Containment Fan Coil Unit Svc Water.Detectors Shielded | | | 05000272/LER-1978-072, Forwards LER 78-072/01X-1.Detailed Event Analysis Encl | Forwards LER 78-072/01X-1.Detailed Event Analysis Encl | | | 05000272/LER-1978-073, Forwards LER 78-073/01X-1.Detailed Event Analysis Encl | Forwards LER 78-073/01X-1.Detailed Event Analysis Encl | | | 05000272/LER-1978-073-01, /01X-1:on 781127,loss of Vital Instrument Bus 1B de-energized RCP Breaker Open Relay in Solid State Protection Sys,Initiating Reactor Trip.Caused by Failure of Output Transformer in Supply Inverter | /01X-1:on 781127,loss of Vital Instrument Bus 1B de-energized RCP Breaker Open Relay in Solid State Protection Sys,Initiating Reactor Trip.Caused by Failure of Output Transformer in Supply Inverter | | | 05000272/LER-1978-075, Supplemental LER 78-075/03X-1:on 781130,while Containment Entry in Progress,Inner Door of Air Lock Elevation 130 Ft Would Not Fully Open.Caused by Failed Cam Roller on Inner Door Operating Mechanism.Cam Roller Replaced | Supplemental LER 78-075/03X-1:on 781130,while Containment Entry in Progress,Inner Door of Air Lock Elevation 130 Ft Would Not Fully Open.Caused by Failed Cam Roller on Inner Door Operating Mechanism.Cam Roller Replaced | | | 05000272/LER-1978-075-03, /03L on 781130:during Oper W/Containment Entry in Progress,Inner Door of Air Lock 130 Would Not Fully Open, Caused by Failed Cam Roller on Inner Door Operating Mechanism.Air Lock Repaired,Tested,Returned to Svc | /03L on 781130:during Oper W/Containment Entry in Progress,Inner Door of Air Lock 130 Would Not Fully Open, Caused by Failed Cam Roller on Inner Door Operating Mechanism.Air Lock Repaired,Tested,Returned to Svc | | | 05000272/LER-1978-076, Forwards LER 78-076/03L-0 | Forwards LER 78-076/03L-0 | | | 05000272/LER-1978-076-03, /03L-0 on 781208:during Surveillance of Meteorological Instruments,Noted That Normal Power Had Failed & Inverter Had Not Shifted to Batteries.No Cause for Failure Discerned;Inverter Tested Satisfactorily | /03L-0 on 781208:during Surveillance of Meteorological Instruments,Noted That Normal Power Had Failed & Inverter Had Not Shifted to Batteries.No Cause for Failure Discerned;Inverter Tested Satisfactorily | | | 05000272/LER-1978-077-03, /03L-0 on 781128:pressurizer Level Read 10% Higher than Other Channels.Calibr of Sensor Showed Tech Spec Limit for Low Level Trip Was Exceeded by 2% Due to Failure of Strain Gauge in Pressurizer Level Sensor | /03L-0 on 781128:pressurizer Level Read 10% Higher than Other Channels.Calibr of Sensor Showed Tech Spec Limit for Low Level Trip Was Exceeded by 2% Due to Failure of Strain Gauge in Pressurizer Level Sensor | | | 05000272/LER-1978-077, Forwards LER 78-077/03L-0 | Forwards LER 78-077/03L-0 | | | 05000272/LER-1978-078-03, /03L-0 on 781130:channel Checks Showed Deviation Between Steam Flow Channels I & II of Steam Generator 13. Caused by Transmitter Zero Shift | /03L-0 on 781130:channel Checks Showed Deviation Between Steam Flow Channels I & II of Steam Generator 13. Caused by Transmitter Zero Shift | | | 05000272/LER-1978-078, Forwards LER 78-078/03L-0 | Forwards LER 78-078/03L-0 | | | 05000272/LER-1978-079, Forwards LER 78-079/03L-0 | Forwards LER 78-079/03L-0 | | | 05000272/LER-1978-079-03, /03L-0 on 781201:steam Generator 12,level Channel III Found to Be Inoperable;Channel Bistables Tripped Per Tech Specs.Caused by Partially Clogged Sensing Lines | /03L-0 on 781201:steam Generator 12,level Channel III Found to Be Inoperable;Channel Bistables Tripped Per Tech Specs.Caused by Partially Clogged Sensing Lines | | | 05000272/LER-1978-080, Forwards LER 78-080/03L-0 | Forwards LER 78-080/03L-0 | | | 05000272/LER-1978-080-03, /03L-0 on 781228:leak Rate Test Showed Excessive Seal Leakage & Air Lock Was Declared Inoperable.Caused by Failure of Outer Door Seal from Normal Wear of the Seal During Air Lock Operation | /03L-0 on 781228:leak Rate Test Showed Excessive Seal Leakage & Air Lock Was Declared Inoperable.Caused by Failure of Outer Door Seal from Normal Wear of the Seal During Air Lock Operation | | | 05000272/LER-1978-081-03, /03L-0 on 781206:noted That Sump Pump Magnetrol Was Overdue for Calibr.Caused by Incorrect Assignment of Responsibility for 18 Month Calibr Surveillance | /03L-0 on 781206:noted That Sump Pump Magnetrol Was Overdue for Calibr.Caused by Incorrect Assignment of Responsibility for 18 Month Calibr Surveillance | | | 05000272/LER-1978-081, Forwards LER 78-081/03L-0 | Forwards LER 78-081/03L-0 | | | 05000272/LER-1978-082-03, /03L-0 on 781228:zero Flow Was Indicated on Plant Vent Recorder Because of Frozen Condensation in Transmitter Sensing Lines.Caused by de-energized Temporary Heat Tracing | /03L-0 on 781228:zero Flow Was Indicated on Plant Vent Recorder Because of Frozen Condensation in Transmitter Sensing Lines.Caused by de-energized Temporary Heat Tracing | | | 05000272/LER-1978-082, Forwards LER 78-082/03L-0 | Forwards LER 78-082/03L-0 | | | 05000272/LER-1978-083, Forwards LER 78-083/03L-0 | Forwards LER 78-083/03L-0 | | | 05000272/LER-1978-083-03, /03L-0 on 781213:Number 13 Auxiliary Feed Pump Tripped on Overspeed Because Governor Operating Speed Was Set at 4200 Rpm.Governor Speed Reset & 3 Tests Confirmed Operability | /03L-0 on 781213:Number 13 Auxiliary Feed Pump Tripped on Overspeed Because Governor Operating Speed Was Set at 4200 Rpm.Governor Speed Reset & 3 Tests Confirmed Operability | | | 05000272/LER-1978-084-03, /03L-0 on 781127:boron Injection Tank Rendered Inoperable Due to Reduced Boron Concentration Resulting from Safety Injection | /03L-0 on 781127:boron Injection Tank Rendered Inoperable Due to Reduced Boron Concentration Resulting from Safety Injection | | | 05000272/LER-1978-084, Forwards LER 78-084/03L-0 | Forwards LER 78-084/03L-0 | | | 05000272/LER-1978-085-03, /03L-0 on 781211:svc Water Flow Through Fan Coil Unit Was Less than Required 2500 Gal Per Minute.Caused When Solenoid Control Coil Developed an Open Circuit | /03L-0 on 781211:svc Water Flow Through Fan Coil Unit Was Less than Required 2500 Gal Per Minute.Caused When Solenoid Control Coil Developed an Open Circuit | |
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