05000272/FIN-2014004-04
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Finding | |
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Title | Inadequate Interim Corrective Actions on Current Transformers Result in Reactor Trip |
Description | A Green, self-revealing finding against PSEG procedure LS-AA-120, Issue Identification and Screening Process, Revision 12, was identified for inadequate interim corrective actions when a Unit 1 main generator phase A differential current lockout relay tripped and resulted in a reactor trip on May 7, 2014. Specifically, interim corrective actions had not been properly implemented in response to a similar trip on April 13, 2014 for the same failure mechanism. PSEG conducted repairs, entered this matter in its corrective action program, and completed a root cause analysis. The issue was more than minor since it was associated with the equipment attribute of the initiating events cornerstone and adversely affected its objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, interim corrective actions did not adequately ensure the near-term reliability of transformer connections following an April 2014 failure, leaving the unit susceptible to a similar failure and a reactor trip in May 2014. In accordance with IMC 0609, Attachment 4 and Exhibit 1 of Appendix A, the inspectors determined that this finding is of very low safety significance, or Green, because the finding did not cause both a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. The finding was determined to have a cross-cutting aspect in Human Performance, Conservative Bias, in that individuals use decision-making practices that emphasize prudent choices over those that are simply allowable. That is, proposed actions are determined to be safe in order to proceed rather than unsafe in order to stop. Specifically, PSEG did not take a conservative approach to decisions regarding the scope of repairs given the unusual condition, did not consider the longer-term consequences when determining how to resolve the emergent CT concern, and did not take timely action to address the degraded condition commensurate with its significance, namely vulnerability to a further failure and a consequent reactor trip. |
Site: | Salem |
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Report | IR 05000272/2014004 Section 4OA3 |
Date counted | Sep 30, 2014 (2014Q3) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | A Patel A Ziedonis E Burket G Dentel J Schoppy P Finney R Barkley |
CCA | H.14, Conservative Bias |
INPO aspect | DM.2 |
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Finding - Salem - IR 05000272/2014004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Salem) @ 2014Q3
Self-Identified List (Salem)
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