At 1449 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.513445e-4 months <br /> on September 21, 2012, the Unit 2, 2B Drywell Radiation Monitor was found downscale during control room panel monitoring. This monitor provides the input into one division of the primary containment isolation logic for a Group 2 isolation. Troubleshooting indentified that this one of the two divisions of the isolation logic was inoperable.
As a result, the division was placed in a tripped condition at approximately 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br /> in accordance with Technical Specifications 3.3.6.1, Conditions A and B; and 3.3.3.1, Condition A.
The cause of the event was monitor failure due to dust and dirt inside the module which caused some of the sub- components to malfunction and result in a downscale indication.FInadequate periodic maintenance, in combination with the chassis ventilation design had allowed the components inside the chassis to be vulnerable to dust and dirt buildup since its installation.
Corrective actions included immediate replacement of the 2B Drywell Radiation monitor to return it to an operable condition.FFuture corrective actions include, detailed failure analysis by the vendor, and development of improved preventive maintenance activities on the monitor.
The safety significance of this event was minimal. Since both divisions of drywell radiation monitoring are required to complete the Group 2 isolation logic, but only one was available during this event, this report is submitted in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(C), and (a)(2)(v)(D), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: control the release of radioactive material, and mitigate the consequences of an accident. |
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor, 2957 Megawatts Thermal Rated Core Power Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
EVENT IDENTIFICATION
The 2B Drywell (DW) Radiation (Rad) Monitor Failed Downscale and resulted in one of the two divisions of the isolation logic becoming inoperable, for which both divisions are required for the Primary Containment Isolation (PCI) Group 2 isolation logic to complete its safety function.
A. CONDITION PRIOR TO EVENT
�Unit: 2 Event Date: September 21, 2012� Event Time: 1449 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.513445e-4 months <br /> � Reactor Mode: 1 Mode Name: Power Operation� Power Level: 100%
B. DESCRIPTION OF EVENT
At 1449 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.513445e-4 months <br /> on September 21, 2012, Operations found the 2B DW Rad Monitor reading downscale. The affected point history data was reviewed for trends. The 2B DW Rad monitor was previously trending between 2.2 and 2.5 Rads per Hour (R/Hr), and during this event, the monitor was indicating between 0.1 to 0.3 R/Hr. Operations inserted a Division II PCI 1/2 Group 2 Isolation at approximately 1515 hours0.0175 days <br />0.421 hours <br />0.0025 weeks <br />5.764575e-4 months <br /> to comply with Technical Specification (TS) 3.3.6.1, Primary Containment Isolation Instrumentation [JM], Conditions A and B since one required Drywell Radiation [NH] Monitor [RIS] division was inoperable. Operations also entered Technical Specification 3.3.3.1, Post-Accident Monitoring (PAM) Instrumentation [IP], Condition A since one required Drywell Radiation Monitor division was inoperable.
Troubleshooting performed on the 2B DW Rad Monitor chassis indentified the chassis had failed. The chassis was replaced with a bench calibrated spare chassis. TS 3.0.5 was entered for functional testing on the new chassis. By 1837 hours0.0213 days <br />0.51 hours <br />0.00304 weeks <br />6.989785e-4 months <br /> the chassis was satisfactorily tested without any issues. Operations then exited TS 3.0.5, TS 3.3.6.1 Conditions A and B, and TS 3.3.3.1, Condition A, and the 2B DW Rad Monitor was returned to operable status.
The safety significance of this event was minimal. Since both divisions of drywell radiation monitoring are required to complete the Group 2 isolation logic, but only one was available during this event, this report is submitted in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(C), and (a)(2)(v)(D), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: control the release of radioactive material, and mitigate the consequences of an accident.
C. CAUSE OF EVENT
The failed 2B DW Rad Monitor was sent to the vendor for failure analysis on September 28, 2012. The apparent cause of the monitor failure was determined to be dust and dirt inside the module which caused some of the sub components to malfunction and result in a downscale indication. Inadequate periodic maintenance, in combination with the chassis [IMOD] ventilation design, had allowed the components inside the chassis to be vulnerable to dust and dirt buildup since its installation. The preventive maintenance (PM) program did not require the chassis to be disassembled to facilitate internal components cleaning. This buildup of dust and dirt caused some of the monitor components to malfunction. The components that malfunctioned were powered by -24 Volts Direct Current, which feeds the trip logic. An additional detailed investigation will be performed by the vendor to determine the exact cause and circuit sub-components that failed.
D. SAFETY ANALYSIS
System Design The Containment Atmosphere Monitoring (CAM) System [IK] instrumentation provides the signals necessary to indicate and alarm high radiation levels in the drywell following a Loss of Coolant Accident (LOCA). At high radiation conditions in the drywell, the DW Rad Monitors initiate: (1) Primary Containment Group 2 isolation, (2) Reactor Building (RB) [NG] Ventilation (Vent) and Control Room [NA] Vent Isolations, and (3) an auto-start of the Standby Gas Treatment (SBGT) System [BH].
Drywell Radiation - High Function: High drywell radiation, as monitored by the DW Rad Monitors, indicates possible gross failure of the fuel cladding. Therefore, when Drywell Radiation - High is detected, an isolation is initiated to limit the release of fission products. However, as provided in the TS Bases 3.3.6.1, Function 2.c (Drywell Radiation - High), this Function is not assumed in any accident or transient analysis in the UFSAR because other leakage paths (e.g., MSIVs) are more limiting.
The Drywell Radiation - High Function receives input from two radiation detector assemblies [RT] (located in capped drywell penetrations) each connected to a switch [RIS] (Radiation Indicating Switch (RIS) 2-2419-A and RIS 2-2419- B). Each switch actuates two contacts. Each contact inputs to one of four trip strings. Two trip strings make up a trip system and both trip systems must trip to cause an isolation of the PCI valves. The contacts associated with the same switch provide input to both trip strings in the same trip system. Any contact will trip the associated trip string.
The trip strings are arranged in a one-out-of-two taken twice logic. As used in TS Table 3.3.6.1-1, Function 2.c, Drywell Radiation High, a channel is considered to include a radiation detector assembly, a switch, and one of two contacts. Under this design, two divisions of Drywell Radiation - High Function are available, and are required to be operable to complete the PCI logic for a Group 2 isolation from DW radiation monitoring.
The PCI function is initiated based on the specific plant accident conditions that have been sensed. The actions in Group 2 are initiated on sensing any one of the following conditions, per TS Table 3.3.6.1-1:
- reactor low water level (>1= 3.8") (Level Transmitters [LT] 2-263-57A/B and 2-263-58A/B);
- high drywell pressure (4= 2.43 psig) (Pressure Switches [PS] 2-1621-A to D); and
- high drywell radiation ( The signals for Group 2 primarily provide for isolation of the containment drywell/torus [NH] atmosphere and include isolation valves for:
- drywell vent, purge, and sump isolation [VB];
- drywell pneumatic supply;
- drywell air sampling (oxygen analyzer valves);
- traversing in-core probe (TIP) [IG] withdrawal and isolation; and
- reactor building main vent isolation [VA].
In addition to providing isolation, the Group 2 signal initiates other actions designed to limit radioactive releases, e.g., the Group 2 isolation signal automatically starts the SBGT system, and trips the Reactor Building floor drain and equipment drain pumps.
Safety Impact Since the 2B DW Rad Monitor was inoperable, this one of the two divisions of the isolation logic was unavailable, whereas, both divisions are required for the PCI Group 2 isolation logic to complete its safety function. Each DW Rad Monitor (2A and 2B) is designed such that a downscale failure mode does not result in an automatic conservative/tripped condition to its associated two channels; rather the chassis provides no automatic channel actuation functions when downscale. Therefore the safety function for Group 2 isolation from DW radiation monitoring was not met during the 2B DW Rad Monitor downscale event.
The 2B DW Rad Monitor had failed downscale for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. During this period, a high drywell radiation condition would not have initiated a Group 2 isolation, however, a Group 2 isolation remained available from reactor water low level, or high drywell pressure signals.
Although a loss of PCI Group 2 isolation function occurred for this brief period .when the 2B DW Rad Monitor failed, this condition did not create any actual plant or safety consequences since the Unit was not in an accident or transient condition requiring use of DW Rad Monitors during this period of time.
Risk Insights The plant Probabilistic Risk Assessment (PRA) model credits the drywell rad monitors, hence the as-found conditions contributed to an increase in risk. Since the 2B DW Rad Monitor had failed downscale for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, during this period, a high drywell radiation condition would not have initiated a Group 2 isolation for valves that are modeled in the PRA model, however, all of these valves are normally closed, except for one valve, 2-1699-7 (Air Operated Unit 2 Vent to Reactor Building), which is normally open.
As such, the risk contribution was calculated as follows: the effect on change in Core Damage Frequency (CDF) is:
1.27E-09/yr, which is insignificant; the effect on change in Large Early Release Frequency (LERF) is: 4.03E-10/yr, which is also insignificant.
In conclusion, the overall safety significance and impact on risk of this event were minimal.
E. CORRECTIVE ACTIONS
Immediate:
1. Replaced the 2B DW Rad Monitor with a new drywell radiation monitor to restore function.
Follow-up:
1. Vendor to perform detailed failure analysis on the failed 2B DW Rad Monitor to determine which circuit subcomponent had failed.
2. Add a PM procedure to clean the DW Rad Monitors on an increased frequency.
3. Develop a PM to Replace/Refurbish the DW Rad Monitors.
F. PREVIOUS OCCURRENCES
The Station Events Database, LERs, and ICES were reviewed for similar events at Quad Cities Nuclear Power Station. This event was a downscale failure of a DW Rad Monitor caused by inadequate periodic maintenance, in combination with the chassis ventilation design which allowed the components inside the chassis to be vulnerable to dust and dirt buildup since installation. Similar events observed are below, however, there were no previous events identified that would have prevented this event.
1. Station Events Database, Issue Report (IR) 868559: On 01/19/09, a lowering trend on the 2B DW Rad Monitor was observed. The 2B DW Rad Monitor was previously trending between 2.2 and 2.4 R/Hr, and during this event the monitor indicated between 1.5-1.9 R/Hr. Bench testing was performed on the failed chassis/power supply and no performance issues were found. No clear cause was found for the failure of the 2B DW Rad Monitor. The 2B DW Rad Monitor chassis was replaced. A dust related cause for failure was possible, but the exact failure mode could not be identified. The issue did not reoccur during troubleshooting.
2. Station Events Database, IR 900795: On 3/31/09, the 1B DW Rad Monitor was observed to be trending downscale. The cause of this event was determined to be an internal cable degradation, or cable connection issue that caused the intermittent spurious downscale indications. This failure was specific to the cable involved and did not appear to be related to a dust buildup in the chassis.
G. COMPONENT FAILURE DATA
Drywell Radiation Monitor Radiation Indicating Switch (RIS) 2-2419-B:
Component Manufacturer: General Atomics/Sorrento Component Model Number: RP-2CM Component Part Number: RP-2CM, Range - 1 to 108 R/hr.
This event has been reported to ICES as Failure Report No. 300720.
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05000413/LER-2012-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2012-001 | Unanalyzed Condition Affecting Essential Raw Cooling Water System due to External Flooding | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000388/LER-2012-001 | Two Control Room Floor Cooling Systems Inoperable | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000395/LER-2012-001 | Vice President, Nuclear Operations 803.345.4342 August 3, 2012SCE~r .so A SCANA COMPANY Document Control Desk U. S. Nuclear Regulatory Commission
Washington, DC 20555
Dear Sir / Madam: Subject:VVIRGIL C. SUMMER NUCLEAR STATION (VCSNS) UNIT 1 DOCKET NO. 50-395 OPERATING LICENSE NO. NPF-12 LICENSEE EVENT REPORT (LER 2012-001-01) CORE EXIT THERMOCOUPLES & REACTOR WATER LEVEL INDICATION SYSTEM INOPERABLE DUE TO AN INADEQUATE MAINTENANCE PROCEDURE Attached is Licensee Event Report (LER) No. 2012-001-01 for the Virgil C. Summer Nuclear Station Unit 1. This revised report describes a condition where Core Exit Thermocouples and Reactor Water Level Indication System would not be operable for accident monitoring. This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B). This letter and attached LER contain no new commitments and no revisions to existing
commitments.
Should you have any questions, please call Bruce Thompson at (803) 931-5042. Very truly yours, Dal Thomas D. Gatlin TS/TDG/jw
Attachment
c: K. B. Marsh P. Ledbetter S. A. Byrne J. C. Mellette J. B. Archie EPIX Coordinator N. S. Carps K. M. Sutton J. H. Hamilton INPO Records Center R. J. White Marsh USA, Inc. W. M. Cherry R. J. Schwartz V. M. McCree NSRC R. E. Martin RTS (CR-11-01807) NRC Resident Inspector FileV(818.07) M. N. Browne PRSF (RC-12-0116) V fALVirgil C. Summer Station • Post Office Box 88 .Jenkinsville, SC • 29065 • F (803) 345-5209 1 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours.0Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocollects.resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management andLICENSEE EVENT REPORT (LER) Budget, Washington, DC 20503. If a means used to impose an information(See reverse for required number of collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, thedigits/characters for each block) information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Virgil C. Summer Nuclear Station Unit 1 05000 395 1 OF 5 4. TITLE Core Exit Thermocouples & Reactor Water Level Indication System Inoperable due to Inadequate Maintenance Procedure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000397/LER-2012-001 | DG-3 Inoperable for Longer than Allowed by TS Due to Failed Governor 05000 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-001 | Forced Shutdown Due to an Increase in Drywell Leakage in Excess of Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000289/LER-2012-001 | Single Condition Making Independent Trains Inoperable | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000286/LER-2012-001 | Common Cause Inoperability of Both Trains of Motor Driven Auxiliary Feedwater (AFW) Pumps Due to Inability to Control AFW Regulating Valves After Isolation of Nitrogen Backup | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000265/LER-2012-001 | Main Steam Isolation Valve Local Leak Rate Test Exceeds Technical Specifications Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000456/LER-2012-001 | Two Main Steam Safety Valves Failed Pre-outage Setpoint Testing Due to Abnormal Spring Geometry | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-001 | Technical Specification Required Plant Shutdown Due to Missed Surveillance and Operation Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000483/LER-2012-001 | Modification Implementation Error Adversely Impacted the Containment Cooling System | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2012-001 | Containment Concrete Thickness At Spalled Patch Does Not Meet Technical Specification Design Value | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000414/LER-2012-001 | Carolinas Duke Energy Carolinas, LLC 4800 Concord Rd. York, SC 29745 803-701-4251 December 20, 2012 U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
Subject:�Duke Energy Carolinas, LLC (Duke Energy)
Catawba Nuclear Station, Units 1 and 2
Docket Nos. 50-413 and 50-414
Licensee Event Report 414/2012-001
Pursuant to 10 CFR 50.73(a)(1) and (d), attached is Licensee Event Report 414/2012-001,
Revision 0 entitled, "Diesel Generator (DG) 2B Was Unknowingly inoperable from 09/28/12 to
10/23/12 Due to Failed Tachometer Relay Power Supply".
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B), 10 CFR
50.73(a)(2)(ii)(B), and 10 CFR 50.73(a)(2)(v)(A)-(D).
There are no regulatory commitments contained in this letter or its attachment. This event is considered to be of no significance with respect to the health and safety of the
public.
If there are any questions on this report, please contact L.J. Rudy at (803) 701-3084. Kelvin Henderson LJR/s Attachment www. duke-energy. corn Document Control Desk Page 2 December 20, 2012 xc (with attachment): V.M. McCree Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, GA 30303-1257 J.H. Thompson (addressee only) NRC Project Manager U.S. Nuclear Regulatory Commission Mail Stop 8-G9A 11555 Rockville Pike Rockville, MD 20852-2738 G.A. Hutto, III NRC Senior Resident Inspector Catawba Nuclear Station INPO Records Center 700 Galleria Place Atlanta, GA 30339-5957 Document Control Desk Page 3 December 20, 2012 bxc (electronic copy)(with attachment): INPO L.E. Harmon C.S. Kamilaris R.D. Hart G.Y. Helton S.F. Hatley (ICES) M.K. Green R.T. Simril, Jr. B.C. Carroll M.C. Nolan W.J. Pritchett, Jr. T.L. Patterson K.R. Alter H.D. Brewer R.E. Abbott, Jr. B.J. Horsley S.L. Western bxc (hard copy)(with attachment): D.B. Alexander L.S. Nichols L.J. Rudy ELL Master File CN-801.01 LER File RGC Date File NCMPA-1 NCEMC PMPA ICES Lee.Harmon@NRC.gov NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013
(10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported
lessons learned are incorporated into the licensing process and fed back to industry. Send commentsLICENSEE EVENT REPORT (LER) regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.resource@nrclov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used(See reverse for required number of to impose an information collection does not display a currently valid OMB control number, the NRCdigits/characters for each block) may not conduct or sponsor, and a person is not required to respond to, the information collection. r1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 05000414 10OF •4. TITLE Diesel Generator (DG) 2B Was Unknowingly Inoperable from 09/28/12 to 10/23/12 Due to Failed Tachometer
Relay Power Supply | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii) | 05000247/LER-2012-001 | Technical Specification (TS) Prohibited Condition Caused by an Inoperable 23 Emergency Diesel Generator Fuel Oil Storage Tank Due to Fuel Oil Below TS Limit | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2012-001 | Unanalyzed Conditions Exist for Standby Shutdown Facility Mitizated Events | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000445/LER-2012-002 | COMANCHE PEAK 05000445 10OF06 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000413/LER-2012-002 | Discovery of Inadequacy in Surveillance Testing of Solid State Protection System | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-002 | Unplanned LCO 3.5.4 Entry Due to RWST alignment to Purification | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-002 | Loss of Isolation Function on RHR Shutdown Cooling Suction Line due to Breaker Trip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000482/LER-2012-002 | . One Train of Automatic Safety Infection Blocked During Entry Into Mode 3 Due To Procedural Weakness | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2012-002 | Emergency Diesel Generator Vibration Trip Not Bypassed For Non-Accident Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000346/LER-2012-002 | Leak from Reactor Coolant Pump Seal Piping Socket Weld due to High Cycle Fatigue | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000333/LER-2012-002 | High Pressure Coolant Injection Pressure Control Valve Failure | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2012-002 | Unit 2 Emergency Diesel Generators Inoperable Due To Missing Flood Control Barrier Seal | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System | 05000250/LER-2012-002 | Non-compliance with TS 3.4.9.3 due to Manual Isolation Valve Found in Incorrect TS Configuration | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000278/LER-2012-002 | Failure of Primary Containment Isolation Valve due to Foreign Material Results in Condition Prohibited by TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2012-002 | Unit 2 Reactor Trip from Generator Trip Due to Incorrect Relay Setting | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000282/LER-2012-002 | Unplanned Actuation of 121 Motor Driven Cooling Water Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-002 | Improper Rotor Installation Causes Failure of Diesel Generator to Start | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2012-002 | Technical Specification (TS) Prohibited Condition Caused by New Fuel Assemblies Stored in a Configuration Prohibited by the TS | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2012-002 | Inlet Steam Drain Pot Drain Line Leaks Result in HPCI Inoperabilities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2012-003 | Reactor Building Doors Opened Simultaneously Causes Loss of Safety Function | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000410/LER-2012-003 | Suppression Pool Level Below Technical Specification Limit During Mode Change | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2012-003 | Plant Modification Interfered with the Operation of Containment Wide Range Level Indicator | | 05000298/LER-2012-004 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000410/LER-2012-004 | Manual Reactor Scram due to a Loss of Main Turbine Gland Sealing Steam Resulting in Lowering Condenser Vacuum | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2012-004 | Essential Chiller Oil Leak Creates Unanalyzed Past Operability Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000265/LER-2012-004 | Drywell Radiation Monitor Failed Downscale | | 05000261/LER-2012-004 | Reactor Tripped Due to a Turbine Trip Caused by a Feedwater Isolation Signal from Steam Generator 'B' High Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000454/LER-2012-004 | Reactor Pressure Vessel Head Control Rod Drive Mechanism Penetration Nozzle Weld Repair Surface Indications | | 05000254/LER-2012-004 | Breech in Secondary Containment | | 05000482/LER-2012-004 | Two Charging Pumps Capable of Injecting into the RCS Due to Inadequate Definition of Centrifugal Charging Pump in LCO 3.4.12 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000410/LER-2012-005 | Automatic Diesel Actuation Due to the Loss of a 115 kV Offsite Power Source | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000298/LER-2012-005 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000298/LER-2012-006 | Missing Vent Plug Results in Technical Specifications Prohibited Condition | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000220/LER-2012-007 | High Pressure Coolant Injection System Logic Actuation Following an Automatic Turbine Trip Signal Due to High Reactor Water Level | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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