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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5679716 October 2023 02:56:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Due to Fire Not Verified to Be Extinguished within 15 Minutes

The following information was provided by the licensee: At 2256 EDT on October 15, 2023, Brunswick declared a Notification of Unusual Event due to a fire not extinguished within 15 minutes. The licensee received fire alarms and indication of a halon discharge in the basement of the emergency diesel generator building. Due to the delay in the entry into the area, the licensee was not able to verify that the fire was out within 15 minutes. Upon entry into the room, the licensee noted an acrid odor near a transformer, but there was not a fire in the room. The fire was declared out at 2310 EDT. The licensee notified the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE AT 0047 EDT ON 10/16/2023 FROM JOSEPH STRNAD TO BILL GOTT * * *

The following information was provided by the licensee via email: Termination of Unusual Event due to verification of no fire in the basement of the emergency diesel generator building." The licensee terminated the Unusual Event at 0045 on 10/16/23. The licensee notified the NRC Resident Inspector. Notified R2DO (Miller), IR-MOC (Grant), NRR-EO (Felts), DHS-SWO, FEMA Ops Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

Emergency Diesel Generator
ENS 548124 August 2020 03:12:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to a Loss of Offsite Power

At 2312 EDT, on August 3, 2020, Brunswick Unit 1 declared an Unusual Event due to a loss of offsite power. The unit was at approximately 20 percent power and was not synced to the grid when the unit automatically scrammed. All control rods fully inserted. Emergency Diesel Generators started and began powering the safety buses. Safety systems actuated as expected. The Unit also experienced a loss of Fuel Pool Cooling and Cleanup System, but one pump was returned to service. Unit 2 remains at 100 percent power and is unaffected. The licensee notified State and local governments, as well as the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, CISA IOCC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE FROM MARK TURKAL TO DONALD NORWOOD AT 0120 EDT ON 8/4/2020 * * *

At approximately 2302 EDT, a loss of offsite power occurred on Unit 1. This resulted in a Reactor Protection System (RPS) actuation. Per design, emergency diesel generators 1 and 2 properly started and loaded to their respective emergency buses. The Reactor Core Isolation Cooling (RCIC) system was manually started and is being used to control reactor water level. The High Pressure Coolant Injection (HPCI) system was manually started and is being used for pressure control. As previously reported, an Unusual Event was declared at 2312 EDT due to the loss of offsite power. At the time of the event, Unit 1 was in the process of shutting down for maintenance associated with a ground on the main generator. Due to the RPS actuation while critical, this event is being reported as a four-hour, nonemergency notification per 10 CFR 50.72(b)(2)(iv)(B). As a result of the reactor trip, reactor water level reached low level 1 (LL1). The LL1 signal causes a Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sample isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Per design, the loss of offsite power also caused a Group 1 (i.e., main steam isolation valve) isolations. Due to the Emergency Diesel Generator and Primary Containment Isolation System (PCIS) actuations, this event is also being reported as an eight-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 was not affected. There was no impact to the health and safety of the public or plant personnel. The safety significance of the event is minimal. All safety related systems operated as designed. Investigation of the cause of the loss of offsite power is in progress. The licensee notified the NRC Resident Inspector. Notified R2DO (Inverso).

  • * * UPDATE ON 8/4/2020 AT 1534 EDT FROM JOSEPH ELKINS TO ANDREW WAUGH * * *

At 1454 EDT on August 4, 2020, the Unusual Event was exited when offsite power was restored to Unit 1. Per design, when the loss of offsite power to Unit 1 occurred, all four emergency diesel generators (EDGs) started and EDGs 1 and 2 properly suppled emergency buses 1 and 2. Since Unit 2 was not affected by the loss of power, EDGs 3 and 4 ran unloaded. With restoration of offsite power to Unit 1, EDG 2 has been secured. EDGs 1, 3, and 4 are being secured as required by plant operating procedure. Notified R2DO (Inverso), NRR EO (Miller), IRD MOC (Grant), DHS SWO, FEMA OC, DHS NICC WO, CISA IOCC (email), DHS SWO (email), FEMA NWC (email), FEMA Ops Center (email), FEMA-NRCC-sasc (email), NRCC THD Desk (email), NuclearSSA (email). ********************************************************************************************************************************

High Pressure Coolant Injection
Reactor Protection System
Emergency Diesel Generator
Main Steam Isolation Valve
Primary Containment Isolation System
Reactor Core Isolation Cooling
Shutdown Cooling
Fuel Pool Cooling and Cleanup
Control Rod
ENS 5460324 March 2020 16:05:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification-Required Shutdown Due to Unidentified LeakageAt 1205 Eastern Daylight Time (EDT) on March 24, 2020, a Technical Specification-required shutdown was initiated on Unit 1 due to indication of a leak in the drywell. Technical Specification Action 3.4.4.A, Unidentified Reactor Coolant System (RCS) leakage increase not within limit, requires RCS leakage to be reduced to within limits within 8 hours. It was expected that the leakage would not have been reduced to within limits within the required Technical Specification completion time; therefore, this event is being reported in accordance with 10 CFR 50.72(b)(2)(i). Reactor water level reached low level 1 (LL1) following the reactor shutdown. The LL1 signal causes Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves), and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the valid Primary Containment Isolation System (PCIS) actuation, this event is also being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 is not affected by this event. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.Reactor Coolant System
Primary Containment Isolation System
Shutdown Cooling
ENS 540527 May 2019 02:04:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNoue Due to Fire Lasting Longer than 15 Minutes in Turbine Building

At 2204 EDT on 5/6/19, a Notification of Unusual Event (NOUE) was declared due to a fire lasting greater than 15 minutes. The fire occurred in the '2B' Heater Drain Pump motor located in the turbine building. The fire was extinguished following initial Emergency Declaration. There were no releases to the environment. Unit 1 was unaffected by the event and remains in Mode 1 at 100 percent power. The licensee notified the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 5/7/19 AT 0002 EDT FROM MICHAEL BRADEN TO BETHANY CECERE * * *

The NOUE was terminated as of 2359 EDT on 5/6/19. No off-site resources were required to extinguish the fire. The turbine building is now free of smoke. The licensee will notify the NRC Resident Inspector, State of North Carolina, Brunswick County, New Hanover County, and the Coast Guard. Notified R2DO (Heisserer), NRR EO (Miller), and IRD (Gott). Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

ENS 5396128 March 2019 18:50:0010 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Unusual Event Declared Due to Rcs Unidentified Leakage

At 1450 EDT on March 28, 2019, the licensee observed that the Unit 1 unidentified Reactor Coolant System (RCS) leakage was greater than 10 gallons per minute (gpm) for greater than or equal to 15 minutes. The licensee declared an Unusual Event in accordance with their EAL SU 5.1. The licensee initiated a unit shutdown in accordance with their procedures and the unit was approximately 58 percent reactor power at 1507 EDT, with unit shutdown in progress. The licensee also received an alarm due to increasing Drywell Pressure at 1.7 pounds drywell pressure. At 1600 EDT the licensee called with an update. Unit 1 was still in an Unusual Event with the unit at 37 percent power with the shutdown continuing. Drywell Pressure had decreased to 0.8 pounds. At 1603 the licensee scrammed Unit 1. Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 3/28/2019 AT 1808 EDT FROM MARK TURKAL TO THOMAS KENDZIA * * *

At 1437 EDT on March 28, 2019, with Unit 1 in Mode 1 at approximately 100 percent power, a Technical Specification-required shutdown was initiated due to indication of a leak in the drywell. Technical Specification Action 3.4.4.A, Unidentified Reactor Coolant System (RCS) leakage increase not within limit, requires RCS leakage to be reduced to within limits within 8 hours. It is expected that the leakage would not have been reduced to within limits within the required Technical Specification completion time; therefore, this event is being reported in accordance with 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 03/29/19 AT 0302 EDT FROM TOM FIENO TO BETHANY CECERE * * *

At 0259 EDT on March 29, 2019, the Unusual Event was terminated because RCS leakage was reduced to less than 10 gallons per minute. The most recent leakage rate measured at 0225 EDT was 3.9 gpm. The source of the leak will be identified when plant conditions allow containment entry. No elevated radiation levels were observed during this event. Drywell pressure is currently 0.0 psig. Unit 1 is in Mode 4. The licensee notified the NRC Resident Inspector. Notified R2DO (Bonser), NRR EO (Miller), IRD MOC (Grant), DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

Reactor Coolant System
ENS 5360915 September 2018 04:00:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationEn Revision Imported Date 9/19/2018

EN Revision Text: UNUSUAL EVENT DUE TO SITE CONDITIONS PREVENTING PLANT ACCESS A hazardous event has resulted in on site conditions sufficient to prohibit the plant staff from accessing the site via personal vehicles due to flooding of local roads by Tropical Storm Florence. Notified DHS SWO, FEMA OPS, and DHS NICC. Notified FEMA NWC, NuclearSSA, and FEMA NRCC via email.

  • * * UPDATE FROM BRUCE HARTSCOK TO VINCE KLCO ON 9/28/2018 AT 1414 EDT * * *

On 9/18/2018 at 1400 EDT, the Unusual Event at Brunswick was terminated due to the ability to transport personnel to the site. The licensee will notify the NRC Resident Inspectors. Notified the R2DO (Guthrie), NRR EO (Miller) and the IRD MOC (Grant). Notified DHS SWO, FEMA OPS, and DHS NICC. Notified FEMA NWC, NuclearSSA, and FEMA NRCC via email.

ENS 5208213 July 2016 00:39:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationAlert Declared for a Fire in the Service Water Building

At approximately 2039 EDT, there was smoke in the Service Water Building with the trip of the 2C service water pump. In accordance with plant procedures, unit-2 was ramped down to 70 percent power and the "Alert" was declared. EAL (emergency action level) SA8.1 was entered for damage with degraded performance including visible damage to the service water pump. Service water pressure was eventually restored by running both the 2A and 2B service water pumps. At 2118 EDT, the site exited the "Alert" because service water pressure had been restored. The licensee notified the NRC Resident Inspector. Notified DHS SWO, FEMA Ops Center, USDA Ops Center, HHS Ops Center, DOE Ops Center, DHS NICC Watch Officer, EPA EOC, FEMA National Watch Center (email), FDA EOC (email), Nuclear SSA (email).

  • * * UPDATE ON 7/14/16 AT 1456 EDT FROM LEE GRZECK TO DONG PARK * * *

The initial notification should read: At approximately 2035 EDT, there was smoke in the Service Water Building with the trip of the 2C conventional service water pump. In accordance with plant procedures, unit-2 was ramped down to 70 percent power and the 'Alert' was declared at 2039 EDT. EAL (emergency action level) SA8.1 was entered for fire/smoke damage with degraded performance including visible damage to the service water pump. Service water pressure was eventually restored and the plant was stabilized. At 2118 EDT, the site exited the 'Alert' when service water pressure had been restored, and the fire was confirmed out (i.e., no reflash within 30 minutes). The licensee notified the NRC Resident Inspector. Notified R2DO (Rich).

Service water
ENS 517157 February 2016 18:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Scram and Alert Declaration Due to Electrical Fault Resulting in Fire/Explosion

At 1346 EST the licensee reported that at 1326, Brunswick Unit 1 declared an Alert under EAL HA 2.1 due to an explosion/fire in the Balance of Plant 4 kV switchgear bus area. Prior to the Alert declaration, the operators initiated a manual SCRAM due to an unexpected power decrease from 88% to 40%. The licensee has visually verified that there is no ongoing fire and is investigating the initial cause of the event. Offsite power is available to the site, but EDGs 1 and 2 are running and supplying Unit 1 loads. The MSIVs shut and HPCI/RCIC are being used to maintain vessel level. At 1412 EST, NRC decided to remain in Normal Mode. At 1704 EST the licensee reported the following: At 1313 hours Eastern Standard Time (EST) a manual reactor scram was initiated due to loss of both recirculation system variable speed drives as a result of an electrical fault. At this time, a Startup Auxiliary Transformer (SAT) experienced a lockout fault; interrupting offsite power to emergency buses 1 and 2. Emergency Diesel Generators (EDGs) 1, 2, 3, and 4 automatically started and EDGs 1 and 2 synchronized to emergency buses 1 and 2 per design. The power interruption resulted in closure of the Main Steam Isolation Valves, per design. The manual scram also resulted in closure of Group 2, 6, and 6 Containment Isolation Valves. The Reactor Core Isolation Cooling (RCIC) system was manually started and is being used to control reactor water level. The High Pressure Coolant Injection (HPCI) system was manually started and is being used for pressure control. The Plant response to the event was per design. Unit 2 is not directly affected by the event, however, due to the shared electrical distribution system is in a Technical Specification Action statement due to the Inoperable Unit 1 SAT. The public health and safety is not impacted by this event. At 1751 EST, the licensee reported that the emergency declaration had been downgraded to an Unusual Event at 1730 because the plant no longer meets the criteria for an Alert, but does meet the criteria for an Unusual Event due to a "loss of all offsite power to Emergency 4 kV buses E1 (E3) and E2 (E4) for greater than or equal to 15 minutes." The NRC Resident Inspector has been notified. The licensee has notified the State and Local governments. Notified DHS, FEMA, USDA, HHS, DOE, DHS NICC, EPA EOC, FEMA NWC (via email), FDA EOC (via email) and Nuclear SSA (via email).

  • * * UPDATE FROM MARTY IRWIN TO DANIEL MILLS AT 1825 ON 2/07/16 * * *

At 1814 EST the emergency declaration was terminated because offsite power was restored. The NRC Resident Inspector has been notified. The licensee has notified the State and Local governments. Notified R2DO (Musser), NRR EO (Morris), IRD MOC (Stapleton), R2RA (Haney), NRR ET (Lubinski), NRR ET (Dean), DHS, FEMA, USDA, HHS, DOE, DHS NICC, EPA EOC, FEMA NWC (via email), FDA EOC (via email) and Nuclear SSA (via email).

High Pressure Coolant Injection
Emergency Diesel Generator
Main Steam Isolation Valve
Reactor Core Isolation Cooling
05000325/LER-2016-001
ENS 5075122 January 2015 23:13:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNotification of Unusual Event Declared Due to Toxic Gas in the Security Diesel Building

At 1801 EST, the control room received multiple fire alarms in the control room. At 1803, site security notified the control room of the presence of smoke in the security diesel building. At 1813, the licensee declared a Notification of Unusual Event due to the presence of toxic gas in the security diesel building on the battery/UPS side of the building. The fire suppression (NOVEC) system had discharged. Both the Technical Support Center and the Operations Support Center were fully manned. The site fire brigade made entry into the building and saw no evidence of fire but they did see and smell an acrid odor from an apparent electrical fire as well as the presence of the NOVEC fire suppressant. Offsite assistance was requested but not required to mitigate the event. Investigation of the cause of the toxic gas is under investigation. At this time, no security equipment is affected. Both the Technical Support Center and the Operations Support Center were fully manned. The licensee notified the State of North Carolina, New Hanover and Brunswick counties, and the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).

  • * * UPDATE FROM BRUCE HARTSOCK TO MARK ABRAMOVITZ AT 1936 EST ON 1/22/15 * * *

At time 1923 EST, the Notification of Unusual Event was terminated after normal access to the security diesel building was restored. The cause of the event is under investigation. The licensee notified the State of North Carolina, New Hanover and Brunswick counties, and the NRC Resident Inspector. Notified R2DO (McCoy), IRD (Stapleton), NRR (Evans), DHS SWO, FEMA Operations Center, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).

ENS 5035512 August 2014 08:32:0010 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Unusual Event for a Halon Release Near the Tsc and Eof

The licensee declared an Unusual Event because of a halon discharge in the simulator. This potentially affects access and habitability of the Technical Support Center (TSC) and the Emergency Operations Facility (EOF). The Unusual Event was declared under HU3.1 "toxic, corrosive, asphyxiate, or flammable gases in amounts that have or could have adversely affected normal plant operations." The fire brigade has been dispatched to determine whether a fire actually exists. The licensee informed State and local agencies and the NRC Resident Inspector. Notified other FEDS (FEMA Ops Center, DHS NICC Watch Officer, DHS SWO) and (Nuclear SSA, FEMA NWC) via email.

  • * * UPDATE AT 0707 EDT ON 8/12/2014 FROM DAVID FASCHER TO MARK ABRAMOVITZ * * *

The Unusual Event was terminated at 0700 EDT. Halon discharged into the plant simulator. There was no actual fire. Offsite assistance was requested. Local fire department and ambulance are on site. The TSC and EOF have been activated. The halon discharge into the simulator building is not impacting normal plant operations where the ERO (Emergency Response Organization) capabilities and staffing are still required. Therefore, activation for UE (Unusual Event) is being terminated. The Incident Commander released the building for normal access at 0717 EDT. The licensee informed State and local agencies and the NRC Resident Inspector. Notified the R2DO (Nease), IRD (Gott), and NRR (Thomas). Notified other FEDS (FEMA Ops Center, DHS NICC Watch Officer, DHS SWO) and (Nuclear SSA, FEMA NWC) via email.

  • * * UPDATE AT 1218 EDT ON 8/12/14 FROM CRAIG OLIVER TO JOHN SHOEMAKER * * *

EVENT DESCRIPTION: This is an update of a previous notification which was made by telephone to the (NRC) Operations Center at approximately 0504 EDT per Event Number 50355. At approximately 0421 EDT on 08/12/2014, the Halon fire suppression system in the Plant Simulator actuated by releasing the Halon. A Notification of Unusual Event (NOUE) was declared at 0432 EDT on the basis that a release of toxic or asphyxiating gas had occurred on site (Emergency Action Level HU3.1). Emergency response personnel reported to the site and prepared to perform emergency response activities. The site fire brigade was dispatched. The local fire department was called and emergency personnel were dispatched to the site. The reason for the Halon discharge is not known at this time and is under investigation. No actual fire was observed. The Plant Simulator is located in the same building with the primary Technical Support Center (TSC) and primary Emergency Operations Facility (EOF). Since the Halon discharge occurred in this building, the site incident commander restricted access to these two primary Emergency Response Facilities, rendering them unavailable for use. The NOUE was terminated at 0700 EDT. Normal access to the TSC and EOF was restored at 0717 EDT. INITIAL SAFETY SIGNIFICANCE EVALUATION: This event had no effect on the operating units, and there was no adverse impact on nuclear safety or on the health and safety of the public. The NRC Resident Inspector has been notified. CORRECTIVE ACTIONS: Offsite fire department personnel assisted by on site fire brigade have validated that no fire condition existed. The building has been ventilated and normal access restored. The failure of the Halon System is being tracked for restoration in accordance with station fire protection documents. Notified R2DO (Hopper) and NRR Daytime EO (Thomas).

ENS 497883 February 2014 15:03:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to Toxic Gas Release That Could Affect Normal Operation

At 1003 EST, Unit 1 declared an Unusual Event - EAL HU 3.1 (Toxic/corrosive/asphyxiate/flammable gas release that could affect normal operations) due to smoke in the Unit 1 "B" Battery room. The Unit 1 standby UPS inverter cabinet was smoking and leaking fluid. The fire brigade responded and declared the room uninhabitable due to smoke. The standby inverter was de-eneergized and the smoke subsided. The standby inverter was not in service and no plant equipment was lost. Unit 2 was not affected. Request for offsite assistance was sent to the local fire department but was not needed.

The licensee notified the NRC Resident Inspector, the State of North Carolina, and local emergency response organizations. Notified Federal Agencies (DHS SWO, FEMA Operations Center, NICC Watch Officer, and NuclearSSA) via email.

  • * *UPDATE PROVIDED TO JEFF ROTTON FROM MARTIN HAMM AT 1045 EST ON 02/03/2014* * *

Licensee terminated from the Unusual Event at 10:25 EST. Licensee notified the NRC Resident Inspector, the State of North Carolina and local emergency response organizations. Notified Federal Agencies (DHS SWO, FEMA Operations Center, NICC Watch Officer and Nuclear SSA) via email.

ENS 4971311 January 2014 00:48:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to Explosion within Protected Area Boundary

The licensee declared a Notice of an Unusual Event per EAL HU2.2 "Explosion with Protected Area Boundary" following an apparent fault and explosion on the M29 transformer (a non-safety related transformer). This resulted in a loss of one electrical bus at the ocean discharge station; however, no safety-related electrical loads were effected and both units remained at 100 percent electrical power. Station personnel reported that there was no smoke in the area of the M29 transformer and the event may have been a flashover explosion in the area of the transformer. All safety systems remain available. Licensee is investigating the cause of the explosion, and no offsite assistance was required. The licensee has notified the NRC Resident Inspector, the State of North Carolina, and other local authorities. Notified DHS SWO, FEMA Operations Center, NICC Watch Officer, and NuclearSSA via e-mail.

  • * * UPDATE ON 01/10/14 AT 2343 EST FROM MIKE MORRIS TO RYAN ALEXANDER * * *

Notification of an Unusual Event is being terminated (at 2320 EST) because the condition no longer exists. The source of the apparent explosion was a failed insulator on a breaker and is known to present no danger to public health and safety. Both Units are stable and a recovery organization is in place. The licensee has notified the NRC Resident Inspector regarding the termination of the event. Notified R2DO (Hopper), NRR EO (Lubinski), IRD Manager (Gott), DHS SWO, FEMA Operations Center, NICC Watch Officer, and Nuclear SSA via e-mail.

ENS 488905 April 2013 10:24:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to a Fire Alarm in the Stack Filter House

At 0624 (EDT), the Brunswick Steam Electric Plant (BSEP) declared an Unusual Event due to a fire alarm in the Stack Filter House. The classification of the Unusual Event is based on Emergency Action Level (EAL) HU2.1, 'Fire not extinguished within 15 minutes of control room notification or verification of a control room fire alarm.' Verification of fire could not be made within 15 minutes of fire alarm due to confined space conditions. Actual fire conditions did not exist; alarm was caused by environmental conditions. There is no impact on the health and safety of the public. The licensee terminated the Unusual Event at 0650 EDT. Personnel injuries and equipment damage did not occur. Offsite assistance was not required. The licensee has notified the state and local authorities. The licensee will notify the NRC Resident Inspector. Notified DHS, FEMA, DHS NICC and NuclearSSA.

  • * * RETRACTION FROM WILLIAM MURRAY TO VINCE KLCO AT 1644 EDT ON 4/5/2013 * * *

This event is being retracted based upon the following: As stated in the original event notification, an actual fire condition did not exist and the control room fire alarm was caused by environmental conditions. Because an actual fire did not exist and the fire detection system alarm was not valid, the condition described in the Emergency Action Level (EAL) HU2.1, 'Fire not extinguished within 15 minutes of control room notification or verification of a control room fire alarm,' also did not exist. The Unusual Event was terminated at 0650 (EDT). The Unusual Event classification was appropriately made, in accordance with the EAL basis which requires the control room alarm be validated by other indications or alarms or by an actual field report, or the classification must be made. Based on the preceding information, Event Notification 48890 is retracted. The licensee will notify the NRC Resident Inspector. Notified the R2DO (Rich) and the NRR EO (Lee).

ENS 4878326 February 2013 14:00:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to Toxic Gas Leak

At 0900, the Brunswick Steam Electric Plant (BSEP) declared an Unusual Event due to a release of Freon from the 2A Turbine Building Chiller. The classification of the Unusual Event is based on Emergency Action Level (EAL) HU3.1, 'Toxic, corrosive, asphyxiant or flammable gases in amounts that have or could adversely affect normal plant operations.' Actions have been taken to secure the chiller and isolate the release of Freon; however, Freon continues to be released. The release is only affecting the area immediately surrounding the 2A Turbine Building Chiller. No other plant areas are being impacted. There is no impact on the health and safety of the public. The licensee notified Brunswick Warning Point, Hanover Warning Point, State Warning Point and the NRC Resident Inspector. Notified DHS, FEMA, DHS NICC and NuclearSSA (email).

  • * * UPDATE AT 1555 EST ON 2/26/13 FROM ERIC WHITE TO S. SANDIN * * *

At 1545 EST on 2/26/13, Brunswick terminated their Unusual Event based on the fact that the entry conditions no longer existed. A temporary patch has been installed on the 2A Turbine Building Chiller and work is in progress to evacuate residual Freon from the chiller unit. The licensee notified state and local agencies and the NRC Resident Inspector. Notified R2DO (Musser), IRD (Kozal) and NRR (Chernoff). Notified DHS, FEMA, DHS NICC and NuclearSSA (email).

ENS 4768723 February 2012 01:14:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Inoperability of Emergency Core Cooling Systems

At 1859 hours EST, the Brunswick site experienced a loss of balance of plant (BOP) bus Common C. As a result, makeup pumps to the ECCS discharge line keepfill systems lost power. At 1905 on Unit 1, 'A' loop of the Core Spray (CS) system received a low discharge pressure alarm and was declared inoperable. At 1916 hours, 'B' loop of the Residual Heat Removal (RHR) system received a low discharge pressure alarm and was declared inoperable. With the loss of the second low pressure ECCS system, Condition J of Technical Specification 3.5.1, 'ECCS Operating,' was entered, which requires the Unit 1 to enter LCO 3.0.3 immediately. At 1931 hours, 'A' loop of RHR was declared inoperable due to low discharge pressure. Power reduction of Unit 1 was initiated at 2014 hours. At 2055 hours on Unit 2, 'A' loop of the Residual Heat Removal (RHR) system received a low discharge pressure alarm and was declared inoperable. At 2128 hours, 'B' loop of the Core Spray (CS) system received a low discharge pressure alarm and was declared inoperable. With the loss of the second low pressure ECCS system, Condition J of Technical Specification 3.5.1, 'ECCS Operating,' was entered, which requires the Unit 2 to enter LCO 3.0.3 immediately. Power reduction of Unit 2 was initiated at 2219 hours. This event reportability is in accordance with 10CRF50.72(b)(2)(i), Technical Specification Required Shutdown, due to inoperability of ECCS systems. The initial safety significance of this event is minimal. Offsite power and the Emergency Diesel Generators are operable. The High Pressure Coolant Injection (HPCI) system remains operable on both Unit 1 and Unit 2. The Reactor Core Isolation Cooling (RCIC) system remains operable on Unit 1 and is being restored following maintenance on Unit 2. Troubleshooting activities to determine the loss of the BOP Common C bus are in progress. Efforts are in progress to install temporary power to the keepfill makeup pumps. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM CURTIS DUNSMORE TO DONALD NORWOOD AT 0223 EST ON 2/23/2012 * * *

Unit 1 - At 2315 hours, temporary power was provided to the ECCS keepfill makeup pump and the ECCS systems were restored. LCO 3.0.3 was exited on Unit 1 at 0041 hours with restoration of the 'A' and 'B' loops of the RHR systems. The 'A' loop of the Core Spray system was restored at 0058 hours on 2/23/2012. During the shutdown, Unit 1 was manually scrammed due to high delta-pressure across the Circulating Water Pump traveling screens. See EN #47690 for details. Unit 2 - At 2315 hours, temporary power was provided to the ECCS keepfill makeup pump and the ECCS systems were restored. LCO 3.0.3 was exited on Unit 2 at 2354 hours with restoration of 'B' loop of the RHR system. The 'A' loop of the Core Spray system was restored at 0039 hours. Unit 2 was at 96% of Rated Thermal Power when the shutdown was terminated. The licensee notified the NRC Resident Inspector. Notified R2DO (Ernstes).

High Pressure Coolant Injection
Emergency Diesel Generator
Reactor Core Isolation Cooling
Core Spray
Residual Heat Removal
Emergency Core Cooling System
05000325/LER-2012-001
ENS 4744416 November 2011 08:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
Unusual Event Due to Drywell Leakage Greater than 10 Gpm

On 11/16/11 at 0208 EST, Brunswick Nuclear Plant, Unit 2 calculated a drywall floor drain 42 minute leak rate of 5.88 gpm, following several hours of gradually rising floor drain leakage during a plant startup. Tech Spec 3.4.4 A was entered, requiring floor drain leakage to be restored below 5 gpm within 8 hours. At 0253 EST, a 45 minute leak rate of 10.11 gpm was calculated. At 0301 EST, Unusual Event SU 6.1 was declared for unidentified leakage exceeding 10 gpm, and at 0309 EST, a manual reactor scram was inserted from approximately 7% power (10 CFR 50.72(b)(2)(iv)(B)). Following the scram, the reactor was depressurized at a maximum cooldown rate of 92.5 deg F/hr, and the unidentified leak rate fell less than 10 gpm within 1 hour and less than 5 gpm within 2 hours. Leak rate at 0614 EST on 11/16/11 is 3.82 gpm with reactor pressure at 228 psig. The exact nature of the leak is unknown at this time. The current plan is to continue to depressurize and cool down the reactor to Mode 4, such that a full drywall inspection can commence. At present, Brunswick has not terminated the Unusual Event. Level control is currently being maintained with control rod drives (CRD). The MSIVs were manually closed to control cooldown. The maximum cooldown was observed to be 92.5 F/hour. The plant plans to reopen MISIVs and depressurized to condensate booster pump injection pressure of 350 psig. The plan is to achieve Mode 4 for a leak inspection. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM DAVID FASHCHER TO CHARLES TEAL AT 0550 EST ON 11/16/11 * * *

The leakage rate is currently 3.73 gpm. The decrease is due to lower pressure which is currently at 258 psig. There are no additional changes. The leakage source is not identified at this time. The licensee has notified the NRC Resident Inspector. Notified R2DO (Vias).

  • * * UPDATE FROM DUSTIN LUPTON TO JOHN SHOEMAKER AT 0648 EST ON 11/16/11 * * *

The leakage rate is currently below the T.S. limit due to lower pressure which is currently at 210 psig. There are no additional changes. The plant will remain in an Unusual Event (UE) until further notice. The licensee has notified the NRC Resident Inspector. Notified R2DO (Vias).

  • * * UPDATE FROM DUSTIN LUPTON TO CHARLES TEAL AT 0749 EST ON 11/16/11 * * *

The leakage rate is stable. The leak rate is calculated at 3.04 gpm at 183 psig at 0708 EST. The current reactor pressure is 162 psig. The licensee has notified the NRC Resident Inspector. Notified R2DO (Vias).

  • * * UPDATE FROM DUSTIN LUPTON TO JOHN KNOKE AT 0832 EST ON 11/16/11 * * *

The licensee terminated from their Unusual Event at 0815 EST. The leakage is still unidentified. The licensee has notified the NRC Resident Inspector. Notified R2DO (Vias).

Control Rod
ENS 4687323 May 2011 19:35:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationAlert Declared Due to Halon Discharge in Emergency Diesel Generator Building

At 1535 EDT, Brunswick Units 1 & 2 declared an Alert condition due to a discharge of Halon gas into the basement of the emergency diesel generator building (EAL H.A.3.1 for toxic gas discharge into a vital area). Initial inspection indicates that there is no fire. No offsite assistance was required and no personnel injuries as a result of the discharge. Both reactors continue to operate at 100% power. The licensee is investigating the cause of the discharge and will terminate the Alert when the area is ventilated and can be reoccupied. The licensee has notified State and local authorities and the NRC Resident Inspector.

  • * * UPDATE FROM CHRIS CINDRIC TO DONG PARK AT 1659 EDT ON 5/23/11 * * *

A later report confirmed that one individual was inside the diesel generator building at the time of the Halon discharge. The individual evacuated the building but complained of chest pains about an hour after the incident. An ambulance was dispatched to transport the individual to the hospital.

  • * * UPDATE FROM CHRIS CINDRIC TO DONG PARK AT 1945 EDT ON 5/23/11 * * *

The licensee terminated the Alert at 1943 EDT based on restoring normal atmosphere conditions in the emergency diesel generator building. The initiating cause of this event is still being investigated. The NRC Operations Center has notified the federal agencies initially notified of this event. Notified R2DO (Shaeffer), NRR EO (Brown) and IRD (Grant).

Emergency Diesel Generator
ENS 459806 June 2010 15:37:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationBrunswick Declared Alert Due to Halon Discharge in Emergency Diesel Generator Building

At 1137 EDT, Brunswick Units 1 & 2 declared an Alert condition due to a discharge of Halon gas into the basement of the emergency diesel generator building (EAL H.A.3.1 for toxic gas discharge into a vital area). Initial inspection indicates that there is no fire. No offsite assistance was required and no personnel injuries as a result of the discharge. Both reactors continue to operate at 100% power. The licensee is investigating the cause of the discharge and will terminate the Alert when the area is ventilated and can be reoccupied. The licensee has notified State and local authorities and the NRC Resident Inspector.

  • * * UPDATE TO ABRAMOVITZ FROM CINDRIC AT 1616 EDT ON 6/6/10 * * *

The licensee terminated the Alert at 1614 EDT based on restoring normal atmosphere conditions in the emergency diesel generator building. The initiating cause of this event is still being investigated. State and local authorities have been notified and the Resident Inspector will be notified. The NRC Operations Center has notified the Federal Agencies initially notified of this event. R2DO (Vias), NRR EO (Galloway) and IRD (Grant) notified.

Emergency Diesel Generator
ENS 4579627 March 2010 02:45:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Dut to Fire Greater than 15 Minutes in Turbine BuildingAn Unusual Event was declared at 2259 EDT due to a fire in the Unit 1 Turbine Building lasting > 15 minutes. The fire was reported by field personnel working in the Unit 1 Turbine Building Condenser Bay at 2245. Smoke was observed coming from the overhead but no visible flames were evident. The source of the fire was from electric blankets used for post-weld heat treatment. The fire was extinguished when the blankets were de-energized. No off-site assistance was required. The Unusual Event was terminated at 2310. There were no injuries and no damage to plant equipment. The fuel for the fire was tape that was used to bind the blankets together. The licensee has notified State and local authorities and will be notifying the NRC Resident Inspector.
ENS 4571119 February 2010 16:11:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnsual Event Due to Carbon Dioxide Discharge in the High Pressure Coolant Injection (Hpci) Room

The licensee reported that a CO2 discharge has occurred in the Unit 1 HPCI room. The cause and amount of CO2 released is not specifically known but the licensee judged that the room was not currently habitable based on the CO2. The licensee consequently declared an Unusual Event (UE) under EAL HU3.1 - "Toxic, Corrosive, Asphyxiant, or Flammable Material in Amounts That Could Adversely Impact Plant Operations. The licensee stated that activities were in progress in the room at the time of the discharge. There is no indication of a fire in the room and there were no personnel injuries as a result of the discharge. The discharge also had no impact on plant operation. The licensee at this point plans to terminate the UE when the room is properly ventilated. The licensee has notified State and local authorities and the NRC Resident Inspector and does not plan a press release.

  • * * UPDATE FROM GARY ROBERTS TO DONG PARK @ 1354 EST ON 02/19/10 * * *

At 1330 EST on 2/19/10, the Unusual Event was terminated. The atmosphere in the HPCI room is back to normal. The CO2 source was from cylinders located in the HPCI room which is part of the fire suppression system. The licensee has notified the NRC Resident Inspector. Notified IRD (Grant), R2DO (Bartley), NRR EO (Thorp), DHS (Vestal) and FEMA (Fuller).

High Pressure Coolant Injection
ENS 4536820 September 2009 18:00:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Inoperability of Diesel GeneratorEvent reportability, is in accordance with 10 CFR 50.72(b)(2)(i), Technical Specification Required Shutdown, due to inoperability of Diesel Generator #4 extending from planned maintenance. Brunswick Nuclear Plant Units 1 and 2 are initiating unit shutdowns in anticipation of Technical Specification Required Shutdown as required by Technical Specification 3.8.1, Condition H due to the inoperability of Diesel Generator #4 lasting longer than seven (7) days. Power reduction commenced at 1400 on Unit 1, and is scheduled to commence at 2200 09/20/2009 on Unit 2 in accordance with site procedures. Both units will continue the shutdown to Mode 4 or until the emergency diesel generator is declared operable following appropriate repairs and testing. The licensee has notified the NRC Resident Inspector.Emergency Diesel Generator05000325/LER-2009-004
ENS 432691 April 2007 14:45:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTech Spec Required Shutdown Due to Edg InoperabilityDuring post-maintenance operability testing, Diesel Generator 4 exhibited unstable power output while synchronized to the grid. This testing was being performed at the conclusion of a planned Diesel Generator 4 maintenance outage. Preventive maintenance activities included in this scheduled outage included replacement of various relays in the Diesel Generator control logic and replacement of the engine governor. Brunswick Nuclear Plant Unit 1 is commencing a unit shutdown as required by Technical Specification 3.8.1 Condition H due to the inoperability of Diesel Generator 4 lasting longer than seven (7) days. TS 3.8.1 Required Action H.1 requires Unit 1 to be in MODE 3 by 1615 on 4/1/2007 and in MODE 4 by 1615 on 4/2/2007. This event is reportable per 10CFR50.72(b)(2)(i). Power reduction was commenced at 1045 in accordance with station procedures for unit shutdown. Power level has been reduced from 100% to 53%. Unit 1 shutdown will continue until the unit is in MODE 4 or until the engine is declared operable following appropriate repairs and testing. Unit 2 is in MODE 4, Cold Shutdown. The inoperable Diesel Generator 4 is not needed to meet the requirements of Unit 2 Technical Specification 3.8.2. The inoperability of Diesel Generator 4 is of minimal safety significance for Unit 1. Unit 1 has two operable off-site circuits and three (3) Diesel Generators are operable. The remaining three (3) operable Diesel Generators and off-site circuits are adequate to supply electrical power to the on-site Class 1 E Distribution System. This maintains the safety function of the AC sources. Unit 1 is being shutdown to place the unit in MODE 4 where the inoperable Diesel Generator 4 is not required. Unit 2 is currently in MODE 4 and does not require Diesel Generator 4 to be operable. As such, this event is of zero safety significance for Unit 2. During post-maintenance operability testing, Diesel Generator 4 exhibited unstable power output while synchronized to the grid. Station engineering and a vendor representative continue to evaluate the engine/generator performance. Repair plans will be developed and implemented as appropriate following completion of the engineering evaluation. The inoperability of Diesel Generator 4 will prevent Unit 2 from changing mode for returning the plant to service. The licensee notified the NRC Resident Inspector.
ENS 429602 November 2006 23:53:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification ShutdownOn 11/01/06 at approximately 18:23 (EST) Brunswick Unit 2 experienced a loss of the unit's Startup Auxiliary Transformer (SAT) and a loss of reactor forced circulation. Due to the loss of the SAT and subsequent manual reactor scram of Unit 2, a loss of Offsite Power resulted to the Unit 2 power buses. All four site Emergency Diesel Generators (EDGs) then started as designed. On 11/02/06 at approximately 0400 (EST) EDG no. 1 tripped on low lube oil pressure due to high differential pressure on the EDG lube oil strainer. The EDG was not loaded at the time of the trip. Due to the loss of one offsite qualified circuit (Unit 2 SAT) and the loss of one EDG (EDG 1), Unit 1 entered Technical Specification (TS) 3.8.1, Condition F, which requires restoration of the inoperable offsite circuit or restoration of the inoperable Diesel Generator within 12 hours. At 1600 on 11/02/06, Brunswick Unit 1 entered TS 3.8.1, Condition H, Required Action H.1 to be in MODE 3 in 12 hours and Required Action H.2 to be in MODE 4 within 36 hours. On 11/02/06 at 17:54 EDG 2 was declared inoperable due to being placed in manual for a required loaded run due to having been operated at no load for a period of time. Unit 1 entered Technical Specification 3.0.3 due to having EDG 1, EDG 2, and one offsite qualified circuit (Unit 2 SAT) inoperable. Per Technical Specification 3.0.3, action shall be initiated within one hour to place the unit in Mode 2 within 7 hours, Mode 3 within 13 hours, and Mode 4 within 37 hours. Unit 1 began a Technical Specification Required shutdown at 18:53 and is presently at 99% power. On 11/02/06 at 21:30, EDG 2 was declared operable following the loaded run and is presently in standby in the auto mode. Technical Specification 3.0.3 was exited at that time. Unit 1 remains in Technical Specification 3.8.1 Condition H at the present time. At 21:59, the NRC resident was notified of this event.Emergency Diesel Generator
ENS 429551 November 2006 23:37:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Unit 2 Declared an Unusual Event Due to Loss of Offsite Power to the 4Kv Emergency Buses

At 1823 EST, Unit 2 was manually scrammed due to a loss of offsite power from the Startup Auxiliary Transformer to both 4KV Emergency (E) buses. Both Emergency Diesel Generators (EDGs) 3&4 autostarted and re-energized the affected electrical buses. At 1823 EST, an Unusual Event was declared based on EAL 06.01.01, "Inability to power either 4KV E bus from offsite power." Unit 2 is currently stable in mode 3, Hot Shutdown, with MSIVs closed and HPCI controlling pressure and RPV Water Level. All control rods fully inserted following the manual reactor scram. The licensee determined that no emergency facilities will be activated and that no offsite assistance is needed at this time. The licensee informed both state and local agencies and will inform the NRC Resident Inspector.

  • * * UPDATE PROVIDED BY JOEL LEVINER TO JEFF ROTTON AT 2214 EST ON 11/01/06 * * *

On 11/01/06 at approximately 18:23 (EST) Brunswick Unit 2 experienced a loss of the unit's Startup Auxiliary Transformer and a loss of reactor forced circulation. A manual reactor scram was performed as required by station Abnormal Operating Procedures. Due to the loss of the Startup Auxiliary Transformer and subsequent manual reactor scram, a loss of Offsite Power resulted to the unit's power buses when unit shutdown was completed. All control rods properly inserted when the manual reactor scram was performed. All four site emergency diesels started and diesels 3 and 4 are supplying the Unit 2 emergency buses. Reactor water level reached low level 1 (LL1) and low level 2 (LL2) as result of the reactor scram and loss of offsite power. The LL1 signal resulted in Group 2 (floor and equipment drain isolation valves), Group 6 (monitoring and sampling isolation valves) and Group 8 (shutdown cooling isolation valves) isolation signals. All low level 1 isolations occurred as designed. The LL2 resulted in a Reactor Core Isolation Cooling (RCIC) system actuation, High Pressure Coolant Injection (HPCI) system actuation, Group 3 (reactor water cleanup valves) isolation signal, a secondary containment isolation signal, a Standby Gas Treatment (SBGT) initiation signal, a Control Room Emergency Ventilation (CREV) initiation signal, and an Alternate Rod Insertion (ARI) actuation signal. All isolation and actuations occurred as designed with the exception the CREV initiation and ARI actuation. CREV initiation and ARI actuations were performed by manual actions. The failure of the CREV and ARI initiation/actuations are under investigation. The RCIC and HPCI systems were used to restore reactor water level to the normal operation band. Reactor vessel pressure is being controlled in the normal band with manual operation of Safety Relief Valves (SRV), and HPCI/RCIC in pressure control mode. The Main Steam Isolation Valves (MSIVs) (Group 1) and the drywell pneumatic isolation valves (Group 10) closed on the loss of power. The plant is a stable condition. Troubleshooting activities are in progress to determine the cause of the event. At 1910, the NRC was previously notified of the Unusual Event declaration. Initial Safety Significance Evaluation: The safety significance of this event is minimal and Unit 2 is in a stable condition. All control rods properly inserted when the manual scram was performed. Plant safety systems responded as required with the exception of the CREV and ARI systems which did not automatically initiate but functioned properly when manually actuated. All four emergency diesels started and Unit 2 diesels 3 and 4 are supplying the Unit 2 emergency buses. Reactor pressure and level are being controlled per procedure, with HPCI and RCIC. Actions are in progress to re-establish off site power supply to emergency buses 3 and 4 via backfeed through the Unit Auxiliary Transformer (UAT). Corrective Actions: Actions are in progress to re-establish offsite power supply to emergency buses 3 and 4 via backfeed through the UAT. Investigations are in progress to determine the cause of the SAT failure and the failure of CREV and ARI to auto-initiate. The licensee has notified the NRC Resident Inspector and the State and local emergency agencies. Update provided also added the following reportable notifications due to the event: 10CFR50.72(b)(2) (iv)(A) and(iv)(B) and 10CFR50.72(b)(3)(iv)(A). Notified R2DO (Evans).

  • * * UPDATE PROVIDED BY MARK SCHALL TO JEFF ROTTON AT 1805 EST ON 11/02/06 * * *

Licensee reported that the Unusual Event was terminated at 1745 EST on 11/02/06 after Offsite power was restored to both 4 KV E Buses from the Unit Auxiliary Transformer (UAT) on Unit 2. The #3 and #4 EDGs have been secured and are in Standby. #1 EDG remains inoperable and #2 EDG is presently being Load Tested. The licensee will be notifying the NRC Resident Inspector and the State and local emergency agencies. Notified R2DO (Evans), NRREO (Richards), IRD Manager (Leach), DHS (Barnes), and FEMA (Kuzia).

Secondary containment
High Pressure Coolant Injection
Emergency Diesel Generator
Main Steam Isolation Valve
Reactor Core Isolation Cooling
Shutdown Cooling
Reactor Water Cleanup
Control Room Emergency Ventilation
Safety Relief Valve
Control Rod
05000324/LER-2006-001
ENS 4198313 September 2005 03:14:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to Hurricane Ophelia Warning

On September 12, 2005, at 2300 hours, a hurricane warning was issued, which resulted in the declaration of an unusual event for both units. Unit 1 and 2 are currently operating at 100 percent of rated thermal power. The plant area is not currently experiencing any hurricane force winds. The wind speed at the site is approximately 24 miles per hour. State and county emergency response organizations have been notified. The resident inspector has been notified. There is no significant impact to the safety of the plant at this time. The plant is currently in Abnormal Operating Procedure 0AOP-13.0, 'Operation During Hurricane, Flood Conditions, Tornado, or Earthquake,' and Plant Emergency Procedure 0PEP-02.6, 'Severe Weather,' in preparation for hurricane conditions. On-site facilities are not being activated at this time. No off-site assistance is requested. Request suspension of additional follow up notification unless plant conditions change. All Emergency Core Cooling Systems and the Emergency Diesel Generators are fully operable if needed. The electrical grid is stable.

  • * * UPDATE AT 0758 EDT ON 9/14/05 FROM BRUCE HARTSOCK TO S. SANDIN * * *

Commenced reduction in power on Unit 2 in anticipation of exceeding 74 mph winds. Prediction revised to maximum of 64 mph onsite. Power reduction stopped. Plant stabilized. Power will be restored. Notified RCT (Hasselberg) and R2IRC (Casto).

  • * * UPDATE AT 0028 EDT ON 9/15/05 FROM KENON CHISM TO S. SANDIN * * *

As of 2300 hours (EDT) on September 14, 2005, the Hurricane Warning south of Cape Fear, North Carolina, has been discontinued; therefore, the Unusual Event has been terminated. Entry into the Unusual Event was reported by Event Notification 41983. Both Unit 1 and Unit 2 continue to operate at 100 percent power. There has been no damage affecting safety equipment or causing operational constraints as a result of Hurricane Ophelia. The licensee notified state/local agencies and will inform the NRC Resident Inspector. Notified R2DO (Munday), NRR (Mayfield), IRD (McGinty), FEMA (Snyder), and DHS (Gomez).

Emergency Diesel Generator
Emergency Core Cooling System
ENS 418955 August 2005 22:40:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Technical Specification Required Shutdown Due to Inoperability of All Emergency Diesel Generators

Event reportability is in accordance with 10 CFR 50.72(b)(3)(v)(D), 'Accident Mitigation,' and 10 CFR 50.72(b)(2)(i), 'TS Required Shutdown,' due to potential COMMON CAUSE FAILURE of all four Emergency Diesel Generators. On 05 August 2005, at 14:31 hrs, DG2 was started for data gathering purposes, and it experienced a trip and lockout on differential current. Investigation revealed that set points for the installed DG differential current protective devices may be set too conservatively. Since each DG has the same relay with the same set point, all DGs were declared inoperable. Preparations are in progress to place both units in Cold Shutdown. The site has insufficient operable backup AC sources. The current effect on the plant is minimal due to all normal AC sources being available and operable. However, due to the potential for losing a normal AC source resulting in insufficient power being available to some emergency systems, both units will be placed in cold shutdown until all emergency diesel generators can be restored to operable. Corrective actions are in progress to correct differential current protective device problem in order to restore availability of DG2 and operability of all four DGs. The licensee plans on commencing a down power on both units (Unit 2 first) within several hours. Technical Specifications require both units to be in Hot Shutdown within 12 hours (approximately 0700 on 08/06/05) and Cold Shutdown within 36 hours. Neither unit has any other significant systems LCOs. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM LICENSEE (BAIN) TO NRC (HUFFMAN) AT 10:38 EDT ON 8/06/05 * * *

This is a follow up message to the initial event reported in accordance with 10 CFR 50.72(b)(3)(v)(D), 'Accident Mitigation' and 10 CFR 50.72(b)(2)(i), 'TS Required Shutdown' due to the potential COMMON CAUSE FAILURE of all four Emergency Diesel Generators. Unit 2 entered Mode 3 (Hot Shutdown) at 04:46. Unit 1 entered Mode 3 (Hot Shutdown) at 05:31. Both units are continuing to cool down in preparation for entering Mode 4 (Cold Shutdown)." The licensee notified the NRC Resident Inspector. Notified R2DO(Landis), NRR EO (Haney), and IRD (McGinty).

Emergency Diesel Generator05000325/LER-2005-006
ENS 4169212 May 2005 08:11:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.73(a)(1), Submit an LER
Technical Specification Required Shutdown Due to Loss of Emergency Bus E1

On May 12, 2005, at 0411 hours, electrical power was lost to the 4160 VAC Emergency Bus E1. Emergency Diesel Generator 1 was inoperable for maintenance at the time of the electrical power loss. This power loss to Emergency Bus E1 affected both Units 1 and 2. Unit 1 The loss of power to E1 resulted in Division 1 Primary Containment Isolation Valve (PCIV) actuations. The actuations included the Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Traversing In-core Probe, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 3 (i.e., Reactor Water Cleanup), and Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems) valves, as well as the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation) and the automatic start of Standby Gas Treatment (SGT) System train B. The actuations of PCIVs and Reactor Building Ventilation System isolation were complete and the affected equipment responded as designed to the invalid signal (i.e., the valves and dampers that were open, at the time of the event, closed). Additionally, SGT System train B started and functioned successfully. Loss of power to E1 also resulted in entry into LCO 3.0.3 (i.e., be in Mode 2 within 7 hours, Mode 3 within 13 hours, and Mode 4 within 37 hours) due to all required reactor coolant leakage detection instrumentation/systems being inoperable. At 0440 hours, it was discovered that all three Control Room Air Conditioning (AC) subsystems became inoperable due to failure of the control building air compressors and Technical Specification LCO 3.0.3 was entered. At 0515 hours, it was determined that both Control Room Emergency Ventilation (CREV) subsystems became inoperable when the dampers drifted shut. At 0546 hours, a control building air compressor was started and the control room air conditioning and CREV subsystems were returned to operable status. Operators initiated a plant shutdown for Unit 1, as required by Technical Specifications at 0948 hours. Unit 2 Conditions and activities associated with the Control Room AC and CREV systems apply to Unit 2 as well as Unit 1. Reporting Requirements Met by this Notification 10 CFR 50.72(b)(2)(1), the initiation of any nuclear plant shutdown required by the plant's Technical Specifications, applies to Unit 1. 10 CFR 50.72(b)(3)(v)(D), a condition that, at the time of discovery, could have prevented the fulfillment of the safety function of systems that are needed to mitigate the consequences of an accident (i.e., Control Room AC and CREV), applies to both Units 1 and 2. 10 CFR 50.73(a)(i), invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system, applies to Unit 1. INITIAL SAFETY SIGNIFICANCE EVALUATION Currently Unit 2 is operating at steady state with Unit 1 being shut down. Specified systems actuated as designed. No adverse impact to the control room environment occurred during the period (i.e., one hour and 35 minutes) the affected ventilation system was inoperable. The other redundant emergency busses are operable. Prior to the event reactor coolant leakage level for Unit 1 was well within operating limits. The actions as required by the applicable Technical Specifications have been established. CORRECTIVE ACTIONS Activities are currently under way to determine the cause of the E1 power loss and restore electrical power to Emergency Bus E1. Causes and actions to preclude recurrence will be addressed in accordance with the corrective action program and provided to the NRC in the associated licensee event report. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 05/13/05 @ 0952 BY LEONARD BELLER TO CHAUNCEY GOULD * * *

On May 12, 2005, at 0411 hours, electrical power was lost to the 4160 VAC Emergency Bus E1. Emergency Diesel Generator 1 was inoperable for maintenance at the time of the electrical power loss. This power loss to Emergency Bus E1 affected both Units 1 and 2. A non-emergency notification (Event Number 41692) was made to the NRC Operations Center at 112:2 hours. This follow-up notification discusses plant recovery from the Emergency Bus E1 power loss. Unit 1 Loss of power to E1 resulted in entry, into LCO 3.0.3 (i.e., be in Mode 2 within 7 hours, Mode 3 within 13 hours, and Mode 4 within 39 hours) due to all required reactor coolant system (RCS) leakage detection instrumentation being inoperable. Operators initiated a plant shutdown for Unit 1, as required by Technical Specifications at 0948 hours. A Notice of Enforcement Discretion (NOED) was requested from the NRC to waive compliance with the shutdown requirements associated with RCS leakage detection instrumentation in order to provide more time for an orderly plant shutdown. In lieu of the RCS leakage detection shutdown requirements (i.e., be in Mode 2 by 1111 hours), Unit 1 would adhere to the shutdown requirements associated with loss of Emergency Bus E1 (i.e.,, be in Mode 3 by May 13, 2005, at 0011 hours). The requested NOED was verbally granted by the NRC on May 12, 2005 at 1050 hours, so shutdown activities for Unit 1 continued versus the insertion of a manual reactor scram, with the unit at approximately 65 percent of rated thermal power. Power was restored to Emergency Bus E1 and the LCO associated with RCS leakage detection instrumentation was exited on May 12, 2005 at 1740 hours. The LCO associated with loss of power to Emergency Bus E1 was exited at 2015 hours. Unit 2 The LCO associated with loss of power to Emergency Bus E1 also applied to Unit 2, and was exited at 2015 hours, CORRECTIVE ACTIONS Emergency Diesel Generator 1 was made available, but not operable, on May 13, 2005, at 0117 hours. The licensee notified the NRC Resident Inspector. Reg 2 RDO (Moorman) was notified.

Reactor Coolant System
Secondary containment
Emergency Diesel Generator
Primary Containment Isolation System
Primary containment
Reactor Building Ventilation
Residual Heat Removal
Reactor Water Cleanup
Control Room Emergency Ventilation
05000325/LER-2005-004
ENS 4095314 August 2004 17:08:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNotice of Unusual Event Emergency Declared Due to Loss of Offsite Power

Licensee declared an Unusual Event at 1308 EDT on 08/14/04. Unusual Event was declared due to a Loss of Offsite Power which occurred due to a Lockout trip of the Station Auxiliary Transformer. All four emergency diesel generators started and loaded properly. On the reactor trip, all rods fully inserted. They received Group II, VI, and VIII PCIS isolations due to the loss of power. The MSIVs are closed and the licensee manually started RCIC for reactor level control and HPCI for reactor pressure control. The licensee in activating the Emergency Response Organizations. No offsite assistance required. The licensee notified the NRC Resident Inspector, State and local Emergency response organizations.

  • * * UPDATE PROVIDED TO JEFF ROTTON FROM KEITH HANZ AT 1727 EDT ON 08/14/04 * * *

Licensee declared termination of the Unusual Event at 1713 EDT on 08/14/04 after restoring offsite power to the Station Auxiliary Transformer, BOP and Emergency Buses. The licensee notified the NRC Resident Inspector. Notified R2DO (Julian), R4DO (Smith), IRD (Nieh), NRR EO (Carpenter), DHS (Doyle), and FEMA (Sullivan)

Emergency Diesel Generator
ENS 4095113 August 2004 22:20:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNotice of Unusual Event Declared Due to Hurricane Warning

Licensee declared Unusual Event due to a Hurricane Warning being issued by the National Weather Service for Brunswick County, NC which includes the Brunswick site. No protective actions are required at this time. No emergency facilities have been activated at this time. No offsite assistance requested. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED AT 1426 ON 08/14/04 TO JEFF ROTTON FROM KEITH HANZ * * *

Licensee terminated the Unusual Event at 1403 EDT on 08/14/04 due to the lifting of the hurricane warning in Brunswick County, North Carolina. The licensee has notified the NRC Resident Inspector. Notified R2DO (Julian), R4DO (Smith), IRD (Nieh), DHS (Inzer), FEMA (Eaches).

05000325/LER-2004-002
ENS 4090529 July 2004 13:42:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownPlant Entered Lco Action Statement Due to Malfunction of a Suppression Chamber-To-Drywell Vacuum Breaker.

On July 29, 2004, at approximately 0351 hours, testing of Suppression Chamber-to-Drywell vacuum breakers commenced in accordance with Periodic Test 0PT02.3.1, "Suppression Chamber-to-Drywell Vacuum Breaker Operability Test." At 0357 hours, it was determined that vacuum breaker 2-CAC-X18D had an open indication. Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.6.1.6, "Suppression Chamber-to-Drywell Vacuum Breakers," Condition B was entered for one suppression chamber-to-drywell vacuum breaker (2-CAC-X18D) not indicating closed. Required Action B.1 of TS LCO 3.6.1.6 provides 4 hours to verify the vacuum breaker closed. Attempts to confirm the vacuum breaker closed were unsuccessful and at 0757 hours, TS LCO 3.6.1.6 Condition C was entered. Required Action C.1 is to be in Mode 3 (Hot Shutdown) in 12 hours and Required Action C.2 is to be in Mode 4 (Cold Shutdown) in 36 hours. Initiation of the plant shutdown required by TS LCO 3.6.1.6 commenced at 0942 hours. This condition is being reported in accordance with 10 CFR 50.72(b)(2)(i) as the initiation of any nuclear plant shutdown required by the plant's TS. INITIAL SAFETY SIGNIFICANCE EVALUATION The initial safety significance of this condition is considered to be minimal. The actual position of the vacuum breaker cannot be confirmed, however if one vacuum breaker was not closed, communication between the drywell and suppression chamber air space could occur, and as a result, there is a potential, for primary containment overpressurization due to this bypass leakage if a loss of coolant accident were to occur. The plant is currently proceeding to hot shutdown with all Emergency Core Cooling systems operable. CORRECTIVE ACTIONS Determine the required corrective actions after entry into the drywell following shutdown. The safety significance of the event will be reviewed when the actual condition of the vacuum breaker is known. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 07/29/04 @ 1654 FROM KEN CHISM TO CHAUNCEY GOULD * * *

On July 29, 2004, at 1517 hours, a manual scram was inserted to shut down the Unit 2 reactor from approximately 23 percent of rated thermal power. The reactor shutdown was implemented to meet the requirements of Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.6 Required Action C.1 to be in Mode 3 in 12 hours. All control rods fully inserted into the core and no ECCS actuation occurred or relief valves lifted. Following the scram, an expected reactor vessel coolant level shrink occurred causing coolant level to decrease below the Low Level 1 setpoint. This coolant level decrease resulted in a Primary Containment Isolation Valve isolation signal to Group 2 (Drywell Equipment and Floor Drain, Traversing In-core Probe, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 6 (Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling System), and Group 8 (RHR Shutdown Cooling Suction and RHR Inboard Injection) isolation valves. The isolation signal closed all of the valves that were open at the time of the expected initiation. The plant is currently in mode 3 and proceeding with a normal cooldown to Mode 4. The NRC Resident Inspection was informed. Notified Reg 2 RDO (Tom Decker).

Primary containment
Shutdown Cooling
Residual Heat Removal
Control Rod
ENS 4016417 September 2003 02:40:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event at Brunswick Due to Hurricane Warning

Hurricane warning issued. There is no significant impact to the safety of the plant at this time. The plant area is not currently experiencing any unusual winds. Unit 1 is at 94% and Unit 2 is at 96% power. The wind speed at the site is 14 miles per hour at the time of this report. The NRC Resident Inspector was notified by the licensee.

  • * * UPDATE ON 09/18/03 AT 1753 EDT FROM FRANK RAMPERSAD TO NATHAN SANFILIPPO * * *

Brunswick has terminated the Unusual Event at 1740 EDT. This is based upon the hurricane warning being lifted. The licensee has notified the NRC Resident Inspector. Notified Wessman (DIRO), Boland (R2DO), FEMA (C. Bagwell), DHS (C. Wilson), Calvo (NRR EO).