ML18142B901

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LER 1975-010-00 for R. E. Ginna, Unresponsive Emergency Generator Governor Control Switch
ML18142B901
Person / Time
Site: Ginna Constellation icon.png
Issue date: 12/02/1975
From: White L
Rochester Gas & Electric Corp
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1975-010-00
Download: ML18142B901 (7)


Text

TRIBUTION FOR PART 50 DOCK~MATERIAL (TEMPORARY FORM)

CONTROL NQ: 13583 FILE. XNCIDENZ REPORT FIT

'C FROM. Rochester Gas Imi Elec. Co DATE OF DOC DATE REC'D LTR TWX RPT OTHER Rochester;.N;Y'..

e Jr 12-2-75 12-4-75 XXX TO: ORIG OTHFR SENT AEC PDR James P.O'Reill Noae 3 SENT LOCAL PDR CLASS UNC LASS PROP INFO INPUT NO CYS REC'D DOCKET NO:

IlXX .3 50-244 DESC R IPTION: ENCLOSURES:

Letter trans the follwoing.... Unusual. Event Report h'. 75-10; on .1.1-6-75, Concerning a, Unresponsiye Emirgency Generator Govenor.........'. W/Attabbaierlt;.',/

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0 'i~ ".',i';;, IYAII ROCHESTER GAS AND ELEC FRIC CORPORATION II 89 EAST AVENUE, ROCHESTER, M.Y. 1 1649 r

LEON D. WHITE. JII. Wg C~O VICt PlltSIDCNT A> Ac. tYi 3 IQ 700 e~ leobSiO~

SW Mr. James P. O'Reilly, Director' U. S; Nuclear Regulatory Commission Office of Inspection and Enforcement Region I

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631 Park Avenue King of Prus sia, Penn sylvania 19406

Subject:

Unusual Event 75-10, Unresponsive Emergency Generator Governor R. E. Ginna Nuclear Power Plant, Unit No. '1 Docket No. 50-244

Dear Mr. O'Reilly:

In accordance with Technical Specifications, Article 6.6.2b, the attached report of Unusual Event 75-10 is hereby submitted. Two additional, copies of this letter and the attachment are enclosed.

Very truly yours, L. D. White, Jr.

Attachment cc: Mr. Donald F. Knuth (30)

Mr. William G. McDonald (3)

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LICENSEE EVENT REPORT CONTROL. BLOCK: (PLEASE. PAINT ALL REQUIRED INFORMATIDf)I) 1 LICENSEE LICENSE EVENT

[oa] )4 YREG NAME 1 00 0000'0 LICENSE NUMBER 00 4 )

TYPE 1 1 1 ~03 TYPE

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7 09 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT DATE

[OD1] CON'T L ~I 0 5 0 0 2 4 4 1 1 0 6 7 5 2 0 2 7 5 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION Jog urin erformance of PT-12. 1 Emer enc Generator 1A immediatel followin close and 7 0 9 00

[pg trip of a service water pump breaker, the generator wattmeter indicated no response to 7 89 00 peration of the governor control switch. During operation of the phase current selector 7 0 9 80

[pg~] switch to check currents the meter indication changed to about full load, and subsequent 7 8 9 Qpg anipulation of the governor control verified proper response. (Unusual Event 50-244/75-80 7 0 9 80 SYSTEM CAUSE PRME COMPONENT COMPONENT 10),

CODE CODE COMPONENT CODE SUPPUER MANUFACTURER

[oa~) ~EE ~F G 3 N 3 R 1) A 1 5 2 7 8 9 10 11 12 17 43 47 40

~ CAUSE DESCRIPTION

~08 NA 7 8 9 00 Jog Recommended actions to determine the cause and remedial action taken are given on the 7 0 9 00

~10 attached sheet.

7 09 00 FACIUTY METHOD OF 7

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STATUS 9

~E ~oo 10

% POWER 12 13 OTHER STATUS 14 44 OISCOVEAY b

45 46 NA DISCOVERY DESCRIPTION 00 FORM OF AMOUNT OF ACTIVITY LOCATION OF AELEASS NA 7 0 9 10 11 44 45 00 PERSONNEL EXPOSURES 9,

NUMBER TYPE DESCRIPTION

~io ~00 0 Pi NA 7 8 11. 12 13. 80 PERSONNEL INJURIES NUMBER DESCRIPTION Q~aj ~oo o NA 7 09 11 12 80 OFFSITE CONSEQUENCES

~15 NA 7 09 00 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q~g z NA 7 09 10 00 PUBLICITY

[is~] NA 7 89 80 ADDITIONAL FACTORS

~10 NA 7 09 J)+ 80 NAME: Bruce A. Snow ext. 291-7'FO 80'HDNE.716/546-2700, Sl 04)~

Licensee Event Report Unusual Event 50-244/75-04 PORC Recommendations

1. Check wiring of emergency generator metering.
2. Perform test procedure PT-12.1 Emergency Diesel Generator 1A to the extent necessary.to observe proper indicated response to generator governor control once each calendar week with appropriate personnel to observe the generator start and operation, to include station mechanics and electricians. This is to begin on the following day, 1 1/7/75, and continue until'the next scheduled monthly surveillance.

Remedial Action Taken

1. The appropriate personnel have checked and tightened all connections .

of the emergency generator metering wiring.

2. Satisfactory response has been demonstrated on each of the five tests conducted following the incident.

'his action is being documented in Corrective Action Report CAR-1047;

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