LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive RelaysML18038B855 |
Person / Time |
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Site: |
Browns Ferry |
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Issue date: |
04/04/1997 |
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From: |
Austin S TENNESSEE VALLEY AUTHORITY |
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To: |
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Shared Package |
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ML18038B854 |
List: |
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References |
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LER-97-001-04, LER-97-1-4, NUDOCS 9704150185 |
Download: ML18038B855 (16) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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NRC FORM 366 U.s. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3160-0104 (4 96), EXPIRES 04/30/98 ESTlMATED BURDEN PER RESPONSE To COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 60.0 LICENSEE EVENT REPORT (LER) HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE UCENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD COMMENTS REGARDING BURDEN (see reverse for required number of ESTIMATE TO THE INFORMATION AND RECORDS digits/characters for each block) MANAGEMENT BRANCH rl-6 '33), U.S. NUCLEAR REGUlATORY COMMISSION, WASHINGTON. DC 20666 FACIUTY NAME (tl DOCKET NUMSElt tsl PAOE la)
Browns Ferry Unit 3 05000296 1 OF 8 TITLE (4I Loss of Offsite Power on Unit 3 During Refueling Outage Resulting From a Shorted Component EVENT DATE (5)
MONTH DAY YEAR LER NUMBER (6)
SEQUENTIAL NUMBER REVISION NUMBER MONTH REPORT DATE (7)
'AY YEAR NA'ocKET FAautv NAME OTHER FACILITIES INVOLVED (6)
NUMOErr FAaUTY NAME DOCKET NVMBErt 03 05 97 97 001 00 04 04 97 OPERATIN(3 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)
'N MODE (9) 20.2201 (b) 20.2203(a) (2)(v) 50 73(a) (2) 0) 50.73(a)(2)(viii)
Z0.2203(a)(1) 20.2203(a)(3)(a 50.73(a) (2) gr) 50.73(a)(2) (x)
POWER LEVEL (10) 000 20.2Z03(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2) (iig ,73.71 20.2203(a)(2) gi) 20.2203(a)(4) X, 50.73(a)(2)(iv) X OTHER 20.2203(a)(2) (iii) 50.36(c)(l) 50.73(a)(2) (v) specify In Abstract below or In NRC Form 366A 20.2203(a)(2) (iv) 50.36(c) (2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
TELEPNONE NLrMSErt Cr>qua Ar~ Coast Steven W Austin, Licensing Engineer (205) 729-2070 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN,THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER i::,~j:;.";.':";.:;;:;.>:::j;;"".) CAUSE SYSTEM COMPONENT MANUFACTURER To NPRDS To NPRDS SUPPLEMENTAL REPORT. EXPECTED (14) 'MONTH DAY YEAR EXPECTED YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X No DATE (16)
ABSTRACT (Limit to 1400 spaces, l.e., approximately 15 single-spaced typewritten lines) (16)
On March 5, 1997, at 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> Central Standard Time, (CST) Unit 3 received engineered safety feature system actuations due to a loss of offsite power. The loss of power was the result of the loss of both-the Athens and Trinity 161 KV power lines. Emergency Diesel Generators 3A, 3C, and 3D automatically started and tied to their respective shutdown boards. At 1122 hours0.013 days <br />0.312 hours <br />0.00186 weeks <br />4.26921e-4 months <br /> CST, BFN declared a Notification of Unusual Event (NUE) for Unit 3 due to a'loss of offsite power greater than 15 minutes and notified NRC in accordance with 10 CFR 50,72(a)(3). At 1136 hours0.0131 days <br />0.316 hours <br />0.00188 weeks <br />4.32248e-4 months <br /> CST, following the restoration of the offsite power to Unit 3, BFN terminated the NUE, and in accordance with 10 CFR 50,72 (c)(1)(iii) notified.NRC. The root cause of this event was the sensitivity of the auxiliary tripping relays. TVA has replaced the relays involved in the event with less sensitive relays. TVA is currently replacing other Westinghouse AR type relays, in similar applications with less sensitive relays. This event is being reported accordance with 10 CFR 50.73 (a)(2)(iv), as any event or condition that resulted in manual or automatic actuation of any engineered safety feature including the reactor protection system.
9704150185 970I/)04 PDR -
ADQCK 0500029b S PDR NRC FORM 366 (4-96)
~I JJRC FORM 3CCA U.S. JJIJCLEAR REOULATORY COMJISSION
'(44r5)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACII(ZTY NAME LER NUMBER NUMBER NUMBER Browns Ferzy Unit 3 05000296 2 of 8 97 001 00 more space reqrer ~ use s oos copes orm (17)
- z. PLMT CONDZTZONS Unit 1 was shutdown and defueled; Unit 2 was at 100- percent, power
,(3290 megawatts thermal) and'naffected by the event. Unit 3 was shutdown in a scheduled refueling outage with the reactor head removed'. The refueling cavity was flooded and the fuel gates were removed. No fuel movement was ongoing at,,the time of the event and the control rods [AA] were fully inserted. The Unit 3 500 KV [EL]
Transformer Bank was out of service for planned. maintenance, so relying on the 1'61'V [EL], power system foz offsite power.
it was ZZ. DESCRZPTZON OF EVENT A Event On March 5, 1997, at 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> Central Standard Time (CST), Unit 3 received engineered safety feature system. actuations (ESF) [JE]
due to a loss of offsite power. The loss of power was the zesult of the loss of both the Athens and Trinity 161'V power lines.
This was followed by the start of Emergency Diesel Generators (EDGs),[E J] .
At approximately 1039 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.953395e-4 months <br /> CST, following initial installation of an Emergency, Bearing Oil Pump [P][SI] foz,the 3B Reactor Feed Pump [SJ], as part of a Feedwater System upgrade, the pump was successfully electrically bumped to verify correct pump rotation.
Following successful verification of puny rotation, the pump was given a start signal. ~Within a few seconds it appazent that an electrical fault had occurred within the pump became visually motor '[MO], and it was shutdown from a local panel.
At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br /> CST, due to the fault in the pump motor, the Athens and Trinity 161 KV power lines tripped resulting in a 1'oss of offsite power to Unit 3. Emergency Diesel Generators 3A, 3C, and 3D automatically started and: tied to their respective shutdown boards. Emergency Diesel Generator 3B and its respective shutdown board was,under administrative hold for planned maintenance activities and did not respond to the event.
Additionally, the loss of offsite power resulted in the Unit 3 reactor scram si'gnal and the initiation of'everal unplanned This included de-enezgization of the Unit 3 Reactor .ESF'ctuations.
Protection System (RPS) [JC]. The loss of RPS resulted in actuation or isolation of the 'Primary 'Containment Isolation System [JE] (PCIS) systems/components.
~ PCIS Group 1, .Main Steam Line Drain Isolation Valve [SB] [ISV]
close signal
~ PCIS Group 2, Shutdown cooling mode of Residual Heat Removal
[BO] system; Drywell floor drain isolation valve, Drywell equipment drain sump isolation valve [WP]
NRC FORM 366A (4W5)
NRC FORMSCCA U.S. NUCLEAR REOULATORY COIVMSSION (405)
LICENSEE EVENT REPORT (LER)
TEXT CONTZNUATZON FACILITY NAME LER NUMBER NUMBER NUMBER Browns Ferry Unit 3 05000296 3 of 8 97 001 00 more space requ<r, use s copes orm (17)
~ PCZS Group 3, Reactor Water Cleanup [CE]
~ PCZS Group 6, Primary Containment Purge and Ventilation [JM]';
Unit 3 Reactor Zone Ventilation [VB]; Refuel Zone Ventilation
[VA]; Standby Gas Treatment (SGT),[BH] system; Control Room Emergency Ventilation (CREV)[VZ]
~ PCIS Group 8, Transverse Incoze Probe [IG] withdrawal signal Additionally, the Spent Fuel Pool Cooling System. [DA] Pumps tripped on undervoltage.
The affected systems were returned to pze-event alignment by 1138 hours0.0132 days <br />0.316 hours <br />0.00188 weeks <br />4.33009e-4 months <br /> CST. All systems responded as expected during the loss of offsite power and subsequent reactor scram signal.
This event is reportable in accordance with 10 CFR 50.73 (a)(2)(iv), as any event or condition that resulted in manual or automatic actuation of any engineered safety feature including the reactor protection system.
B. Zno rable Structures, nents, or stems that Contributed to e Event:
During the event, the Unit 3 Main Bank 500 KV Transformer was out of service for planned maintenance, and Unit 3 was relying on the 161 KV power lines for offsite power. Had the Unit 3 Main Bank 500 KV Transformer been in service during the event, the loss of the 161 KV power lines would not have resulted in the loss of offsite power to Unit 3.
C. Dates and roximate Times of Ha or Occurrences:
March 5, 1997 at 1040 CST Unit 3 experienced a loss of offsite power resulting in a full xeactor scram signal.
March 5, 1997 at 1122 CST TVA declared a Notice of Unusual Event (NUE) on Unit 3 due to a loss of offsite power. TVA made a one hour notification in accordance with 10 CFR 50.72(a)(3).
March 5, 1997 at 1131 CST TVA made a 4 hour nonemezgency notification to NRC in accordance with 10 CFR 50.72(b)(2)(ii) ~
NRC FORM 386A (405)
Il Al
'RC FORM 366A U.S. NUCLEAR REOULA')ORY COMWSSION (44r5)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACZLZTX KAME NUM88R NVM88R Browns Ferry Unit 3 05000296 4 of 8 97 001 00 more space is requir, use s orrs copies oim 1 )
March 5, 1997 at 1136 CST Following successful restoration of offsite power, TVA terminated the NUE. Follow-up notification for termination of the NUE was made in accordance with 10 CFR 50.72 (c) (1) (iii) .
D. Other S stems or Secon Functions Aff'ected:
None.
E. Method of Discove The Unit 3 operator received numerous main control room alarms indicating the loss of the 161 KV Athens and Trinity power lines.
This was followed by indications that a ful'l reactor scram signal had been generated, and EDGs 3A, 3C, and 3D had started and tied to their respective shutdown boards.
orator Actions:
Operator actions taken during- this event were as expected.
Operations responded .to the loss of offsite power to Unit 3 using the applicable portions of Abnormal Operating Instzuctions 0-AOI-57-1A; Loss of Offsite Power (161 And 500 KV)/Station Blackout, 3-AOI-99-1; Loss Of Power to One RPS Bus, 3-AOI-100-1; Reactor Scram and Emergency Plan -Implementing Procedure (EPIP), EPIP-1, Emergency Classification Procedure.
G. Safet S stem Re nses:
The safety systems listed in section IIA of this report 'responded to the loss of offsite power as designed.
CAUSE OF THE EVENT A. Immediate Cause:
The loss of offsite power and subsequent scram were initiated by a failure of a conductor in the Emergency Bearing Oil Pump for the 3B Reactor Feed Pump. The conductor came in contact with the rotor in the motor thus causing a ground fault in a 250 volt Non-1E direct current (VDC) [EI] circuit.
The failure was the result of poor craftsmanship. An individual
[contract, electrician] terminating the power leads for the 3B Reactor Feed Pump Emergency Bearing Oil Pump did not exhibit due care in his work. After terminating the power feed conductors to the motor conductors, the individual replaced them into the motor housing.
NRC FORM 368A (4M)
0 NRC FORIVI 3QCA U.S. NUCLEAR REOULATORY COIVIVIISSION (44)5)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACZLITX NAME DOCKET LER NUMBER NUM88R NUMSKR Browns Ferry Unit 3 05000296 5 of 8 97 -- 001 -- 00 more space is requfr ~ Use a eris copies This type of motor does not have a termination box, and the conductors are normally terminated and then placed back in the motor housing. In placing the conductors back in the housing, the electrician allowed one of the conductors to be placed into the rotor portion of the motor. 'Subsequently, when .the motor was started, the resulting contact of the conductor with the rotor severed the conductor causing a ground in the motor power circuit.
The motor involved in the event is a 7.5 horsepower 250 VDC motor. During the event, no breaker tripped or fuse cleared as a result of the ground fault. TVA determined analytically that a fault current of approximately 450 amps for 0.2 seconds occuzred.
Under these conditions, this is an expected response.
B. Root Cause:
The root cause of this event was the sensitivity of the auxiliary tripping relays [94]. These relays, (Westinghouse AR type) are 250 VDC fast acting relays used as tripping relays in the circuits involved in this event.
TVA's investigation into this event has determined that based on vendor information Westinghouse AR type relay can operate in approximately 2 milliseconds at current as low as 20 milliamperes. The relay can operate due to transient current flow caused by a ground on a circuit with long cable runs where capacitance has developed which can discharge through ground.
Initially personnel responding to the event found no indication of protective relay [94] operation. Furthermore, there was no indication that the protective relays that would normally operate due to a fault on the 161 KV system had operated. However, upon further investigation, lockout relays were found tripped at the cooling tower switchgear. Personnel found the ground switches in the 161 KV switchyard for both the Athens and the Trinity lines closed indicating the auxiliary tripping relays had operated and the main breakers open.
C. Contributin Factors:
Circuit capacitance of the field cables contributed in the event.
TVA believes that the relay actuation occurred because of the ground in the 3B Reactor Feed Pump Emergency Bearing Oil Pump motor resulting in a transient voltage to actuate the auxiliary relays. TVA developed an equivalent circuit of the schematic and modeled the circuit utilizing computer software. By simulating the event, TVA found that this type of relay would actuate with a ground at the 3B Reactor Feed Pump Emergency Bearing Oil Pump motor followed by separation of the motor conductor.
NRC FORM 366A (4M)
'\
~\
'RC T
(405)
'.S.
FORM 3CSA ZACILZTZ HAMS Browns Ferry more space re Unit requrr, 3
use e LICENSEE'VENT oopee 05000296 OAll 1 )
'REPORT CONTINUATZON
'97 (LER)
NUMBER 001
'EXT NUCLEAR REOULATORY COIVMSSION.
NUMBER, 00 6 of 8 The computer simulation indicated that the current that caused relays to. operate was through the capacitance to ground in long.-
field'ables (approximately 2000-4500. feet) into the grounded 3B Reactor Feed Pump 'Emergency Bearing Oi:1 Pump motor conductor through the motor field'nductance (field, armature or both) and through the relay coil. The capacitance to ground discharged when the grounded. motor leads separated which resulted in .a voltage spike on the control'i:rcuit causing the operation of four AR type relays. TVA has determined -based on .field testing that the minimum operating voltage foz this type of'elay is 59 volts. DC.
Additionally, TVA has found that a,transient on one 250 non-, 1E.
VDC circuit has the potential to trip both the Athens and Tzinity 161 KV power lines. The motor that failed was powered from battery .board 4, the same battery board'hat suppl'ied'ontrol power to the Athens and Trinity protective relays. The failed motor conductor placed a ground on the battery board, resulting in a .transient which operated protective relays.
This operation resulted in the loss of both the Athens and.
Trinity. 161 KV power lines and operation of .two 500 KV power circuit breakers. The operation of the two 500 KV,.power circuit breakers had no impact on, plant operation.
'ANALYSZS OF THE EVENT Bzowns Ferry is analyzed in Chapter 14 of the Updated Final Safety Analysis Report for a loss of offsite power assuming a starting point of greater than 100'b reactor power. In this instance, the loss, of offsite power occurred while Unit 3 was in scheduled refueling outage.
Consequently, this event had minimal impact on Unit 3 and no impact on Unit .2 operati;on. Additionally, affected components functioned as designed. Thus, this event is bounded by the plant safety analysis and had no impact on the safety of the plant, its personnel, or the public.,
CORRECTZ'.~~ ACTZONS A. Zmmediate .Corrective Actions:
Offsite'ower was restored to Unit 3. Other affected systems were returned to their pre-event status. 'The motor was inspected and meggered to verify no internal damage. The motor conductors were zetezminated and the pump successfully operated.
Modifications .activities associated with DC pump motor iristallation was 'stopped. TVA Modifications Management met with the appropriate craft personnel to discuss the event, emphasizing the significance of the event, reinforcing safety and quality craftsmanship.
NRC FORM 3MA (~)
Ik jl
~1
HRC FORM366A U.S. NUCLEAR REGULATORY COMVlSSION (485)
LICENSEE EVENT REPORT. (LER)
'EXT CONTINUATION PACZLITZ 'NAME DOCKET PAGE NUMBER NUMBER Bzowns Ferry Unit 3 05000296 7'of 8 97 001 00 Illoce space Is foqos ~ Uso a as copes cell t ).
B. Corrective Actions to Prevent, Recurrencet TVA has replaced the relays, that were involved in the loss of offsite power with"less. sensitive relays. 'TVA is c'urrently replacing the Westinghouse AR type relays in similar appl'ications with less sensitive relays.
'TVA will evaluate the current 161 KV and 500 KV protective relay functions for possible design changes .
vz. ADDZTZONAL ZNFORMATZON A. Failed onents:
None.
B. Previous LERs on Similar Eventst LER 259/85003 di'scusses an event in which a perturbation on a non-1E 250 VDC power system actuated relays and resulting in start of EDGs. On February 5, 1985, during functional'esting of the protective rel'ays for the Unit '2'tation Service. Transformers
[XPT] and Main Generator [GEN], a voltage spike was generated when connecting test equipment which resulted'in the operati'on of high speed tripping relays. 'This resulted in the tripping of the both 161 KV lines (two '500 KV 'Power Circuit Breakers) and a brief ~
undervoltage condition on Shutdown Boards C and D. 'This resulted in Units 1 and 2 .EDGs C and, D starting. Because the undervoltage condition. was brief, the EDGs did not tie to the Shutdown Boards.
The cause of this event was attributed to the 250 VDC battery board .bus filter being, inoperable.. The investigation team was able to repeat the, event with the battery .board bus filter inoperable. However, with the 250 VDC battery board bus filter operable,, the voltage spike would not actuate the relays. The Westinghouse, AR type fast acting relays could have contributed in this event. An evaluation of the relays was performed 'to see This evaluation resulted if they need replacement or desensitized.
in a design change request that was not implemented. Based on the cause and, contributing factors of this event, TVA determined BFN could be safely operated without replacement of these type relays.
TVA does aot coasidez this cozzective action a Regulatozy Cctsaitmeat. TVA's cozzective actioa pzogzaa will tzack cocpletioa of the actioa.
NRC FORM 366A (495)
II II
l' NRC FORM 3QCA U.S. NUCLEAR REOULA'IQRY COWISSION
(~)
'ICENSEE EVENT REPORT (LER)
TEXT CONTINUATION ZACZLZTZ ?RIME NUMBER NUMBER Bzowns Ferry Unit 3 05000296 8 of 8 97 '01 ~ 00 IIIOfO SPOCO IO fOqUlf ~ USO Il Ol4l OOPIOS Onn 17)
VZZ . COMHZTMENTS TVA will complete the replacement of the Westinghouse AR type relays in similar applications with less sensitive relays by June 1, 1997.
Energy Industry Identification System (EIIS) system and component codes are identified in'he text with brackets (e.g., [XX]).
NRC FORM 36BA (445)
Il II
'ii'