05000387/FIN-2015004-04
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Finding | |
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Title | Inadvertent Closure of the B Inboard MSIV |
Description | A self-revealing finding of very low safety significance (Green) was identified when Susquehanna did not correctly validate a deficient condition associated with the Unit 1 B inboard main steam isolation valve (MSIV) direct current (DC) solenoid valve as an actual valve issue, vice indication-only, through the use of specific acceptance criteria as required by MT-AD-509, Control of Minor Maintenance Activities. By incorrectly concluding the issue was indication only, testing was allowed to be performed which inserted a half-isolation by de-energizing the alternating current (AC) solenoid valve on the B inboard MSIV. When this maintenance was performed, the B inboard MSIV closed unexpectedly, resulting in a reactor scram. The cause of the closure was the failure of the DC solenoid valve on the B inboard MSIV. Susquehanna entered the issue into the CAP as CR-2015-30721 and replaced the DC solenoid for the B MSIV. The finding is more than minor because it is associated with the equipment performance attribute of the Initiating Events cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during power operations. Specifically, the maintenance activity performed to validate the DC solenoid valve continuity was inadequate and as a result the testing was allowed to be performed which relied on DC solenoid valve continuity to prevent an MSIV closure. The inadvertent closure of the B inboard MSIV resulted in a high pressure scram. The inspectors evaluated the finding in accordance with IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, for the Initiating Events cornerstone. The inspectors determined the finding was of very low safety significance (Green) because it did not cause the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Specifically, the condenser was maintained for decay heat removal via the bypass valves through the other three main steam lines following the trip. This finding had a cross-cutting aspect in the area of Human Performance, Challenge the Unknown, because Susquehanna did not stop when faced uncertain conditions and instead rationalized unanticipated test results. Specifically, the investigation of the extinguished continuity monitor focused on the possibility that it was an indication-only issue and failed to question the acceptability of the current values obtained during troubleshooting [H.11]. |
Site: | Susquehanna |
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Report | IR 05000387/2015004 Section 4OA3 |
Date counted | Dec 31, 2015 (2015Q4) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | C Graves D Schroeder E Gray J Deboer J Grieves N Embert S Barr T Daun T Fish P Meier |
CCA | H.11, Challenge the Unknown |
INPO aspect | QA.2 |
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Finding - Susquehanna - IR 05000387/2015004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Susquehanna) @ 2015Q4
Self-Identified List (Susquehanna)
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