Similar Documents at Perry |
---|
Category:NRC Preliminary Notification of Event/Occurrence
MONTHYEARPNO-III-18-002, Beaver Valley, Davis-Besse, Perry Notification of Bankruptcy Filing by Firstenergy Solutions2018-04-0404 April 2018 PNO-III-18-002: Beaver Valley, Davis-Besse, Perry Notification of Bankruptcy Filing by Firstenergy Solutions PNO-III-16-002, Perry Nuclear Power Plant: Unplanned Shutdown Greater than 72 Hours Due to Spurious Opening of Safety Relief Valves and Subsequent Plant Restart2016-02-18018 February 2016 PNO-III-16-002 Perry Nuclear Power Plant: Unplanned Shutdown Greater than 72 Hours Due to Spurious Opening of Safety Relief Valves and Subsequent Plant Restart PNO-III-16-001, A, Perry Nuclear Plant, Unplanned Shutdown Greater than 72 Hours Due to Reactor Coolant System Leakage Exceeding Technical Specification Limits and Subsequent Plant Restart2016-02-0505 February 2016 PNO-III-16-001A, Perry Nuclear Plant, Unplanned Shutdown Greater than 72 Hours Due to Reactor Coolant System Leakage Exceeding Technical Specification Limits and Subsequent Plant Restart ML16032A3942016-01-29029 January 2016 PNO-III-16-001 Perry Nuclear Power Plant, Unplanned Shutdown Greater than 72 Hours Due to Reactor Coolant System Leakage Exceeding Technical Specification Limits ML14316A5802014-11-12012 November 2014 PNO-lll-14-011: Unplanned Shutdown Greater than 72 Hours Due to a Loss of Feedwater ML14301A0342014-10-27027 October 2014 PNO-lll-14-009A Update to Unplanned Shutdown Greater than 72 Hours Due to a Loss of Feedwater PNO-III-14-009, Perry Nuclear Power Plant - Unplanned Shutdown Greater than 72 Hours Due to a Loss of Feedwater2014-10-24024 October 2014 PNO-III-14-009: Perry Nuclear Power Plant - Unplanned Shutdown Greater than 72 Hours Due to a Loss of Feedwater PNO-III-14-004, Perry Nuclear Power Plant Notification of Unusual Event Due to Toxic Chemical Leak2014-04-0303 April 2014 PNO-III-14-004: Perry Nuclear Power Plant Notification of Unusual Event Due to Toxic Chemical Leak ML13169A3672013-06-18018 June 2013 PNO-lll-13-005, Perry Nuclear Power Plant Shutdown Greater than 72 Hours Due to a Pressure Boundary PNO-III-13-001, Unplanned Shutdown Greater than 72 Hours Due to an Automatic Reactor Protection System Actuation2013-01-29029 January 2013 PNO-III-13-001, Unplanned Shutdown Greater than 72 Hours Due to an Automatic Reactor Protection System Actuation PNO-III-12-017, Perry Nuclear Power Plant Unusual Event Declared After Carbon Monoxide Detectors Alarmed in the Radwaste Building Control Room2012-11-29029 November 2012 PNO-III-12-017 - Perry Nuclear Power Plant Unusual Event Declared After Carbon Monoxide Detectors Alarmed in the Radwaste Building Control Room PNO-III-12-005, Perry Unplanned Shutdown Greater than 72 Hours2012-06-19019 June 2012 PNO-III-12-005 - Perry Unplanned Shutdown Greater than 72 Hours PNO-III-11-012, A - Perry Unplanned Shutdown Greater than 72 Hours (Update)2011-10-19019 October 2011 PNO-III-11-012A - Perry Unplanned Shutdown Greater than 72 Hours (Update) ML1127801372011-10-0505 October 2011 PNO-III-11-012 - Perry - Unplanned Shutdown Greater than 72 Hours PNO-III-10-006, A: Perry, - Update - Manual Reactor Scram Due to Loss of Control Rod Drive Charging Water Header Pumps2010-05-19019 May 2010 PNO-III-10-006A: Perry, - Update - Manual Reactor Scram Due to Loss of Control Rod Drive Charging Water Header Pumps ML1013407362010-05-14014 May 2010 PNO-III-10-006-Perry-Manual Reactor Scram Due to Loss of Control Rod Drive Charging Water Header Pumps PNO-III-10-005, A - Perry - Update - Turbine-Driven Feedwater Pump Fire Caused by Leak in Lube Oil System2010-03-31031 March 2010 PNO-III-10-005A - Perry - Update - Turbine-Driven Feedwater Pump Fire Caused by Leak in Lube Oil System PNO-III-09-012, A: Perry, Manual Reactor Scram During Planned Shutdown (Update)2009-11-0303 November 2009 PNO-III-09-012A: Perry, Manual Reactor Scram During Planned Shutdown (Update) ML0929203402009-10-19019 October 2009 PNO-III-09-012: Perry, Manual Reactor Scram During Planned Shutdown PNO-III-07-015, A: Perry, Update to Scram at Perry Nuclear Power Station and Feedwater Loss2007-12-0606 December 2007 PNO-III-07-015A: Perry, Update to Scram at Perry Nuclear Power Station and Feedwater Loss ML0733212692007-11-28028 November 2007 PNO-III-07-015: Scram at Perry Nuclear Power Station and Feedwater Loss PNO-III-07-009, A: Perry: Update to Unexpected Reactor Shutdown Exceeding 72 Hours Due to Problem with Reactor Recirculation Pump Motor2007-07-24024 July 2007 PNO-III-07-009-A: Perry: Update to Unexpected Reactor Shutdown Exceeding 72 Hours Due to Problem with Reactor Recirculation Pump Motor ML0718606072007-07-0505 July 2007 PNO-III-07-009: Perry: Unexpected Reactor Shut Down Exceeding 72 Hours Due to Problem with Reactor Recirculation Pump Motor PNO-III-06-016, Perry Nuclear Power Plant Unusual Event Declared Due to Earth Quake2006-06-21021 June 2006 PNO-III-06-016 Perry Nuclear Power Plant Unusual Event Declared Due to Earth Quake PNO-III-06-009, Perry Nuclear Power Plant Low Level Tritium Identified in Underdrain System2006-04-0606 April 2006 PNO-III-06-009 - Perry Nuclear Power Plant Low Level Tritium Identified in Underdrain System PNO-III-04-015, Perry Nuclear Power Plant, Inadvertent Discharge of CO2 Fire Protection System in Turbine Building2004-11-12012 November 2004 PNO-III-04-015: Perry Nuclear Power Plant, Inadvertent Discharge of CO2 Fire Protection System in Turbine Building PNO-III-04-014, Perry Nuclear Power Plant, Chemical Spill in Water Treatment Building2004-11-0404 November 2004 PNO-III-04-014: Perry Nuclear Power Plant, Chemical Spill in Water Treatment Building PNO-III-04-007, Perry, Alert Declared Because of Malfunctioning Radiation Monitor2004-07-20020 July 2004 PNO-III-04-007: Perry, Alert Declared Because of Malfunctioning Radiation Monitor PNO-III-03-022, Perry-Alert Declared Due to High Radiation Alarm in Fuel Handling Building2003-04-24024 April 2003 PNO-III-03-022: Perry-Alert Declared Due to High Radiation Alarm in Fuel Handling Building PNO-III-02-039, Reactor Scram During Main Turbine Testing Leads to Shutdown Greater than 72 Hours2002-09-23023 September 2002 PNO-III-02-039: Reactor Scram During Main Turbine Testing Leads to Shutdown Greater than 72 Hours 2018-04-04
[Table view] |
Text
PRELIMINARY NOTIFICATION January 29, 2016 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-16-001 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated and is basically all that is known by the Region III staff on this date.
Facility Perry Nuclear Power Plant FirstEnergy Nuclear Operating Company Perry, OH Docket No.: 05000440 License No.: NPF-58 Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable
SUBJECT:
UNPLANNED SHUTDOWN GREATER THAN 72 HOURS DUE TO REACTOR COOLANT SYSTEM LEAKAGE EXCEEDING TECHNICAL SPECIFICATION LIMITS On January 23, 2016, at 2100 EST, the Perry Nuclear Power Plant commenced a controlled plant shutdown due to an increasing trend in reactor coolant system leakage in the drywell. At 2122 EST leakage exceeded Technical Specification limits. On January 24, 2016, at 1007 EST with the plant at approximately 8 percent power, plant operators placed the motor-driven feedwater pump in service. During this operation, the reactor water level rose to the reactor trip set points. The reactor protection system auto-initiated, as designed, scramming the reactor.
The licensee continues to investigate the cause for the feedwater transient and reactor water level rise.
Following the plant shutdown, licensee personnel entered the drywell and identified the leak on recirculation loop 'A' pump discharge valve vent line. As required by Technical Specifications, on January 24, 2016, at 2059 EST the plant was cooled down to Mode 4 to conduct repairs.
The leakage was contained in the plant. There was no impact on public health.
The State of Ohio has been notified.
This preliminary notification is issued for information only.
The Resident inspector responded to the control room to monitor plant parameters and licensee actions. The NRC resident staff assisted by inspectors from the NRC Region 3 Office monitored licensee actions to identify the leak and continue to monitor the repair activities.
The information presented herein has been discussed with the licensee, and is current as of
4:10 p.m. EST on January 29, 2016.
ADAMS Accession Number: ML16032A394
Contact: B. Dickson (630) 829-9827 Billy.Dickson@nrc.gov
PRELIMINARY NOTIFICATION January 29, 2016 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-16-001 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated and is basically all that is known by the Region III staff on this date.
Facility Perry Nuclear Power Plant FirstEnergy Nuclear Operating Company Perry, OH Docket No.: 05000440 License No.: NPF-58 Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable
SUBJECT:
UNPLANNED SHUTDOWN GREATER THAN 72 HOURS DUE TO REACTOR COOLANT SYSTEM LEAKAGE EXCEEDING TECHNICAL SPECIFICATION LIMITS On January 23, 2016, at 2100 EST, the Perry Nuclear Power Plant commenced a controlled plant shutdown due to an increasing trend in reactor coolant system leakage in the drywell. At 2122 EST leakage exceeded Technical Specification limits. On January 24, 2016, at 1007 EST with the plant at approximately 8 percent power, plant operators placed the motor-driven feedwater pump in service. During this operation, the reactor water level rose to the reactor trip set points. The reactor protection system auto-initiated, as designed, scramming the reactor.
The licensee continues to investigate the cause for the feedwater transient and reactor water level rise.
Following the plant shutdown, licensee personnel entered the drywell and identified the leak on recirculation loop 'A' pump discharge valve vent line. As required by Technical Specifications, on January 24, 2016, at 2059 EST the plant was cooled down to Mode 4 to conduct repairs.
The leakage was contained in the plant. There was no impact on public health.
The State of Ohio has been notified.
This preliminary notification is issued for information only.
The Resident inspector responded to the control room to monitor plant parameters and licensee actions. The NRC resident staff assisted by inspectors from the NRC Region 3 Office monitored licensee actions to identify the leak and continue to monitor the repair activities.
The information presented herein has been discussed with the licensee, and is current as of
4:10 p.m. EST on January 29, 2016.
ADAMS Accession Number: ML16032A394
Contact: B. Dickson (630) 829-9827 Billy.Dickson@nrc.gov