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ACCELZMTED DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8802230392 DOC.DATE: 88/02/15 NOTARIZED: NO DOCKET g
FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH.NAME AUTHOR AFFILIATION DAVISON,W.S.
Washington Public Power Supply System POWERS,C.M.
Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-001-00:on 880118,Reactor protective systm automatic actuation during plant shutdown due to inadequate procedure.
W/8 ltr.
DISTRIBUTION CODE:
ZE22D COPIES RECEIVED:LTR i ENCL
/
SIZE: ~
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT ID CODE/NAME PD5 LA SAMWORTH,R COPIES LTTR ENCL 1
1 1
1 RECIPIENT ID CODE/NAME PD5 PD COPIES LTTR ENCL 1
1 8
A INTERNAL: ACRS MICHELSON AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS NRR/DEST/ELB NRR/DEST/MEB NRR/DEST/PSB NRR/DEST/SGB NRR/DLPQ/QAB NRR/DREP/RAB NRR/IDRIS/S IB
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'ES/DRPS DIR FORD BLDG HOY,A LPDR NSIC HARRIS,J 2
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TOTAL NUMBER OF COPIES REQUIRED:
LTTR 46 ENCL 45
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NRC Form 366 (94)3)
LICENSEE EVENT REPORT (LER)
V.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31604101 EXPIAES: 8/31/88 FACILITYNAME (Il Washington Nuclear Plant - Unit 2 TITLE (4)
Due to Inadequate Procedure DOCKET NUMBER (2)
PAGE 3
0 5
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0 3 g 7
1 OF EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED(8)
MONTH DAY YEAR YEAR @. SEGUENTIAL 'or%
'UMSER REVISION NUMBER MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S) 0 5
0 0
0 0
1 1
8 8 8 8 8 00 1
15 88 0
5 0
0 0
OPERATING 3
MODE (9)
POWER LEUEL 0 0 0
(10) cS".
v 20.402(8) 20A05(e) (I)(ll 20.405 (4)(I)(8) 20.405(e) IS)Alii 20A06(e) (1)(lv) 20.405(c) (1)(r) 20.406(c) 50M(c)11) 50.36(c) (2) 50.73(el(2) (I) 50.73(e)(2)(il) 50.73(e l(2)(illl LICENSEE CONTACT FOR THIS LER (12) 50,73(e) I2)(iv) 50.73(e I(2)(vl 50.73(e) (2) Ivll) 50.73(e) (2)(vill)(A) 50.73(e) (2) (rl5)(B) 50.73(e) (2) Ixl THIS REPORT IS SUBMITTED PURSUANT T0 THE REDUIREMENTs oF 10 cF A Q (check one or more of the foflovffnPI (11) 73.71(8) 73.71(cl OTHER (Specify In Ahttrect helovr end In Text, HRC Form SSBAI NAME W.S.
Davi son, Comp 1 iance Engineer TELEPHONE NUMBER ARFA CODE 50 37 7-'01 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
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SYSTEM COMPONENT L
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CAUSE
SYSTEM COMPONENT MANUFAC.
TVRER EPORTABLE TO NPRDS N3%~%"
H&AII SUPPLEMENTAL REPOAT EXPECTED (14)
EXPECTED SUBMISSION DATE 05)
MONTH DAY YEAR YES (Ifyet, compfete EXPECTED SIIBhtISSIOH DATEI NO ABSTRACT (Lfmltto f400 tpecet, I.e., epproxfmetefy fifteen tinple-tpece typerrrftten (Inn( (16)
Abstract On January 18, 1988, at 1354 hours0.0157 days <br />0.376 hours <br />0.00224 weeks <br />5.15197e-4 months <br />, following a plant shutdown, an automatic Reactor Protective System (RPS) actuation occurred due to an actual low Reactor Pressure Vessel (RPV) water level condition.
While the plant was being maintained in the Hot Shutdown Condition with the Hain Steam Isolation Valves closed, a main steam Safety Relief Valve (SRV) was opened to preclude approaching the automatic reactor high pressure RPS actuation setpoint of 1037 psig.
While the SRV was open, RPV water level swell effect caused level to increase above the RPV high water level setpoint which resulted in the automatic shutdown of the Reactor Core Isolation Cooling (RCIC) System.
This system was being operated to supply water to the RPV and assist in controlling RPV pressure.
When the RCIC System shut down, the decision was made to depressurize to 875 psig with an SRV.
After reaching the desired
- pressure, the SRV was closed, causing RPV level to drop from +40 inches to -5 inches.
The automatic low RPV level RPS actuation occurred as level decreased through the +13 inch setpoint.
During the event, a narrow range RPV level recorder pen stuck at the high end of the scale for approximately one minute.
The root cause of the event was procedural inadequacy.
Plant procedures did not contain sufficient information to adequately address the degree of difficulty involved in controlling reactor pressure with the plant in Hot Shutdown with the Hain Steam Isolation Valves (HSIV) closed.
The significant corrective actions include:
revision of Plant Procedures to include specific information concerning control of reactor pressure and level in Hot Shutdown with the HSIVs closed, inclusion of this event as a future simulator training scenario, required reading of this LER by licensed operators and comoletion of an evaluation of the need for a digital RPV level indicator at the reactor control console.
This event posed no threat to the safety of Plant personnel or the Public
~
)8802230392 '8802k 5 j DR:.ADOCK 05000397,(94)3)
LICENSEE EVENT REPORT {LER) TEXT CONTINUATION V.S. NUCLEAR REQVLATORYCOMMISSION APPROVEO OM8 NO. 3)50&)04 EXPIRES: 8/31/88 FACILITYNAME (11 DOCKET NUMBER (2)
LER NVMSER (6)
SEQUENTIAL g>f REVISION N U ME E R
")rr N UM6 6 R
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Washin ton Nuclear Plant - Unit 2 TEXT ///moro 4/Mco /4 I/U)rorLoff~ H/(C fomr36((4'4/ (17)
Plant Conditions
0 5
0 0
0 3 9788 001 0
0 0 2 OF 0 4
a)
Power Level -
OX b) Plant Mode
- - 3 (Hot Shutdown)
Event Descri tion Following a scheduled plant shutdown on January 18,
- 1988, an automatic Reactor Protective System (RPS) actuation occurred at 1354 hours0.0157 days <br />0.376 hours <br />0.00224 weeks <br />5.15197e-4 months <br /> due to an actual low Reactor Pressure Vessel (RPV) water level condition.
At the time of this RPS actuation, the reactor was shut down and the plant was being maintained in a hot condition with the Main Steam Isolation Valves (HSIVs) closed.
RPV level and pressure control were being maintained using the Reactor Core Isolation Cooling (RCIC) System and the Reactor Water Cleanup (RWCU) System.
Just prior to the event, it was noted by the Control Room Supervisor (CRS) that when RCIC was not injecting into the vessel, reactor pressure was rising at an approximate rate of 3 to 4 psig per minute.
When reactor pressure reached
'l020 psig, with reactor level at approximately 40 inches, the decision was made to lower reactor pressure to 875 psig using a Main Steam System (HS) Safety Relief Valve (SRV) to discharge to the pressure suppression pool.
This decision was based on preventing an automatic reactor high pressure RPS actuation at 1037 psig and to preclude the automatic actuation of SRVs.
Under direction of the CRS, in accordance with approved plant procedures, HS-RV-5B was opened and then reclosed.
RPV level subsequently
- swelled, due-to core void increase, to greater than +60 inches by narrow range level indication
(+50 inches on upset range, no increase on wide range),
causing the RCIC turbine steam admission valve (RCIC-V-45) to close at +54.5 inches (RPV Level 8).
This resulted in shutdown of RCIC, the system which was supplying water to the reactor vessel.
In accordance with approved Abnormal Condition Procedures, approximately ten seconds
- later, HS-RV-5B was reopened for about two minutes, dropping reactor pressure to 875 psig.
The basis for this action was to allow sufficient time for restart of the RCIC turbine in order to minimize SRV lifting prior to restoration of RCIC spray to control pressure.
When HS-RV-5B was closed, reactor level dropped from +40 inches to -5 inches.
As level decreased through
+13 inches, a reactor low level (RPV Level 3) automatic RPS actuation occurred.'mmediate
Corrective Action
The plant operators responded in accordance with Plant Procedures by promptly restarting the RCIC System to supply feedwater to the RPV.
Reactor level was restored to greater than
+13 inches at 1403 hours0.0162 days <br />0.39 hours <br />0.00232 weeks <br />5.338415e-4 months <br />.
Further Evaluation and Corrective Action o
This event is being reported as an automatic actuation of an Engineered Safety Feature per the requirements of 10CFR50.73(a) (2) (IV).
NRCPQRM 346A (943)
- V.S GPO 1986 0 624 538/455
NRC form 358A (SS3)
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROV EO OMS NO, 3(50M)DE EXPIRES: 8/31/88 FACILITYNAME ()I Washin ton Nuclear Plant - Unit 2 TEXT ///more EF>>c>> S>>>>)M)er/ rr>>>> ac /I/O/I>>/HRCForm 3//Sl3/117)
DOCKET NUMSER (21 0
5 0
0 0
3 9
LER NUMSER LS)
SEOVENTIAL NVMEER
+~ REVISION
" NVM ER PACE (3)
OF o
The immediate cause of this event was opening the SRV for a longer continuous period than necessary to control RPV pressure rise, thus allowing water inventory loss sufficient to cause a low RPV level RPS actuation.
The licensed senior reactor operator (CRS) did not anticipate the exact response of RPV level as a result of opening an SRV with no feed water being supplied to the RPV.
o The root cause of this event was determined to be inadequate procedures in that, approved Plant Procedures did not contain sufficient information to adequately address the degree of difficulty involved in controlling reactor pressure and level with the plant in Hot Shutdown w'ith the Main Steam Isolation Valves closed.
Control of RPV level while isolated from the condenser with significant decay heat generation and the accompanying level swell-and-shrink transient effects during SRV operation were not 'addressed in detail by the Plant Procedures.
o Several contributing factors were identified as having some impact on the response to this event:
During the course of the initial RPV water level swel'l transient, the ink pen for the narrow range reactor level recorder stuck at the high end of the scale.
This provided the operators with an erroneous indication of actual RPV level from this recorder.
This instrument is one of four narrow range level indicators located on the Reactor Control Console and consequently did not have a major impact on the operational response to this event.
Previous to this event, the operator training program covered Hot Shutdown scenarios during simulator training; however, this particular event (i.e.,
Hot Shutdown with NSIVs closed and no high pressure water source) has not been stressed.
Lack of specific training relating to this scenario is considered a contributing factor.
o All automatic actions which should have been initiated at RPV Level 3 (+13 inches) did occur as designed.
The only actual operation of components that occurred were logic relay actuation and repositioning of valves for the reactor scram function of the Control Rod Drive (CRD) System.
No control rods were actually repositioned since they had been previously inserted fully into the core.
Other automatic functions which occurred are:
Reactor Recirculation Pumps received a signal to automatically shift to slow speed (15 hertz) operation.
This shift did not occur because both pumps were being operated at 15 hertz at the time of the event.
Nuc'lear Steam Supply Shutoff System (NS4) Groups 5 and 6 received an isolation signal.
No valves or components changed status because they were in the isolation position at the time of the event.
An Automatic Depressurization System (ADS) Low RPV Level 3 Confirmation Signal was generated.
This is one of two control logic RPV level functions required for the ADS initiation of seven Safety Relief Valves.
NRC FORM SEEA (8831
- U.S GPO.108S 082>> 538/>>55
NRC Form 388A (9031 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION U.S. NUCLEAR REQULATORY COMMISSION APPROVED OMB NO. 3150-0104 EXPIRES: 8/31/SS FACILITYNAME (I)
DOCKET NUMBER (2)
YEAR LER NUMBER (8)
SEQUENTIAL NUMSER REVISION NUMSER PACE (3)
Washington Nuclear Plant - Unit 2 TEXT//Imare g>>ce /e derr)her/. Iree I//aar>>///RC Arm3r/SA'f/ (13) o s
o o
o 3
9 7 8 8 001 0 004 oFo 4
o The narrow range reactor level recorder is a Model Ho. 732, manufactured by Bailey Instrument
- Company, GE MPL Number C34-R608.
This instrument was inspected,
- cleaned, calibrated and placed back into service.
These instruments ar e a known high maintenance item.
WNP-2 is in the process of evaluating qualified replacements for this type of recorder.
No further corrective action is planned.
o Plant procedures will be revised to include specific information concerning control of reactor pressure and level in Hot Shutdown with the MSIVs closed.
o A technical evaluation of the need for a digital RPV level indicator at the reactor control console wi 11 be performed.
o This LER will be required reading for all licensed operators at WNP-2 and will be added to the subject matter list for requalification training.
o This event scenario will be specifically covered as a part of future simulator requa1 ification training.
.Safet Si nificance The Reactor Protective System functioned correctly to cause an automatic actuation in response to an actual reactor vessel low level (Level 3) condition.
The faulty RPV narrow range level recorder reading was compensated for by valid readings on the vertical section of the reactor control console from three reactor narrow range level indicators.
With the reactor shut, down, the significant safety concern is potential uncovering of the fuel.
The top of active fuel is located at -161 inches vessel level.
Since the level transient was terminated at -5 inches, more than adequate vessel water inventory remained to assure fuel coverage.
This event posed no threat to the safety of Plant personnel or the public.
Similar Events
- - Hone.
EIIS Information Text Reference EI IS Reference System Component RPS RPV MSIV RCIC RWCU MS-RV-5B RCIC-V-45 Narrow Range Reactor Level Recorder JC
. SB SB BN CE SB BH SJ RPV ISV RV ISV LR NRC FORM Sddk L903) e U S OP(),)988.0.828 538/d 55
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WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968
~ 3000 George Washington Way
~ Richland, Washington 99352 Docket No.
50-397 February 16, 1988 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C.
20555
Subject:
NUCLEAR PLANT NO.
2 LICENSEE EVENT REPORT NO.88-001
Dear Sir:
Transmitted herewith is Licensee Event Report No.88-001 for the WNP-2 Plant.
This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Very truly yours, C.H.
Powers (H/D 927H)
WNP-2 Plant Hanager CHP:sm
Enclosure:
Licensee Event Report No.88-001 cc:
Hr. John B. Hartin, NRC Region V
Hr. C.J.
- Bosted, NRC Site (H/0 901A)
INPO Records Center Atlanta, GA Hs. Dottie Sherman, ANI Hr. D.L. Williams, BPA (H/D 399) ss "
P 72,y OR3 ft,t,
|
|---|
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| | | Reporting criterion |
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| 05000397/LER-1988-001, :on 880118,following Plant Shut Down,Automatic Reactor Protective Sys Actuation Occurred Due to Low Reactor Pressure Vessel Water Level Condition.Caused by Procedural Inadequacy.Plant Procedures Revised |
- on 880118,following Plant Shut Down,Automatic Reactor Protective Sys Actuation Occurred Due to Low Reactor Pressure Vessel Water Level Condition.Caused by Procedural Inadequacy.Plant Procedures Revised
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) | | 05000397/LER-1988-002, :on 880122,discovered RCIC Pump Suction Line Failed to Meet Containment Isolation & Single Failure Design Criteria.Caused by Ae Design Error.Check Valve Installed & Ltr Re Error Sent to B&R.Part 21 Related |
- on 880122,discovered RCIC Pump Suction Line Failed to Meet Containment Isolation & Single Failure Design Criteria.Caused by Ae Design Error.Check Valve Installed & Ltr Re Error Sent to B&R.Part 21 Related
| 10 CFR 50.73(e)(2) 10 CFR 50.73(s)(2) | | 05000397/LER-1988-003, :on 880204,reactor Scram Due to Main Steam Line Isolation Occurred.Caused by Personnel Error.Rcic Sys Manually Initiated to Restore & Maintain Water Level. Procedure Revised & Technicians Counseled |
- on 880204,reactor Scram Due to Main Steam Line Isolation Occurred.Caused by Personnel Error.Rcic Sys Manually Initiated to Restore & Maintain Water Level. Procedure Revised & Technicians Counseled
| 10 CFR 50.73(s)(2) 10 CFR 50.73(s)(2)(iii) | | 05000397/LER-1988-004, :on 880204,standby Liquid Control Pump 1B Inoperable for Longer than 7-day Period Allowed by Tech Specs.Caused by Procedural Inadequacy.Tech Specs Reviewed to Identify Any Similar Remaining Situations |
- on 880204,standby Liquid Control Pump 1B Inoperable for Longer than 7-day Period Allowed by Tech Specs.Caused by Procedural Inadequacy.Tech Specs Reviewed to Identify Any Similar Remaining Situations
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(e)(2)(vii) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(v) | | 05000397/LER-1988-005, :on 880208,determined That CR Emergency Filtration Sys,Train B Bypass Flow Greater than TS Limit of 0.05 Gpm from 870923-880120.Caused by Installation Deficiency.Flow Restrictor Installed |
- on 880208,determined That CR Emergency Filtration Sys,Train B Bypass Flow Greater than TS Limit of 0.05 Gpm from 870923-880120.Caused by Installation Deficiency.Flow Restrictor Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000397/LER-1988-006, :on 880213,series of Reactor Pressure Vessel Level Transients Resulted in Low Reactor Protective Sys Actuation Following Manual Scram.Caused by Procedural Inadequacy.Procedures Modified |
- on 880213,series of Reactor Pressure Vessel Level Transients Resulted in Low Reactor Protective Sys Actuation Following Manual Scram.Caused by Procedural Inadequacy.Procedures Modified
| 10 CFR 50.73(e)(2)(v) | | 05000397/LER-1988-007, :on 880214,rupture of Reactor Bldg Roof Occurred Due to HVAC Overpressurization Transient.Caused by Personnel Error.Equipment Operator Training Program & Investigative Process Being Developed |
- on 880214,rupture of Reactor Bldg Roof Occurred Due to HVAC Overpressurization Transient.Caused by Personnel Error.Equipment Operator Training Program & Investigative Process Being Developed
| 10 CFR 50.73(e)(2)(vii) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(iv) | | 05000397/LER-1988-008, :on 880318,determined That 11 Plant TS Fire Penetration Seals Discovered Impaired.Caused by Inadequate Control of Fire Seal Penetrations.Maint Work Requests Written to Repair Penetrations |
- on 880318,determined That 11 Plant TS Fire Penetration Seals Discovered Impaired.Caused by Inadequate Control of Fire Seal Penetrations.Maint Work Requests Written to Repair Penetrations
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(B) | | 05000397/LER-1988-009, :on 880401,standby Gas Treatment Sys Tech Spec Surveillances Not Performed within Time Limits.Caused by Personnel Error.Personnel Counseled & Procedure Revised to Provide Guidance When Surveillance Exceeded |
- on 880401,standby Gas Treatment Sys Tech Spec Surveillances Not Performed within Time Limits.Caused by Personnel Error.Personnel Counseled & Procedure Revised to Provide Guidance When Surveillance Exceeded
| 10 CFR 50.73(c)(2) 10 CFR 50.73(c)(2)(i) | | 05000397/LER-1988-010, :on 880430,nuclear Steam Supply Shutoff Sys Group 1 Isolation Occurred.Caused by Low Pressure in Main Steamlines W/Reactor Mode Switch in Run Position.Valve RFW-FCV-10B Repaired |
- on 880430,nuclear Steam Supply Shutoff Sys Group 1 Isolation Occurred.Caused by Low Pressure in Main Steamlines W/Reactor Mode Switch in Run Position.Valve RFW-FCV-10B Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) | | 05000397/LER-1988-011-02, :on 880501,reactor Protection Sys Actuation Occurred as Result of Reactor Pressure Vessel Low Water of +13 Inches.Caused by Personnel Error & Inadequate Design. Individual Involved Counseled |
- on 880501,reactor Protection Sys Actuation Occurred as Result of Reactor Pressure Vessel Low Water of +13 Inches.Caused by Personnel Error & Inadequate Design. Individual Involved Counseled
| | | 05000397/LER-1988-012, :on 880606,potential Existence of Unmonitored Radiological Effluent Release Path During Certain Emergency Conditions Determined.Cause Unknown.Fan Disabled.Part 21 Related |
- on 880606,potential Existence of Unmonitored Radiological Effluent Release Path During Certain Emergency Conditions Determined.Cause Unknown.Fan Disabled.Part 21 Related
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(c)(2) 10 CFR 50.73(r)(2) | | 05000397/LER-1988-013-01, :on 880512 & 13,loss of Power Occurred on Reactor Protection Sys (Rps).Caused by phase-to-ground Faults Due to Lightning.Rps Alternate Supply Electrical Protection Assembly Breaker & Logic Reset |
- on 880512 & 13,loss of Power Occurred on Reactor Protection Sys (Rps).Caused by phase-to-ground Faults Due to Lightning.Rps Alternate Supply Electrical Protection Assembly Breaker & Logic Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000397/LER-1988-014, :on 880512,RWCU Sys Resin Tank Spill Occurred. Caused by Open RWCU Sample Line Isolation Valves RWCU-V-442 & 443.RWCU-V-442 & 443 Tagged Shut & de-energized & Radwaste Control Room Operator Involved Counseled |
- on 880512,RWCU Sys Resin Tank Spill Occurred. Caused by Open RWCU Sample Line Isolation Valves RWCU-V-442 & 443.RWCU-V-442 & 443 Tagged Shut & de-energized & Radwaste Control Room Operator Involved Counseled
| | | 05000397/LER-1988-015, :on 880515,loss of Power to Reactor Protection Sys (RPS) Ocurred Due to Flooding of Reactor Cavity.Caused by Inadvertent Removal of Power to MC-7A.RPS Switched to Alternate Power Supply & RHR Cooling Restored |
- on 880515,loss of Power to Reactor Protection Sys (RPS) Ocurred Due to Flooding of Reactor Cavity.Caused by Inadvertent Removal of Power to MC-7A.RPS Switched to Alternate Power Supply & RHR Cooling Restored
| | | 05000397/LER-1988-016, :on 880518,reactor Protection Sys Actuation Ocurred.Caused by Error in Plant Design.Event Discussed in Mechanics Shop Meeting & Article Describing Event to Be Included in Prefuelling Outage Bulletin |
- on 880518,reactor Protection Sys Actuation Ocurred.Caused by Error in Plant Design.Event Discussed in Mechanics Shop Meeting & Article Describing Event to Be Included in Prefuelling Outage Bulletin
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000397/LER-1988-017, :on 880615,problems W/Limitorque Models SMB-000 & SMB-00 Discovered W/Potential Defective Switches.Caused by Design Problem.Investigation & Evaluation of Switch Problems Immediately Initiated.Part 21 Related |
- on 880615,problems W/Limitorque Models SMB-000 & SMB-00 Discovered W/Potential Defective Switches.Caused by Design Problem.Investigation & Evaluation of Switch Problems Immediately Initiated.Part 21 Related
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(v) | | 05000397/LER-1988-018, :on 880522,noted That Green Status Indicating Light for Div Two Emergency Diesel Generator Start Circuit Not Energized.Control Power Transfer Switch Was Not in Required Position.Switch Replaced |
- on 880522,noted That Green Status Indicating Light for Div Two Emergency Diesel Generator Start Circuit Not Energized.Control Power Transfer Switch Was Not in Required Position.Switch Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(e)(2) | | 05000397/LER-1988-019, :on 880527,determined That Control Room Emergency Filtration Sys Actuation Occurred on 880520.Caused by Technician Failure to Reset Trip Logic During Response Time Test Due to Inadequate Procedure |
- on 880527,determined That Control Room Emergency Filtration Sys Actuation Occurred on 880520.Caused by Technician Failure to Reset Trip Logic During Response Time Test Due to Inadequate Procedure
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(iv) 10 CFR 50.73(a)(1)(ii) | | 05000397/LER-1988-021, :on 880530,outboard Nuclear Steam Supply Shutoff Sys Group 6 Automatically Isolated.Caused by Inadvertent Removal of Trip Logic Circuit Fuse by Licensed Operator.Operator Counseled |
- on 880530,outboard Nuclear Steam Supply Shutoff Sys Group 6 Automatically Isolated.Caused by Inadvertent Removal of Trip Logic Circuit Fuse by Licensed Operator.Operator Counseled
| 10 CFR 50.73(e)(2) | | 05000397/LER-1988-022, :on 880616,violation of Fire Zone in Radwaste Bldg Cable Spreading Room.Caused by Missing thermo-lag Insulation Due to Personnel Error.Outline of 20 Ft non- Combustible Zone Will Be Taped on Floor |
- on 880616,violation of Fire Zone in Radwaste Bldg Cable Spreading Room.Caused by Missing thermo-lag Insulation Due to Personnel Error.Outline of 20 Ft non- Combustible Zone Will Be Taped on Floor
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(s)(2) | | 05000397/LER-1988-023, :on 880629,Tech Spec Violation of Secondary Containment to Outside Differential Pressure Occurred.Caused by Sys Configuration Error.Instrument Setpoint Change Request Initiated |
- on 880629,Tech Spec Violation of Secondary Containment to Outside Differential Pressure Occurred.Caused by Sys Configuration Error.Instrument Setpoint Change Request Initiated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000397/LER-1988-024, :on 880703,single Primary Containment Monitor Intermittently Exceeded 150 F Temp & Time Limit.Cause Contributed to Leaking Main Steamline Safety Relief Valves & Leaking Tailpipe Vacuum Breaker Valves |
- on 880703,single Primary Containment Monitor Intermittently Exceeded 150 F Temp & Time Limit.Cause Contributed to Leaking Main Steamline Safety Relief Valves & Leaking Tailpipe Vacuum Breaker Valves
| 10 CFR 50.73(e)(2) | | 05000397/LER-1988-025, :on 880708,discovered Instrumentation Channel Inoperable Due to Incorrect Wiring & Personnel Error.Caused by Failure of Shiftly Channel Check to Promptly Determine Inoperable Status of Channel |
- on 880708,discovered Instrumentation Channel Inoperable Due to Incorrect Wiring & Personnel Error.Caused by Failure of Shiftly Channel Check to Promptly Determine Inoperable Status of Channel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000397/LER-1988-026, :on 880715,determined That Sensing Line Support Hangers Would Not Withstand Design Basis Fire W/O Mod or Protection.Caused by Inadequate Design by Architect Engineer.Areas Placed on Hourly Fire Tour |
- on 880715,determined That Sensing Line Support Hangers Would Not Withstand Design Basis Fire W/O Mod or Protection.Caused by Inadequate Design by Architect Engineer.Areas Placed on Hourly Fire Tour
| 10 CFR 50.73(e)(2)(vii) 10 CFR 50.73(e)(2) | | 05000397/LER-1988-027, :on 880728,reactor Water Cleanup Sys (RWCU) Isolated on High Differential Flow During Preparations to Place RWCU Recirculation Pump in Svc.Caused by Personnel Error.Personnel Counseled Re Incident |
- on 880728,reactor Water Cleanup Sys (RWCU) Isolated on High Differential Flow During Preparations to Place RWCU Recirculation Pump in Svc.Caused by Personnel Error.Personnel Counseled Re Incident
| | | 05000397/LER-1988-028, :on 880823,determined That on 870220-21 & 0619,Tech Spec Heatup/Cooldown Limit of 100 F in Any 1 H Period Exceeded.Caused by Program Inadequacy.Heatup & Cooldown Trending Program Added |
- on 880823,determined That on 870220-21 & 0619,Tech Spec Heatup/Cooldown Limit of 100 F in Any 1 H Period Exceeded.Caused by Program Inadequacy.Heatup & Cooldown Trending Program Added
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000397/LER-1988-029, :on 880824,RCS Unidentified Leakage Noted to Be in Excess of 5 Gpm Tech Spec Limit & RCIC Steam Supply Inboard Isolation Valve Had Large Packing Leak.Caused by Maint Program Deficiency |
- on 880824,RCS Unidentified Leakage Noted to Be in Excess of 5 Gpm Tech Spec Limit & RCIC Steam Supply Inboard Isolation Valve Had Large Packing Leak.Caused by Maint Program Deficiency
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(s)(2) | | 05000397/LER-1988-030, :on 880825 & 26,full Reactor Protection Sys (RPS) Actuations Occurred.Caused by Switch Overtravel.Rps Power Supply Select Switch Returned to Normal Position & Scram Reset |
- on 880825 & 26,full Reactor Protection Sys (RPS) Actuations Occurred.Caused by Switch Overtravel.Rps Power Supply Select Switch Returned to Normal Position & Scram Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(i)(2) | | 05000397/LER-1988-030-01, Forwards LER 88-030-01.Rept Submitted Per Commitment in Response to Violation B Noted in Insp Rept 50-397/88-24 | Forwards LER 88-030-01.Rept Submitted Per Commitment in Response to Violation B Noted in Insp Rept 50-397/88-24 | | | 05000397/LER-1988-031, :on 880902,determined That Due to Single Failure CR HVAC Sys Could Operate in Recirculation Mode. Caused by Lack of Communication Between Ae Design Groups.Cr HVAC Recirculation Mode of Operation Analyzed |
- on 880902,determined That Due to Single Failure CR HVAC Sys Could Operate in Recirculation Mode. Caused by Lack of Communication Between Ae Design Groups.Cr HVAC Recirculation Mode of Operation Analyzed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000397/LER-1988-032, :on 880905,inadvertent Containment Isolation of RCIC Sys Steam Supply Line Occurred While Reactor Pressure Held at 90 Psig.Caused by Personnel Error.Startup Halted & Excess Flow Check Valves Reopened |
- on 880905,inadvertent Containment Isolation of RCIC Sys Steam Supply Line Occurred While Reactor Pressure Held at 90 Psig.Caused by Personnel Error.Startup Halted & Excess Flow Check Valves Reopened
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000397/LER-1988-033, :on 880907,determined That Tech Spec Re Control Room Emergency Filtration Sys Verification Not Performed Since Startup in Dec 1983.Caused by Personnel Error. Temporary Procedure Will Be Initiated |
- on 880907,determined That Tech Spec Re Control Room Emergency Filtration Sys Verification Not Performed Since Startup in Dec 1983.Caused by Personnel Error. Temporary Procedure Will Be Initiated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000397/LER-1988-034, :on 880909,pipe Failure Caused by Introduction of Liquid Nitrogen Into Primary Containment Supply Purge. Inerting Nitrogen Supply Valve & Containment Supply Purge Shut to Terminate Containment Inerting |
- on 880909,pipe Failure Caused by Introduction of Liquid Nitrogen Into Primary Containment Supply Purge. Inerting Nitrogen Supply Valve & Containment Supply Purge Shut to Terminate Containment Inerting
| | | 05000397/LER-1988-035, :on 881101,determined That Control Rod Block Intermediate Range Monitor Quarterly Channel Calibr Surveillances Not Performed.Caused by Lack of Review of Testing Required for Changes in Conditions |
- on 881101,determined That Control Rod Block Intermediate Range Monitor Quarterly Channel Calibr Surveillances Not Performed.Caused by Lack of Review of Testing Required for Changes in Conditions
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(s)(2) | | 05000397/LER-1988-036, :on 881118,inconsistency Noted Between Channel Functional Test Surveillance Procedure & Tech Specs for Div 1 4.16 Kv Emergency Bus Undervoltage Degraded Voltage.Caused by Inadequate Procedure.Tech Spec Revised |
- on 881118,inconsistency Noted Between Channel Functional Test Surveillance Procedure & Tech Specs for Div 1 4.16 Kv Emergency Bus Undervoltage Degraded Voltage.Caused by Inadequate Procedure.Tech Spec Revised
| 10 CFR 50.73(a)(2) | | 05000397/LER-1988-037, :on 881130,plant Shutdown Initiated Due to Containment Supply Purge Valve Air Vol Leak Exceeding Tech Spec Limits.Caused by Damaged CSP-V-9 Rubber Seat.Damaged Seat Replaced W/New Seat Matl |
- on 881130,plant Shutdown Initiated Due to Containment Supply Purge Valve Air Vol Leak Exceeding Tech Spec Limits.Caused by Damaged CSP-V-9 Rubber Seat.Damaged Seat Replaced W/New Seat Matl
| | | 05000397/LER-1988-038, :on 881219,determined That Reactor Bldg to Suppression Chamber Vacuum Breaker Valve Inoperable.Caused by Procedural Inadequacies.Technicians Allowed to Complete Channel Functional Test |
- on 881219,determined That Reactor Bldg to Suppression Chamber Vacuum Breaker Valve Inoperable.Caused by Procedural Inadequacies.Technicians Allowed to Complete Channel Functional Test
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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