05000272/LER-1980-036-03, /03L-0:on 800612,during Transfer of Boric Acid to Boric Acid Storage Tank,Tank Level Not Increased Above Min Level.Caused by Procedural Error.Procedure Revised

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/03L-0:on 800612,during Transfer of Boric Acid to Boric Acid Storage Tank,Tank Level Not Increased Above Min Level.Caused by Procedural Error.Procedure Revised
ML18082A761
Person / Time
Site: Salem 
Issue date: 07/11/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A760 List:
References
LER-80-036-03L, LER-80-36-3L, NUDOCS 8007220627
Download: ML18082A761 (1)


LER-1980-036, /03L-0:on 800612,during Transfer of Boric Acid to Boric Acid Storage Tank,Tank Level Not Increased Above Min Level.Caused by Procedural Error.Procedure Revised
Event date:
Report date:
2721980036R03 - NRC Website

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I While-transferring a solution of boric acid to the Boric Acid Storage Tanks (BAST),

[]JI] I the level in the operable tank was not increased above the minimum level required by [Q]I)

Technical Specifications and Action Statement 3.1.2.B(al) was entered at 1235 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.699175e-4 months <br /> [QJI]

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43 44 47 The procedure used did not require when taking one BAST out of service for the transfer the second tank level to be raised above the minimum level required.

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