05000325/LER-1979-092-03, /03L-0:on 791204,during Normal Plant Operation, Operator Noticed Containment Atmospheric Monitor CAC-ATH-1263 Was Reading Downscale.Caused by Blown Power Supply Fuse & Shift in Instrument Zero.Fuse Replaced

From kanterella
Revision as of 23:05, 3 January 2025 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L-0:on 791204,during Normal Plant Operation, Operator Noticed Containment Atmospheric Monitor CAC-ATH-1263 Was Reading Downscale.Caused by Blown Power Supply Fuse & Shift in Instrument Zero.Fuse Replaced
ML19256G153
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/20/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256G146 List:
References
LER-79-092-03L, LER-79-92-3L, NUDOCS 7912270528
Download: ML19256G153 (2)


LER-1979-092, /03L-0:on 791204,during Normal Plant Operation, Operator Noticed Containment Atmospheric Monitor CAC-ATH-1263 Was Reading Downscale.Caused by Blown Power Supply Fuse & Shift in Instrument Zero.Fuse Replaced
Event date:
Report date:
3251979092R03 - NRC Website

text

,m.-.-

(7 778 LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATiON) l 6

M lN lC lB lE lP l 1 l@l0 l0 l-l0 l0 l0 IO l0 l-lO!0l@l4l1lll1l1l@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE Jo 57 C A T b3 CON'T 0

1 lL l0 l 5 l01-l0 l3 l2 l5 @l1 l210 l4l7Io h 1l2l2l0l7 9 l@

5OURCE 7

8 60 61 DOCKET NUVBER 6d 69 EVENT OATE 74 15 REPORT DATE do EVENT DESCRIPTICN AND PROBABLE CONSEOUENCES h o

2 During normal plant operation, the onerator noticed that the containment atmospheric l monitor CAC-ATH-1263 was reading downscale.

I o

3 o

4 i

I o

s i o

6 o

7 l Technical Specification 3.3.5.3, 6.9.1.9b l

o 8

l 7

8 9 SYSTEM

CAUSE

CAUSE CCNP-VA L'. E CODE COCE SL8C00E COYPCNENT CODE SLSLOCE Sv3C00E lS lE l@ lE @ lG l@ lII N l S l T l R l U lh lY l@ y @

o 9

7 8

9 to 11 12 10 18 19 N

REVISION SECL E N T:AL CCCU A AEP.CE AEFCRT y

E's E N T Y E.1 A REPCRT*.C.

COOE TYPE NO.

@ ]= a pg l7l9l l-l l0 9l2l

]/l 10 l 3 l lL l ll l0 l l{a;

_:2 a

4
e
r
s 23 aa si CC'#C ' '

ACT!ON FUTLAE EFEECT 5-UTOOWN A TT AC H V E N T N8 A O-4

    • 'YECOYP-Y A N '.J A C ? L C E A TAKEN ACTIC N JN PLANT VETwCD DOL 95 SLaYlTTEO FC A9 2L S.

SLDOL;ER E l.gl54X lg l;5Zlg l Z l@

l0l0l0l l

l Y [Q lY lQ l A l@

l3l1l315l@

26 3,

40 41 4;

43 44 47 23 CAUSE CESCRIPTION ANC CCAPECTIVE ACT;CNS h l The power supply fuse was found blown and the instrument zero had shifted.

The reasen) t o

1 i

[ for the fuse blowine could net be detemined and is censidered an isolatmi m'ent.

n.el

[ fuse was replaced and the instrument calibrated. Shifts in the instrument zero have i 7

l occurred previously on these monitors. The manuf acturer is beine contacted to sucolv i 3

i 4

l80 7

8 9 C,ETHCO CF V

F ACILITY SCOVERY DISCOVERY DESCR6PTION STATUS

% PCWER oTHER STATUS l C l@ ln ln ln l@

N/A l

lA l@l Operator Surveillance l

i 5

7 a 3 10 i;

11 44 45 46 80 ACTIVITY CONTENT RELEASED OF aELE ASE AVCLNT CF ACTIVITY LOCATION CF RELE ASE Izl@Izl@l

'uA l

l N/A l

i e

7 8 9 10 11 44 45 30 PERSONNEL EXPOSURES NUv9ER TYPE

DESCRIPTION

1010 l 0 l@l Z l@l N/A l

i 7

,ERSc~~d',N;u'4ES eo

=

'y

~

NuvsER

DESCRIPTION

l

. fiTTl l o l 0 l O l@l N/A ew o

3 7

8 9 11 12 80 LOSS OF CA DAMAGE TO FACILITY TYPE

DESCRIPTION

W @l N/A l

i 9

79122 70 S.2f NRc UsE Onty PUsu TY ISSUED 0ESCRIPTION [f!R4jl N/A I

l l l l 1 I I I I I I l' I }

m 2 o 7

8 3 10 68 69 80 5 o

NAME OF PREPARER A.

C.

N 14m T *- -

PHONE:

410 457 0521 1,

r

LER CONTINUATION - Ro# l-79-92 Facility: BSEP Unit #1 Event Date:

12-4-79 assistance in determining the cause for the zero shifts,and engineering is eval-uating other systems to determine a qualified replacement for the system now in use, e

S 1645 018