05000325/LER-1979-057-03, /03L-0:on 790926,containment Atmospheric Monitor Found Erratic.Cause Unknown.Instrument Calibr & Returned to Svc.Investigation Underway to Determine Best Replacement Sys

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/03L-0:on 790926,containment Atmospheric Monitor Found Erratic.Cause Unknown.Instrument Calibr & Returned to Svc.Investigation Underway to Determine Best Replacement Sys
ML19262A504
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/25/1979
From: Tollison A
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262A503 List:
References
LER-79-057-03L, LER-79-57-3L, NUDOCS 7910310391
Download: ML19262A504 (1)


LER-1979-057, /03L-0:on 790926,containment Atmospheric Monitor Found Erratic.Cause Unknown.Instrument Calibr & Returned to Svc.Investigation Underway to Determine Best Replacement Sys
Event date:
Report date:
3251979057R03 - NRC Website

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LICENSEE EVENT REPORT

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o

2 lDuring normal plant operation. the operator noticed that the containment atmospheric lo la i monitor CAC-AT-1263 was erratic. The same indication occurred on October 2, 1979 l

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o lIn both instances, the zero reference had shifted upscale. The instrument was cali-l 1

i brated both times and returned to service. Engineering is now investicating other I

f7TTl Isystems to determine the best replacement for our system, which has a history of l

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