05000325/LER-1981-011-03, /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage

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/03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage
ML19351G572
Person / Time
Site: Brunswick 
Issue date: 02/18/1981
From: Pastva M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19351G571 List:
References
LER-81-011-03L-01, LER-81-11-3L-1, NUDOCS 8102250278
Download: ML19351G572 (1)


LER-1981-011, /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage
Event date:
Report date:
3251981011R03 - NRC Website

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60 61 DOCKET NUU8ER 68 69 EV ENI D AT E 74 75 REPORT OATE 80 EVENT DESCRIPTION AND PRCBABLE CONSEQUENCES h 10121 l During routine shutdown operations it was discovered that reactor recirculation I

[TTT1 l sample inboard isolatiot. 31ve,1-B32-F019, model no. T36D-13, had seat leakaze I

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I l 1-332-F020, was then closed and deactivated as required by. technical specifications.

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