05000395/LER-1982-056-03, /03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised

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/03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised
ML20028D323
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 01/07/1983
From: Mckinney C
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20028D322 List:
References
LER-82-056-03L, LER-82-56-3L, NUDOCS 8301170404
Download: ML20028D323 (1)


LER-1982-056, /03L-0:on 821209,surveillance Test Procedure, Nis Power Range Heat Balance, Not Performed in Specified Intervals.Caused by Personnel Oversight.Administrative Procedures for Control of Surveillances Revised
Event date:
Report date:
3951982056R03 - NRC Website

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES l o l2 l l On December 9. 1982. with the Plant in Mode 1. Surveillance Test Procedure (STP)l lo l3 ll 102.002 "NIS Power Range Heat Balance," was not performed in accordance with l

l o l4 l l the surveillance interval identified in Surveillance Requirement 4.0.2.(a).

l [o lS l l There were no adverse consequences from this event since the Plant had remained l [o le [ [ at a stchie 30% of Rated Thermal Power during the subject time period.

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STP-102.002 was satisfactorily performed l l t l 2 l l on December 9 1982. The administrative procedure covering the surveillance l

l i j a l l program is being revised to improve controls on surveillances with short l

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