ML20059G316

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Safety Insp Repts 50-454/93-12 & 50-455/93-12 on 930707- 0930.Violations Noted.Major Areas Inspected:Operational Safety Verification,Onsite Event Followup,Matl Condition, Security,Radiological Controls & Surveillance Activities
ML20059G316
Person / Time
Site: Byron  Constellation icon.png
Issue date: 10/25/1993
From: Farber M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20059G298 List:
References
50-454-93-12, 50-455-93-12, NUDOCS 9311080065
Download: ML20059G316 (37)


See also: IR 05000454/1993012

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-454/93012(DRP); 50-455/93012(DRP)

Dockets No. 50-454; 50-455 Licenses No. NPF-37; NPF-66.

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Licensee: Commonwealth Edison Company

Executive Towers West III

1400 Opus Place

Downers Grove, IL 60515 '

facility Name: Byron Station, Units 1 and 2-

Inspection At: Byron Site, Byron, Illinois

Inspection Conducted: July 7 through September 30, 1993 __

Inspectors: H. Peterson

C. H. Brown

J. L. Hansen l

V. P. Lougheed

Approved By: Y h /0 f!93

MartinJ.ffarber, Chief '

Date

Reactor Wojects Section lA

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1_nspection Summary

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inspection from July 7 through September- 30. 1993 (Reports No. 50-

454/93012(DRP): 50-455/93012(DRP)).

Areas Inspected: Routine, unannounced safety inspection by the resident

inspectors of previous inspection findings, operational safety verification,

onsite event follow up, material condition, housekeeping and plant >

cleanliness, radiological controls, security, safety assessment / quality

verification, maintenance activities, surveillance activities, engineering and

technical support, and refueling activities.

Results: Of the twelve areas inspected, two violations, one. non-cited

violation, and two inspection followup items were identified. The violations >

pertained to failure to follow procedures (paragraph 3b). The non-cited  :

violation pertained to minor security concerns-(paragraph 3f). The inspection l

followup items pertained to engineering and technical support. The following- i

is a summary of performance during this inspection period: l

93110B0065 931101

PDR ADOCK 05000454 l

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Plant Operations

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Overall, performance in this area continues to be good. During this

inspection period, several operational events occurred, including a. Generating

Station Emergency Plan (GSEP) Unusual Event associated with complete loss of

commercial and emergency telephone communications. The licensee's.re:ponse to

this event was excellent. <

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Three operational personnel errors occurred during this period. One

particular incident resulted in an inadvertent initiation of Safety Injection.

Another personnel error resulted in a significant safety hazard to personnel '

in the affected area. These incidents and one other example of a personnel-

error resulted in a violation of NRC requirements (paragraph 3b). '!

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Radiological controls continue to be good. In evaluating radiation protection

goals, the number of personnel contamination events and total personnel  ;

exposure were below the projected values during this inspection period.  !

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Security continues to be generally good; however, a non-cited violation was  :

identified concerning minor incidents which violated the station's' returity i

plan (paragraph 3f).

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Safety Assessment /0uality Verification

Performance in this area remains good. The inspectors reviewed the On-Site .

Quality Verification (SQV) program during the refueling outage. The SQV '

department initiated 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> coverage during the outage. Station management

continues to give high regard to the findings and recommendations identified

by the SQV organization. On the other hand, recurrence of administrative

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errors in the review, distribution, and control of documents, went

unidentified and uncorrected for several years.

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Maintenance and Surveillance

Performance in this area was satisfactory; however, personnel errors ,

pertaining to failure to follow procedures resulted in three operational -!

events (paragraph 3b).

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Enaineerina and Technical Succort

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Performance in this area was good. The inspectors observed portions of-the

Integrated Leak Rate Testing (ILRT) and the Erosion / Corrosion testing programs

-and considered both programs to be good. The licensee identified two

engineering concerns, specifically pressurizer anomalies and differences ,

between Technical Specifications and Westinghouse recommendations. The

inspectors are monitoring the engineering department's progress on these two

items as an inspection followup item (paragraph 7).

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note completion of one of the required test procedures and left

the item blank on the work request. Then, a Senior Reactor

Operator performed an inadequate review of the package and

incorrectly signed the package as complete.

The licensee initiated a root cause analysis on.the SPPs and

LC0ARs deficiencies. The indepth root cause analysis was

performed utilizing a multi-disciplined investigation team. The

results of the analysis indicated specific procedural problems.

These problems included no formal procedural guidance, a lack of

written communication control, and lack of supervisory methods for

controlling these types of documents. The root cause analysis

specifically outlined corrective actions for each causal. factor. _

This incident and the administrative control deficiencies related

to the SPPs and LC0ARs are examples of inadequate procedural

adherence to Byron Administrative Procedures (BAP 1210-1

Attachment A.3, " Review of Special Procedures / Tests / Experiments";

BAP 1310-8, "Special Procedures / Test / Experiments"; BAP 1400-6,

" Technical Specification Limiting Condition for Operatien Action

Requirements"; BAP 1600-IIA.1, "NWR Testing Requirements") and the

requirements of Technical Specification. (TS) Section 6.8,

" Procedures and Programs." Therefore, this is a violation

(454/455-93012-01(DRP)). In view of the licensee's corrective

actions, this violation does not require a written response. This

unresolved item is closed.

b. (Closed) Inspection Followup Item 454/455-93010-01 (DRP): This

item concerned an apparent non-conservative policy in making ,

emergency declarations, identified during the June 7, 1993,.

licensed operator requalification examination. .The inspectors

interviewed licensed operators and discussed the issue with the  :

training department. Associated lesson plans were reviewed.

Overall, the station operating and training departments adequately  ;

stressed that anytime any value is exceeded pertaining to an j

Emergency Action Level, the appropriate classification shall be

made. This item is considered closed. .

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c. (Closed) Violation 455-91022-01 (DRS): This item concerns the  !

failure to adequately take data during the performance of the

Integrated Leak Rate. Testing (ILRT) on Unit 2 containment. During

the Unit 2 refueling outage on September 14, 1991, ILRT-hourly D

data was not recorded from 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> until 2114 hours0.0245 days <br />0.587 hours <br />0.0035 weeks <br />8.04377e-4 months <br />. The 1

reason for the problem was that power supply to the ILRT equipment-  !

was inadvertently de-energized. During.the September 1993, Unit 2

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refueling outage, the inspectors reviewed and observed the

performance of the Unit 2 containment.ILRT. The licensee enhanced

the ILRT procedure; including new computer software, data

recording every 15 minutes, and ensuring operations awareness of

the test by enforcing a tagout protection on the power supply for

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the ILRT equipment. Overall, the ILRT. results were satisfactory, l'

and the test was conducted by the engineering personnel in an

excellent manner. This item is considered closed. #

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One violation was identified. l

3. Plant Operations .!

Unit 1 operated at power levels up to 100% in the load following mode-

throughout the report period.

Unit 2 operated at reduced power levels for plant end of life coastdown

in preparation for the refueling outage. On September 2, 1993, a .

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reactor shutdown commenced for the planned 60 day refueling outage. The

reactor was shutdown at 4:41 a.m. on September 3, 1993. e

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a. Operational Safety Verification (71707. 93702)  ;

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The inspectors verified that the facility was being operated in

conformance with the licenses and regulatory requirements, and

that the licensee's management control system was effectively. .i

carrying out its responsibilities for safe operation. i

On a sampling basis, the inspectors verified proper control room .

staffing and coordination of plant activities; verified operator

adherence with procedures and TSs; monitored control room  :{

indications for abnormalities; verified that electrical power was  !

available; and observed the frequency of plant and control room ,

visits by station management. ,

Overall, the licensee's awareness of plant safety continues to be j

good. During this-inspection period, three personnel errors, due ' i

to the failure to follow procedures and lack of attention to "

detail, were identified during the performance of maintenance and '

surveillance activities. These errors are discussed in detail in ,

paragraph 3b. Extensive corrective actions and root cause 'i

analyses have been initiated to prevent recurrence of personnel

errors.  ;

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The inspector observed a fire drill associated with a simulated  !

warehouse fire in the protected area on August 5, 1993. This was  !

a complete activation of fire' brigade personnel and equipment. ,

The fire brigade response was very quick. All personnel donned j

fire fighting gear and participated in actual pressurization and l

use of fire hoses. The drill was an excellent training aid and '

overall' performance was good. :l

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b. Onsite Event follow-up (93702)

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Inadvertent Safety In.iection Actuation i

On September 5, 1993, during the performance of 2BOS 3.2.1.1.a-1, .l

" Unit Two Train A Manual Safety Injection Initiation and Manual ,

Phase A Initiation Surveillance," an inadvertent safety injection I

(SI) occurred. It was identified that during the restoration of  ;

train B solid state protection system, the nuclear station

operator (a licensed reactor operator) placed the train B  !

multiplexer test switch in the inhibit position, instead of  !

placing the input error inhibit switch in the inhibit position, as

required by the procedure. When the subsequent step was

performed, placing the train B mode selector switch to operate, a i

51 signal was initiated due to permissive P-11 signal not being  ;

present. At the time of the event, the reactor was shutdown for

the refueling outage and reactor coolant system was at 140 F and j

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350 psig. As a result of this event, pressurizer level increased

approximately 10% (an indication of approximately 1200 gallons  !

injected), and reactor coolant system pressure increaset j

approximately 50 psig (from 350 to 400 psig). During the event,

no relief valves were actuated and one train of residual heat i

removal in shutdown cooling remained operating. All systems  !

responded as expected.  :

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After further review, it was identified that the operator  !

performing the surveillance test failed to follow the surveillance l

procedure. Step 1.58, parts a, b, and c of this procedure require l

an independent verification after each part. Had the proper '

independent verification been performed, the verifier could have

identified that the wrong switch was manipulated and could have l

prevented the event. l

Loss of Unit 2 Instrument Buses 211 and 213  ;

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On September 7, 1993, while performing electrical preventive  !

maintenance'on inverter 211 for instrument bus voltage adjustment, ,

actions were taken to swap instrument bus 211 power supply. Buses  ;

-211 and 213 were initially powered from their respective constant  :

voltage transformer (CVT). When directed to shift instrument bus .

211 to its main power source (inverter), the operator incorrectly I

transferred bus 213 to its main feed inverter, which was out of  !

service. Not realizing the mistake, the operators then de-

energiz9d bus 211 CVT. This caused the loss of both instrument  ;

buses 211 and 213. Operators responded to the event, and _

identified that both source range nuclear instruments (NI) had de- l

energized. Appropriate actions were taken for source range LC0AR  !

2BOS 3.1-la, and abnormal operating procedure for the loss of 1

instrument buses, ELEC-2. Buses 211, 213, and both source range  !

NIs were re-energized. The licensee initiated an investigation i

encompassing personnel error, adherence to procedures, and human l

factor concerns. j

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Wrono C0. Fire Protection System Train Actuation

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On September 10, 1993, the Electrical Maintenance department was

performing fire protection test 2BHS 7.10.3.2.b.1-7,'" Low Pressure l

CO, System Actuating 18 Month Surveillance," in the . Unit '2 lower j

cable spreading room zone 2S-46. All precautionary. steps were

taken prior to actuation of CO,; however, due to-failure to follow

procedures and a lack of attention to details, the' wrong lower

cable spreading room zone (2S-45) CO, system was manually

actuated. The technicians attempted to terminate the injection, t

but CO, discharged into the room. A pot _ential personnel injury  !

was associated with this event. There was a firewatch located. ~!

inside room 25-45! however, the warning alarm prior to CO, _  ;

injection allowed the individual to exit the room and no personnel 1

injury occurred. j

The three preceding incidents are examples of errors in failing to

adequately follow procedures. This is a violation of 10 CFR 50,  !

Appendix B, Criterion V (50-454/455-93012-02 (DRP)).  ;

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GSEP Unusual Event > l

On July 28, 1993, at 10:22 a.m., an Unusual Event -(UE) was l

declared based on Byron's Generating Station Emergency Plan  !

(GSEP), Emergency Action Level 3C, " Loss of Commercial Telephone  !

Communications, NARS, HPN, and ENS." The licensee made its  ;

initial State, local, and NRC notifications utilizing the .l'

dedicated microwave communications link to the load dispatcher's

office. All notifications were made within the required ,

regulatory time limits. Subsequently, the licensee established a ,

continuous open communications link with the NRC Headquarters +

Operations Center utilizing the microwave communications system j

and tieing it to an outside long distance operator. An additional  !

communication link was established by utilizing the Station '

Manager's cellular phone. l

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It was later identified that a fiber optic communications line at  !

an outside telephone switching station had been accidentally cut.  ;

After verifying that all phone communication systems were ]

permanently repaired and operating satisfactorily, the license j

terminated the emergency event at 2:47 a.m., on July-29, 1993.  ;

Considering the uniqueness and difficulty associated with the lack .:

of normal communications, the control room licensed operators and 1'

emergency planning personnel performed their GSEP responsibilities

in an excellent manner.

Stuck Control Rod Durina Reactor Shutdown

At 3:20 a.m.,-on September 3, during the Unit 2 reactor shutdown, '

control rod C-5 of shutdown bank D failed to insert past the

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transition position indication, resulting in a rod misalignment

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with the other three rods of bank D. The licensee entered

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abnormal procedure 2 BOA ROD-3, " Dropped or Misaligned Rod " Blown

fuses for the lift coil of rod C-5. were identified and replaced.

Proper precautionary steps were taken prior to attempting to move ,

the affected rod. At 4:40 a.m., rod C-5 was satisfactorily  ;

restored to operation and inserted to its rod bottom position, j,

The inspectors questioned the cause of the blown fuse and the fuse

replacement program for the control rod drive (CRD) system. The  ;

inspectors determined that fuses associated with the CRD.  :

stationary and moveable gripper circuits were replaced every other ,

refueling outage. Unit I fuses had been replaced in March 1993

during the last refueling outage. Unit 2 fuses had been replaced

during its last refueling outage in April 1992. The investigation .

as to the cause of the blown fuse was inconclusive; however, .the '

fuse control program for the CRD system appeared adequate.

Overall, the station operators responded quickly and performed the

required actions of the abnormal procedures in an excellent

manner,

c. Current Material Condition --

The inspectors performed general plant walkdowns, as well as,.

selected system and component walkdowns to assess the general and

specific material condition of the plant, to verify that Nuclear

Work Requests (NWRs) had been initiated for identified equipment

problems, and to evaluate housekeeping. Walkdowns -included an

assessment of the buildings, components, and systems for proper-

identification and tagging, accessibility, fire and security door

integrity, scaffolding, radiological controls, and any unusual

conditions. Unusual conditions included but were not limited to

water, oil, or other liquids on the floor or equipment;

indications of leakage through ceiling, walls or floors; loose

insulation; corrosion; excessive noise; unusual temperatures; and

abnormal ventilation and lighting.

Considering that Unit 2 was in a refueling outage, the general

material condition inside containment was considered satisfactory.

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Some areas of clutter, loose tools and equipment, and oil spilled

from the steam generator snubber maintenance were observed. The.

atmosphere and humidity within the containment were properly

regulated to ensure safe working conditions.

d. Housekeepina and Plant Cleanliness

The inspectors monitored the status of housekeeping-and plant

cleanliness for fire protection and protection _of safety-related-

equipment from intrusion of foreign matter. In general,

housekeeping and plant cleanliness has improved.

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In the' Unit 2 containment, even with the outage, the housekeeping

and cleanliness condition are satisfactory; however, there are

some. areas of clutter and foreign material which will require- .

extensive cleanup efforts at the conclusion of the outage,

e. Radioloaical Controls

The inspectors verified that personnel were following health

physics procedures for dosimetry, protective clothing, frisking, ,

posting, and randomly sxamined radiation protection ,

instrumentation for operability and calibration.  ;

During a tour of the 346 feet elevation of.the auxiliary building, _

the inspectors discovered a gum wrapper, a piece of gum in the

waste gas decay valve aisle, and cigarette butts under the waste

gas decay tanks. These items were brought to the attention of the

radiation. protection personnel. The items were removed and plant .;

management re-emphasized proper radiological controls to all site  !

personnel.  ?

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Overall, radiological controls continue to be good. Radiation

protection personnel continue to be very responsive to the needs

of the plant. In evaluating radiation protection goals, the

number of personnel contamination events and total personnel -

exposure were below the projected value during the inspection '

period.

f. Security

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Each week during routine activities or tours, the inspectors I

monitored the licensee's activities to ensure that observed i

actions were being implemented according to the approved security i

plan. The inspectors noted that persons within the protected area '

displayed proper photo-identification badges and those individuals

requiring escorts were properly escorted except as discussed

below. . The inspectors also verified that vital areas were locked l

and alarmed. Additionally, the . inspectors also observed that '

personnel and packages entering the protected area were searched

by appropriate equipment or by hand, J

On Wednesday, September 15,-1993, the inspectors identified that a  ;

visitor was not in immediate visual contact with-his escort. The

inspectors accompanied him until his escort was located. Followup

investigation by the security department found that the escort and ,

visitor had been separated for approximately two to three minutes ~ s

after a roll-up door was closed between them.  ;

During a followup tour with a security officer and a contract crew

foreman the next day, the inspectors discovered an individual

within the protected area who was not wearing his security badge. 1

The individual had removed his shirt, with the badge attached, and

hung it off a piece of scaffolding in the area.

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On September 2,1993, an individual failed his Nuclear General l

Employee Training (NGET) requalification training. According to

Byron administrative procedures, his access to the plant should be

suspended. However, the training department did not communicate- i

the failure to the security department and on September 7, the  ;

individual was allowed access into the station. The corrective i

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actions included formalizing communications between the training  ;

and security department, and changing the appropriate procedures  !

such that the training department will immediately call security l

and inform them of personnel failing NGET requalification. j

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During the month of September, two incidents of issuance of wrong

security badges were identified by the licensee. One incident was ..

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immediately corrected at the badge receipt window. On

September 15, another error in issuing a security badge took about l

two hours to identify. In both events, the administrative  ;

security procedure, which required the positive identification of ,

badges prior to issuance, was not rigorously followed. The  ;

licensee's security department took immediate and extensive

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corrective actions following the September 15 event, inciuding

individual disciplining.

The above four items are isolated events with little or no safety  !

significance, and corrective actions were immediate and i

appropriate. Additionally, the security department has initiated i

the development of a training video concentrating on

administrative security issues, such as visitor escorting

practices and badge receipt responsibilities. It was determined

that these events meet the criteria outlined in 10 CFR part 2,

Appendix C,Section VII.B, and therefore are considered a non-

cited violation of station administrative security procedures.

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One violation and one non-cited violation were identified.

4. Reaional Reauest (92701)

Temporary Instruction 2500/028 " Employee Concerns Proaram" j

The inspectors verified the licensee had implemented an employee

concerns program to provide an alternate path from normal line

management to raise safety concerns. The specific characteristics of

this program and an evaluation of its effectiveness is described on the

attached form (Attachment 1). This temporary instruction is considered

closed.

NRC Technical Trainino Center (TTC) Information Reauest-

The NRC TTC requested updated information pertaining to Westinghouse 4-

loop plants. The request was in.the form of a questionnaire. The

inspectors requested the licensee. supply specific information associated

with the questionnaire. The licensee's response was timely and

thorough.

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Action Item neauest on Post-Fire Shutdown Procedures '

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NRC Headquarters Office of Nuclear Reactor Regulation (NRR) identified

cases where abnormal opera'ing crocedures for achieving and maintaining

safe shutdown from cutside che control room instructed the operators to

isolate both onsite and offsite electrical power sources. While power

to the station is isolated, operators reconfigure shutdown systems and .

isolate electrical circuits tnat could cause spurious signals and  !

prevent safe shutdown capability. To conduct a detailed study to -

determine how many plants take this approach and assess the potential ,

risk, copies of plant post-fire shutdown procedures and management of '

onsite and offsite power sources were requested. The inspectors .

identified the following pertinent procedures at the Byron station: .

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  • BCA-0.0, " Loss of All AC Power," )
  • BOA-ELEC-1, " Loss of DC Buses,"
  • BOA-ELEC-2, " Loss of Instrument Bus," and

a BOA-ELEC-4, " Loss of Offsite Power for Modes 3 or 4." '

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No violations or deviatic.ns were identified. -

5. Safety Assessment /0cality Verification (40500. 90712. 92700)

During this inspection period, the inspectors evaluated the scope and I

effectiveness of the On-Site Quality Verification (SQV) program during

the refueling outage. This included the review of the SQV Shutdown Risk .

Assessment Report for Byron Station Refuel Outage B2R04. This report. l

was an independent evaluation of shutdown risk for the planning and  ;

scheduling portion of the refueling outage. ,

SQV made eleven recommendations to the station work planning department.

Three recommendations dealt with equipment availability, administrative ,

controls, and plant conditions tied to minimizing risk associated with  !

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loss of decay heat removal. Two recommendations dealt with enhancements

to minimize risk associated with loss of reactor coolant system  ;

inventory. Three recommendations dealt with issues associated with  !

activities impacting loss of AC power. These items particularly l

enhanced the work activities associated with the diesel generator work  !

and the system auxiliary transformer work. The remaining three  !

recommendations dealt with administrative controls. All recommendations

were appropriately accepted and resolved.

In addition to the shutdown risk review, the inspectors periodically l'

monitored the SQV evaluators on daily field monitoring report (FMR)

inspections. During the month of August, SQV generated'66 FMRs. In the

month of September, the SQV department generated 251 FMRs by providing i

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> coverage of activities related to the refueling outage. The l

resident inspectors are evaluating a sample of these FMRs and their

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resolution to assess the effectiveness of the process.

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INP0 Assistance Visit

On August 9 through 13, 1993, an INP0 inspection team conducted an

evaluation of licensee's corrective actions associated with the June

1992 INP0 evaluation. This assistance visit was-requested by the

station management to conduct followup inspection, and to evaluate the

Byron excellence review team trending and the integrated reporting

programs. The team consisted of three INP0 evaluators, a peer evaluator

from Crystal River station., and a Byron in-house peer evaluator. No

major concerns were identified during this visit.

No violations or deviations were identified.

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6. Maintenance / Surveillance (62703. 617261

a. Maintenance Activities (62703)-

Station maintenance activities were routinely observed and/or.

reviewed to ascertain whether they were conducted in accordance

with approved procedures, regulatory guides and industry codes or

standards, and in conformance with technical specifications.

The following items were also considered during this review: ..

approvals were obtained prior to initiating the work; functional

testing and/or calibrations were performed prior to returning

components- or systems to service; quality control records were

maintained; and activities were accomplished by qualified

personnel.

Portions of the following maintenance activities were observed and

reviewed:

  • NWR-B04196 - Replace diodes on Unit- 2 Turbine Driven

Auxiliary Feedwater Pump,

  • 2CV85238 - 28 CV MB Demin Resin Fill / Flush Gearbox Assembly

Repair,

  • NWR-B03393- IPR 013J- Check Source Repair on RM-11,
  • SPP 93-049 - Damaged Fuel Assembly Manipulation,
  • NWR-803525 - Loading Damaged Fuel Assembly,
  • BFP FH-21T2 - Shipping Container Inspection Checklist,
  • NWR-B03822-1B Feed Pump low Pressure Governor Valve

Oscillation, ara

  • Unit 2 Low Pressure Turbine Disassembly' and Inspection.

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During the last refueling outage in April '1993,'the' Unit 1 upper

internal and fuel assembly misalignment resulted in damage to one

new fuel assembly and guide pins. The inspectors observed the

coordination between operations, fuel handlers, maintenance, and

radiation protection personnel during the handling of the damaged

new fuel assembly in preparation for shipment to Westinghouse

Electric Corporation. Overall, the fuel handling and shipping

activities were well managed.

b. Surveillance Activities (61726)

During the inspection period, the inspectors observed TS required

surveillance testing and verified that testing was performed in .

accordance with applicable procedures, that test instrumentation

was calibrated, that results conformed with TSs and procedure

requirements and were reviewed, and that any deficiencies

identified during the testing were properly resolved.

The inspectors witnessed portions of the following surveillances:

2BHS-XLT-1 - Limitorque Valve Operator Signature on Valve

2SX007,-

  • 1A Diesel Generator (DG) Monthly Operability Surveillance,
  • New Fuel Receipt Inspection,

a 2BOS 9.4-1 - Unit 2 Containment Building Penetraticn to

Outside Atmosphere Weekly Surveillance, -and-

2A DG 18 Month Surveillance / Maintenance.

Review of 2BOS 9.4-1, performed during'the core refueling, showed

that the surveillance was performed as' required and that all-

requirements were met. Specifically, there were no paths to the

outside atmosphere and the fuel handling building ventilation

could maintain at least a negative 0.25 inches water pressure in-

the building.

During the 2A DG post surveillance / maintenance run, a problem was

identified with a ground fault trip calibration. Engineering

determined that the trip had been set non-conservatively; however,

this trip mechanism was not used or required during emergency

operation of the diesel. Following calibration, the diesel post-

maintenance run proceeded to go smoothly both in the control room

and in the diesel room. Adequate personnel were available to

ensure all necessary parameters were observed and adjustments

completed.

No violations or deviations were identified.

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7. Enoineerinq & Technical Support (37700)

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Information Notice 93-33. " Potential Deficiencies of Certain Class IE  !

Instrumentation and Control Cables"

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Byron station performs systematic reviews of all industry operating ,

experience including information notices (IN), bulletins, lNPO I

information, and vendor information. The majority of the followup  ;

responsibilities have been recently assigned to the individual sites. .

Issues of generic concerns are assigned to the corporate regulatory i

organization, while the individual sites perform parallel reviews.  !

The inspectors performed a review of licensee's actions associated with _  !

IN 93-33. Site engineering, in conjunction with corporate, had reviewed

l- the EQ aspects of electrical cabling and had concluded that Byron's

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l cables were tested and installed per IEEE Std 323-1974, "IEEE Standard

for Qualifying Class lE Equipment for Nuclear Power Generating

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Stations." The corporate staff is participating in an industry group,

called the Nuclear Utility Group on Equipment Qualification (NUGEQ), i

associated with EQ. - '

Discrepancy on Scheduled Removal of Irradiated Reactor Vessel Samole

Capsules i

On September 3,1993, the inspectors became aware of a potential problem

associated with the TS scheduled removal of reactor vessel material

irradiation surveillance specimens.

In preparing for the removal of the irradiated surveillance specimen,-

the licensee discovered that the specimen capsule removal schedule in TS i

Table 4.4-5 was inconsistent with Westinghouse Commercial Atomic Power

(WCAP) documents. The WCAP document recommended a revised schedule for-

future capsule removals based on the latest specimen analyses. TS Table -

4.4-5 accurately reflected the original WCAP recommendations; however, i

after the first refueling outage, the TS table was not updated in

accordance with WCAP revised recommendations.

Westinghouse and site engineering have discussed the inconsistency in

the specimen removal for Unit 1. They determined that the specimen

which was removed in accordance with the TS table can be used to make

the necessary predictions required of the reactor vessel radiation

surveillance program. Therefore, there are no concerns involving Unit 1

reactor vessel operability.

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For Unit 2, Westinghouse has concluded that either the specimen required

by the IS table or the specimen recommended by the WCAP document could

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Although there are no immediate operability concerns on the reactor

vessels, the inspectors will follow the licensee's action to address the

necessary changes to the TS or the WCAP document. This item is

considered as an inspection followup item (454/455-93012-03 (DRP)).

Pressurizer Transients

Two pressurizer transients occurred during the Unit 2 shutdown, which

initiated followup activities by the engineering department.

On September 3,1993, while shutting down Unit 2, the Digital Electro-

Hydraulic Control (DEHC) system induced a main turbine transient causing

pressurizer pressure to decrease to less than 2219 psig, the departure _

from nucleate boiling (DNB)-limit. The operators-immediately~ entered-

the LC0AR 2BOS 2.5-la, "DNB Parameters," and within 5 minutes restored

pressurizer pressure to above 2219 psig. A mismatch in the DEHC

reference and reference demand caused a load increase from 160 to 180

megawatts. This secondary transient caused pressurizer pressure to

decrease. The thermal system engineering department is evaluating this

transient. --

On September 5,1993, wh'ile Unit 2 was in Mode 5 with reactor coolant

temperature at approximately 125 F, pressurizer vapor space temperature

at approximately 400 F, and pressurizer liquid space at approximately

128 F, the'2D reactor coolant pump was started. After the pump was

started, the pressurizer vapor space and liquid space temperatures

equalized at approximately 320 F. The-subsequent cooldown resulted in

rapid temperature decrease to approximately 128*F. 'No TS limit ~was-

violated and the pressurizer cooldown. limit of 200 per hour was not-

exceeded; however, questions exist on proper control of pressurizer

cooldown. The site engineering department was also tasked to. evaluate

this transient. These two items are considered an inspection followup

item (454/455-93012-04 (DRP)).

Erosion / Corrosion Prooram Observation (49001)

During the Unit 2 refueling outage, the inspectors discussed the

erosion / corrosion program with site engineering personnel and conducted

a walkdown of outage related program activities. Interviews with

engineers responsible for program implementation and field personnel

performing the testing indicated that personnel were qualified and

proper attention was being given to piping replacement-, The program

appeared to meet all requirements and was considered proactive in the

testing of small bore piping. The licensee continued to have an

aggressive erosion / corrosion investigation program.

Two inspection followup items were identified.

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8. Refuelina Activities (60710) '

During the refueling outage, the inspectors observed the licensee's fuel

handling operations, including the receipt and storage of new fuel; and

discussed refueling operations with plant operators and fuel handling

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personnel. The licensee used approved procedures for fuel

accountability and movements. Communications between the control room ,

and fuel handlers were effective. The inspectors witnessed fuel  ;

handling operations from the control room, in the fuel building, and in  ;

containment.

The refueling activities were initiated and are being completed on .

schedule, and are proceeding in accordance with the plan and _  !

requirements. The submerged cameras were a great help in ensuring rods

or assemblies were not attached to the upper internals. Activities i

prior to and during vessel internals removal were satisfactory. '

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During the core offload, a gear failed in the transfer mechanism of the

fuel transfer cart. The fuel transfer canal was required to be drained

to initiate repairs. All proper radiological precautions were taken and ,

only one minor personnel contamination occurred within this highly

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contaminated area. The licensee's response and repair activities were .

excellent. l

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No violations or deviations were identified.

9. Report Review

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During the inspection period, the inspector reviewed the licensee's

Monthly Performance Reports for July and August 1993. The inspectors  :

confirmed that the information provided met the requirements of l

Technical Specification 6.9.1.8 and Regulatory Guide 1.16. .;

The inspector also reviewed the licensee's Monthly Plant Status Reports '

for July and August 1993.

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No violations or deviations were identified.

10. Inspection Followup Items

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Inspection followup items are matters which have been discussed with the

licensee, which will be reviewed by the inspector and which involve some 5

action on the part of the NRC, licensee or both. Two inspection

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followup items were identified during the inspection and are discussed

in paragraph 7. i

11. Non-Cited Violations 'l

Non-cited violations are violations for which a " Notice of Violation"

will not be issued. The NRC uses the " Notice of Violation" as a i

standard method of formalizing the existence of a violation of legally  !

binding requirement. However, because the NRC wants to encourage and

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support licensee's'in'itiatives for selt-identification and correction lof

problems, the NRC will not generally issue a " Notice of Violation" for a

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violation that meets the tests of 10 CFR Part 2, Appendix C, Section i

VII.B. -A non-cited violation was identified during this inspection and

is discussed in paragraph 3. e

12. Meetinas and Other Activities -

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Management Meetinas (30702)

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On July 29-30 and September 15, 1993, Mr. Martin J. Farber, NRC

Region Ill Section Chief, toured the Byron plant and met with

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licensee management to discuss plant performance, plant material  !

condition, and recent personnel errors.

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On September 22-23, 1993, Mr.. Ramin Assa, NRR Licensing Project '

Manager for Braidwood Station, toured the Byron plant and met with  !

licensee management for backup site coverage and observation. 1

b. Manaaement Visit by International Nuclear Industry Reoresentatives  !

(30702)

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Representative from Hungarv  !

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One Hungarian representative, from the Nuclear Power Plant (NPP)  !

Paks, visited Byron station during the week of August 16, 1993.  ;

He was in this country on an International Atomic Energy Agency- ,j

sponsored scientific information visit that included some labs and ',

other NPPs. The purpose of the visit was to review high-  !

technology maintenance practices and methods. I

Representative from Great Britain

The Assistant Outage Manager for Sizewell B, a United _ Kingdom

Central Electricity Generating Board Power Plant, arrived at the .;

Byron station on September 4,1993, for approximately three weeks. i

The purpose of the visit was to observe outage planning and  :

implementation during the refueling outage.

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c. Exit Interview (30703) I

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The inspectors met with the licensee representatives denoted in .j

paragraph I during the inspection period and at the conclusion of  ;

the inspection on September 30, 1993. The inspectors summarized l

the scope and results of the inspection and discussed the likely l

content of this inspection report. The licensee acknowledged the  ;

information and did not indicate that any of the information i

disclosed during the inspection could be considered proprietary in

nature.

Attachment: Employee Concerns Programs

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Attachment'l l

MPLOYEE' CONCERNS PROGRAMS  !

PLANT NAME: LaSalle Licensee: CECO DOCKET #: 50-373/374 -

Dresden CECO 50-237/249 .

Quad Cities CECO 50-254/265  :

Byron CECO 50-454/455 i

Braidwood CECO 50-456/457-

Zion CL(Q 50-295/304  ;

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NOTE: Please underline yes or no if applicable and add comments in the space ,

provided. }

A. PROGRAM: ,

1. Does the licensee have an employee concerns- program?

(Yes or No/ Comments) c

The licensee conducts.a Quality First program to identify and j

address employee concerns. Other programs such as the vision

through quality (VQ) search for opportunity (SFO) exist. The VQ l

SF0 program is more oriented toward identifying and developing _  ;

improvement initiatives versus a_ formal program for raising

specific safety issues. Therefore, the completion of this form

will deal only with the QF program.

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2. Has NRC inspected the program? Report #  !

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The NRC_had not recently inspected this program.

B. SCOPE: (Circle all that apply)

1. Is it for: I

a. Technical? (Yes. No/ Comments) ,

b. Administrative? (Yes. No/ Comments) l

c. Personnel issues? (Yes. No/ Comments)

The concerns are categorized as security, quality, and management  :

but may, in fact, involve any of the above. '

2. Does it cover safety as well as non-safety issues?

(Yes or No/ Comments)

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3. Is;it designed for:

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a. Nuclear safety? (Yes. No/ Comments)

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b. Personal safety.? (Yes. No/ Comments)  ;

c. Personnel issues - including union grievances?

(Yes or (Lo/ Comments)

Although it can involve personnel issues, it does not deal -:

with union grievances.  ;

4. Does the program apply to all licensee employees? ,

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(Yes or No/ Comments)  ;

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5. Contractors?

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(Yes or No/ Comments) L

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This program is not necessarily stressed to contract employees.the  ;

licensee believes are not in a position to identify QuaHty First  ;

issues such as parking lot pavers. ]

6. Does the licensee require its contractors and their subs to have a j

similar program? r

(Yes or tLq/ Comments)

Ceco administers the entire program.

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7. Does the licensee' conduct an exit interview upon terminating l

employees asking if they have any safety concerns? j

(Yes or No/ Comments)  ;

Upon termination, employees are given concern disclosure  ;

statements to complete. Exit interviews are given. .The-  !

percentage of terminating employees receiving them is dra'stically.- -l

reduced due to a reduction in program manpower since the beginning ,

of the year. '

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C. INDEPENDENCE:

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1. What is the title of the person in charge?  ;

Quality First Administrator (QFA)

2. Who do they report to?

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Director of Station Quality Verification

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3. Are they independent of line management? *

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Yes - Reports through offsite quality verification organization

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4. Does the ECP use third party consultants?

No - However, quality verification personnel have been utilized to

do interviews. The QFA determines the appropriate group to do:the

investigation.

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5. How is a concern about a manager or vice president followed up?J

This would be decided on a case by case basis.

D. RESOURCES:

1. What is the size of staff devoted to this program? _

Since the beginning of the year, staff has been cut to one

individual for all six Ceco plants.

2. What are ECP staff qualifications (technical training,

interviewing training, investigator training, other)?

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No specific qualifications exist for the QFA, who has been

involved in the program a number of years. Guidelines for

interviewers are available but there are no specific

qualifications.

E. REFERRALS:

1. Who has followup on concerns (ECP staff, line' management, other)?

The QFA may do the followup himself or assign it to .another group

including line management.

F. CONFIDENTIALITY:

1. Are the reports confidential?

(Yes or No/ Comments)

2. Who is the identity of the alleger made known to (senior

management, ECP staff, line management, other)?

Information on the alleger identity remains with QFA.

3. Can employees be:

a. Anonymous? (Yes/No Comments)

b. Report by phone? (les, No/ Comments)

A toll free. number is available.

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G. FEEDBACK:

1. Is feedback given to the ' alleger upon completion of the followup?  :

(Yes-or No - If so, how?) .I

Feedback is given by mail or telephone.

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2. Does program reward good ideas? '

No  !

3. Who, or at- what level, makes the final decision of resolution?

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This is determined by QFA in conjunction with line management. ,

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4. Are the resolutions of' anonymous concerns disseminated?  ;

No .

5. Are resolutions of valid concerns publicized (newsletter, bulletin ,

board, all hands meeting, other)? l

No

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H. EFFECTIVENESS: l

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1. How does the licensee measure the effectiveness of the program?

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Not measured

2. Are concerns:

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a. Trended? (Yes or Lo/ Comments)

There are too few official " Records of Concern" (ROC) to

warrant trending. The QFA does informally look for common

concerns on items which do not warrant official ROCS.

b. Used? (Yes or No/ Comments)  ;

Corrective actions are addressed in the program.

3. In the last.three years how many concerns were raised? '

Closed? What percentage were substantiated?

The QAF screens comments and identifies those to be handled as

official Records of Concern" (ROC).

The following data is for ROCS from 1990 through August 1993. No

formal ROCS have been initiated'thus far in 1993.

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  1. Closed  % Substantiated ~f

LaSalle 2 100  ;

Byron 9- 22 l

Braidwood 6 33 i

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Quad Cities 3 33-

Dresden 4 25 1

Zion 1 0 1

Comments received during or after a refuel outage that the QAF l

determines do not warrant an official ROC are compiled and  ;

transmitted to plant management for information.1 This occurs  !

several months after the outage. ,

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4. How are followup techniques used to measure effectiveness (random [

survey, interviews, other)? j

No followup techniques utilized except perhaps for contractors  !

they see multiple times at different Ceco sites. ,

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5. How frequently are internal audits of the ECP conducted and by-  !

whom? .;

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There are no audits of this area. The onsite quality verification  ;

superintendent is responsible _ for reviewing information copies of _ <

quality ROCS to determine if additional QA reviews are warranted.

I. ADMINISTRATIVE / TRAINING: 1

1. Is ECP prescribed by a procedure? (Yes or No/ Comments)  ;

a

Nuclear Operations Directive (NOD)-0A.12, " Quality First Program j

Directive"

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2. How are employees, as well as contractors, made aware of this. 1

program (training, newsletter, bulletin. board; other)?

The program is briefly described-in Nuclear General Employee

Training (NGET). It may also be mentioned in . occasional safety ,

meetings or departmental tailgates. 'l

ADDITIONAL COMMENTS: (Including characteristics which make the program

especially effective or ineffective.)

In viewing the number of official " Records of Concerns (ROC)," that are-  ;

formally tracked, investigated, and resolved, the effectiveness of the  :

program is questionable. No ROCS have been generated thus far for 1993. H

This may be partially related to the staff reduction and availability of

personnel to conduct exit interviews. Due to the lack of resources, .

some concerns which would have been handled as official ROCS in previous "

years are now being handled more informally.

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The person completing this form please provide the following information to

.the Regional. Office Allegations . Coordinator and ' fax it 'to Richard Rosano at~ -

301-504-3431.

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NAME: TITLE:- PHONE #:

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David E. Hills / Senior Resident inspector'/ (815) 357-8611

DATE COMPLETED: 09-06-93 1

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