ML20101G729

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NPDES Noncompliance:On 841129 Weekly Analysis of Discharge Point 001 Showed Oil & Grease Concentration Above Tech Spec Limits.Caused by Large Amount of Oil in Turbine Bldg Sump. Sump Pump Shut Off & Sump Pumped Out
ML20101G729
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 12/06/1984
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To: Johnson E, Martin R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
References
P-84518, NUDOCS 8412270622
Download: ML20101G729 (2)


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, public Service Company IPOd a de V -

16805 WCR 19 1/2, Platteville, Colorado 80651 December 6, 1984 Fort St. Vrain Unit #1 P-84518

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Mr. Robert Martin, Regional Administrator /, )

Nuclear Regulatory Commission, Region IV DEC I 4 5 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011 ,

8 ATTN: Mr. E. H. Johnson

SUBJECT:

NPDES Noncompliance Report

Dear Mr. Martin:

In accordance with the requirements of Appendix B to the Fort St.

Vrain Technical Specifications, Section 3.2 a), this letter is to submit a copy of the NPDES. Noncompliance Report concurrently submitted to the Colorado Department of Health and the Environmental Protection Agency.

If you have any questions regarding this in' formation, please contact Mr. M. H. Holmes at (303) 57.-8409.

Sincerely, ,

J. W. Gahm Manager, Nuclear Production Enclosure

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NPDES DISCHARGE PERMIT NONCOMPLIANCE REPORTING FORM Date: Nov 30, 1984 Applicable Permit No. CO-0001121 Discharge No. 001 I. GENERAL A. Company: PUBLIC SERVICE COMPANY OF COLORADO Mailing Address:

Plant Name: Fort St. Vrain Plant Location: Platteville, CO County Weld-II. Noncompliance Report A. Description And Cause Of Noncompliance:

Weekly analysis of discharge point 001 (Goosequill Ditch) showed oil and grease concentration of 27.6 ppm, thereby exceeding the discharge permit level of 20.0 ppm. Cause was Tound to be a large amount of oil in the Turbine Building sume.

B. honcompliance Period:

Started: ~~

A.M. 1:00 P.M. 11/28/84 DATE Ended: A.M. 4:00 P.M._ 11/29/84 DATE Estimate Of Return To Compliance: 4:00 p.m. 11/29/84 i C. Action Taken To Reduce, Eliminate. Prevent: Sump pumps shut off immediately and sump pumped out. Follow-up samples taken to verify return of compliance.

D. Person Initiating Report Debra Schaub - chemist Person Autnor,ized o File Report: Jan Wagner 572-8265/ Bob Pearson

Title:

Signature:

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Signature: ,/ .

Signature of Plant Manager:Ad%/L E. Water Quality Control Division Notification Requirements:

Telephone (24 hrs) Date Person Notified Written (5 days) Date Copy: Jan Wagner, Belleview S.C./ Bob Pearson Room 946 HQB Plant File SUBMIT REPORT TO:

Mr. Stanley May Regional Administrator Colorado Department Of Health U.S. Environmental Protection Agency Water Quality Control Division 1860 Lincoln Street - Suite 103 Monitoring & Enforcement Section Denver, CO 80295 4210 East lith Avenue Denver, CO 80220 ATTN: Enforcement - Permit Program

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