ML19242A864

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LER 79-044/03L-0 on 790706:while Performing Reactor Low Water Level 1 Channel Calibr,Switch 1 Found Out of Tolerance Low.Caused by Instrument Drift.Instrument Recalibr & Returned to Svc
ML19242A864
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/03/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19242A854 List:
References
LER-79-044-03L, LER-79-44-3L, NUDOCS 7908060501
Download: ML19242A864 (1)


Text

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i o I :' ' [Whi le .per forming _PT 1.1.4PCu_ Reactor Low Water Level il Channel Calibration, a 3 [B21-LIS-N017B, switch I was found to be out of tolerance low. The required value is l 4 l

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