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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:RO)
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
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- 16805 WCR 19 1/2; Platteville, Colorado 80651 June 3, 1993 Fort St. Vrain Unit No. 1 P-93049 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Docket No. 50-267
SUBJECT:
Licensee Event Report 93-003-00, Final Report
REFERENCE:
Facility Operating License No. DPR-34 Gentlemen:
Enclosed is a copy of Licensee Event Report No. 50-267/93-003-00, Final, submitted per the requirements of 10 CFR 50.73 (a) (2) (B) .
If you have any questions regarding this report, please contact Mr.
M. H. Holmes at (303) 620-1701.
Sincerely, hDonWW. OlvuY Warembour Decommissioning Program Director DWW/JRJ Enclosure cc: Regional Administrator, Region IV '
Mr. Ramon E. Hall, Director Uranium Recovery Field Office Mr. Robert M. Quillin, Director Radiation Control Division Colorado Department of Hea)th 090040 l
9306100243 930603 i PDR ADDCK 05000267 -
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F ACluTY NAME (1) DOCP.ET NUMBER (2) PAGE (3)
Fort St. Vrain Nuclear Station 05000 10F 8 TITLt. (4)
New Natural Gas Source Within One-Half Mile EVENT DATE (5) LER NUMBER (61 REPORT NUMBER (7) OTHER FACILITIES INVOLVED (8) i f AG)Uf 4 NAMti DUGPET NUMBER I MONTH DAV YEAR YEAR f MON'M DAY YEAR gg uGw nam m tTNuMBEn
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LICENSEE CONTACT FOR THIS LER (12)
NAME TF.LENNE NUMtdEH qmouae Ar.a Cooep M. H. Holmes, Project Assurance Manager (303)620-1701 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE S VSTE M COVPONENT MANUFACTUREn CAUSE SYSTEM COMPONENT MANUFACTURER N
l SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED l MON
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ABSTRACT (Limrt to 1400 spacer,, i e., approximately 15 singie-spaced typewritten lines) (16)
On May 5, 1993, with the Fort St. Vrain (FSV) reactor permanently shutdown, defueled to the Independent Spent Fuel Storage Installation (ISFSI) and decommissioning actively in progress, a new source of natural gas was introduced within 0.5 mile of the ISFSI and the Reactor Building without prior NRC approval. This violates license conditions in both ISFSI Materials License No.
SNM-2504 and FSV Facility License No. DPR-34, and Technical Specification 5.11.
The event occurred due to field routing of a natural gas pipe from a new oil / natural gas well to a connection point which differed from the routing previously agreed upon by PSC and the well operator (outside the 0.5 mile restriction).
This condition was bounded by previous analyses of postulated ruptures of higher capacity natural gas pipelines much closer to the Reactor Building and ISFSI. The well operator isolated the new well until a new pipeline is installed, outside the 0.5 mile distance from these structures.
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$6G.ENLAL REr$ca NUMBER NVVBER Fort St. Vrain Nuclear Station 05000 93 003 0 2 8 m w n. so.c. ., ,.w.a . .~. - .a wc m ma, o n BACKGROUND:
The Fort St. Vrain Nuclear Station (FSV) is being decommissioned in accordance with the Decommissioning Order issued November 23, 1992, and FSV Facility License No. DPR-34. Spent nuclear fuel is being stored in the Independent Spent Fuel Storage Installation (ISFSI) in accordance with ISFSI Materials License No. SNM-2504.
License Condition 2.D(4) of the FSV Facility License states that unanalyzed sources of natural gas shall not be introduced within 0.5 mile of the location where spent fuel or radioactive graphite core components are stored without prior NRC review and approval.
Administrative Control 5.11 of the Decommissioning Technical Specifications reiteraces this restriction with respect to activated graphite blocks. License Condition 16 of the FSV ISFSI License states that no new gas or oil pipelines shall be installed within 0.5 mile of the ISFSI without prior NRC approval, as evidenced by a license amendment.
In March, 1993, Barrett Resources Corp. (Barrett) requested permission from PSC to drill 3 new oil / gas wells on PSC property which would be connected to the natural gas collection system that has pipelines in the vicinity of the FSV Reactor Building and the ISFSI. One of these wells is FSV Well No. 30, shown on the attached Figure 1. Barrett holds a lease to mineral rights in the vicinity of FSV. Barrett stated that the wells, and associated equipment and piping, would be outside of the 0.5 mile ,
radii from the ISFSI and Reactor Building. PSC granted permission for Barrett to drill the wells and connect them to the natural gas collection piping system near FSV, based on a 10 CFR 50.59 safety evaluation that concluded the 3 wells and their associated piping and equipment would be outside of 0.5 mile from the Reactor Building and the ISFSI, and would not constitute an unreviewed safety question.
PSC's safety evaluation recognized that the FSV natural gas collection piping system, which would be supplied gas from the three new wells (16 wells total), includes piping within O.G mile of the ISFSI and the Reactor Building. The safety evaluation assessed the effects of the three new wells on the previous pipeline rupture analyses. The ISFSI SAR discusses the analysis of the worst case postulated collection pipeline rupture consisting of a 4 inch diameter pipeline located 540 ft. to the north of the ISFSI. The worst case postulated collection pipeline ruptures evaluated for the Reactor Building consist of ruptures of a 4 inch diameter collection pipeline located 930 ft.
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0 3 8 rut w m w. v.w.a a. .m~ n.. e ~~c *n e o n to the southeast of the Reactor Building and a 6 inch line located 1340 ft. to the west of the Reactor Building. Postulated ruptures of 4 inch lines were modelled to release gas at a rate of 66 million cfd for 2 minutes, followed by steady state flow of 12 million cfd. Postulated ruptures of 6 inch lines were modelled to release gas at a rate of 120 million cfd for 1 minute, again followed by steady state flow of 12 million cfd. >
Modelling of plume dispersion for these postulated worst case collection pipeline rupture scenaries resulted in the determination that a flammable concentration of gas could reach a maximum horizontal distance of 197 ft. from the postulated !
rupture location for the 4 inch line ruptures, and 230 ft. from the postulated rupture location for the 6 inch line rupture. It ,
was determined in the safety evaluation that the addition of the three new wells to the FSV collection piping system would not result in natural gas release quantities in excess of those conservatively assumed in the analyses reviewed by the NRC, and it was concluded that no new natural gas sources would be introduced within 0.5 mile of the Reactor Building and the ISFSI that were ne' previously analyzed.
Natural ga: relw ces from accidents involving individual wells were also pe de '" analyzed. Due to the lower flow rates from ruptures fed by .ndividual wells (1 million cfd was considered a maximum credible flow) compared to flows from the 4 inch and 6 inch postulated collection pipelines ruptures, accidents involving individual wells were bounded by ruptures of collection pipelines.
The NRC's safety evaluation for Amendment i!o. 82 to the FSV Facility Operating License states the following in regards to accidents involving individual wells:
"The licensee's contractor performed analyses which concluded that rupture of the 2 1/2 inch well piping would not produce flammable gas concentrations further than 120 feet from a postulated break and that detonation of the gas plume or explosion of a metering shed would not affect the structural integrity of the reactor or turbine building...The NRC staff has reviewed these submittals and agrees with the licensee's conclusions. The staff has also performed independent flammability and explosive concentration limit calculations which further support these conclusions."
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0 4 8 texr w - ,o.c. v.w.a . .~ an., a ue ,m o n PSC's safety evaluation clearly stated that the three new wells, and new piping and equipment associated with the new wells, would be located outside of 0.5 mile from the Reactor Building and the '
ISFSI. It indicated that the flow pipe from new FSV Well No. 30 would tie into the existing flow pipe of FSV Associated Well No. .
1, outside of the 0.5 mile radius. This was based on phone conversations between PSC and Barrett personnel. PSC formally "
transmitted the draft safety evaluation to Barrett in a letter i dated March 16, 1993, requesting Barrett to respond in writing t with any corrments on the draft safety evaluation. Barrett ;
responded in a letter dated March 18, 1993, stating: ;
"The information presented in the Safety Analysis is correct as to the hookup of the new wells to the pipeline system."
i PSC finalized the safety evaluation and it was approved by the FSV Decommissioning Safety Review and ISFSI Safety Review ,
Committees on March 25, 1993.
Drilling commenced on FSV Well No. 30 on' April 1, 1993. The pipeline connecting FSV Well No. 30 to the FSV natural gas collection piping system was installed between April 28 and May 4, 1993.
4 EVENT DESCRIPTION: L On May 5, 1993, natural gas was introduced from FSV Well No. 30 into its 2 inch diameter flow pipe that was routed within 0.5 mile of both the Reactor Building.and the ISFSI, as shown on l Figure 1. This pipe constituted a new source of natural gas i
installed within 0.5 miles of these facilities without prior NRC review and approval. PSC discovered the situation on the afternoon of May 10, 1993, when concerns arose regarding an excavation under the Goosequill Ditch. Upon investigation, PSC determined that the flow pipe from FSV Well No. 30 had been routed under the Goosequill Ditch and connected to the flow pipe .
from FSV Well No. 1 (refer to Figure 1), within 0.5 mile from the '
ISFSI and the Reactor Building. This was a deviation from Barrett's plans.
This event was evaluated and PSC determined that the condition was in violation of the FSV Facility License, the ISFSI Materials License and out of compliance with Administrative Control 5.11 of the Decommissioning Technical Specifications. PSC promptly ,
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0 5 8 rur - . .c. ., . - ,....,~ % ,,, m n notified the NRC of this event on May 10, 1993. This LER is submitted in accordance with the requirements of 10 CFR 50.73 (a) (2) (B) .
ANALYSIS:
This event did not compromise nuclear safety at the ISFSI nor decommissioning safety in the Reactor Building. The worst case event which could have occurred, associated with the new natural gas source, would have been complete rupture of the FSV Well No.
30 2 inch diameter flow pipe at its closest point of approach to the ISFSI (approximately 1630 ft.) and Reactor Building (2408 ft.). Such an occurrence would have been completely bounded by previous analyses of flow pipe ruptures at the wells nearest the ISFSI (1163 ft. away) and nearest the Reactor Building (1184 ft.
away). Although an individual, newly completed, well typically produces approximately 150,000 cfd of natural gas, these analyses conservatively assumed a natural gas release rate of 1 million cfd (694 cfm) from a sheared flow pipe at the closest wells. It was determined that such a release would not result in a flammable concentration of natural gas near the structures of concern and hypothetical detonation of the gas cloud would not produce a significant overpressure at these structures.
Due to its distance from the structures of concern, worst case rupture of the FSV Well No. 30 flow pipe would have no effect on safety.
CAUSE:
The cause of this noncompliance was failure to adequately communicate understandings reached between PSC and Barrett with field personnel laying the pipe. Field routing of the 2 inch flow pipe used the most direct path, along the east side of Weld County Road 19 1/2, connecting to the flow pipe from FSV Well No.
- 1. However, this connection involved a different flow pipe path than that previously discussed and documented in PSC's safety evaluation. Also, PSC did not require Barrett to submit detailed routing plans of the FSV Well No. 30 flow pipe.
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Barrett isolated FSV Well No. 30 at the wellhead at 7:30 a.m.,
May 11, 1993. This prevented supplying the new pipe within 0.5 mile of the ISFSI and the Reactor Building with gas and oil from new FSV Well No. 30. This action did not depressurize the new pipe, which was pressurized from FSV Well No. 1.
Depressurization of this piping was not considered warranted from a safety standpoint, since the new flow pipe is substantially further from the structures of concern than those previously analyzed, as discussed above.
Barrett has committed to maintain FSV Well No. 30 isolated until -
its flow pipe can be routed outside of the 0.5 mile radii, and connected to the FSV Associated No. 1 flow pipe, as originally planned. A survey has staked out the 0.5 mile radius from the ISFSI (which is more limiting than the 0.5 mile radius from the Reactor Building) in the area of interest. It is anticipated that the new pipe will be installed and FSV Well No. 30 returned to service in early June, 1993.
PSC has informed Barrett that for future wells, survey teams will stake out the 0.5 mile radii prior to installation of new sources of natural gas which could potentially be placed within 0.5 mile of the ISFSI or Reactor Building. PSC will also require detailed pipe routing plans for proposed natural gas / oil wells located within 3/4 mile of the ISFSI or Reactor Building and located between the South Platte River and St. Vrain Creek, and for any natural gas / oil piping planned to be routed within this zone.
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NRC FORU 3%A (S-92;