ML20010H874

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Monthly Operating Rept for Aug 1981
ML20010H874
Person / Time
Site: Oyster Creek
Issue date: 09/16/1981
From: Sklar J
JERSEY CENTRAL POWER & LIGHT CO.
To:
Shared Package
ML20010H870 List:
References
NUDOCS 8109290375
Download: ML20010H874 (12)


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M1mILY OPERATIONS SGNARY AUGUST 1981 At the beginning of the reporting period, the Oyster Creek Nuclear Generating Station was operating at 370 FWe limited by degraded condenser vacuun. '1he Drywell Unidentified Icak Rate was gradually increasing and being closely monitored. Between August 1 and August 14, load fluctuated between 330 FWe and 410 Mie dependent upon intake temperature and its effect upon condenser vacuum. On August 11, the plant was released fran systen to shut down to correct the Drywell Unidentified Leak Rate and Condenser Vacuan problens. '1he plant was shut dom and in the cold condition on August 15. Startup was delayed into the next reporting period by a tube failure in the Shutdown Cooling Systen and depends upon the results of tests currently in progress.

'ite following Reportable Occurrences occurred or were identified during the nonth of August:

R.O. 81-38 was identified on August 28 when two out of three Shutdown Cooling heat exchangers were out of service due to tube failures.

g R.O. 81-39 was identified on August 14 when West Deactor Building Closed Cooling Water heat exchanger tube leakage had resulted in an unmonitored release of radioactivity to the environment.

R.O. 81-40 was identified on August 16 when the setpoints for Electranatic Relief Valves B & D were found to be less conservative than Technical Specification requirements.

R.O. 81-41 occurred on August 24 when "A" Stack Gas Sample Pump tripped.

R.O. 81-42 occurred cn August 28 when "B" Stack Gas Sample

Punp tripped.

R.O. 81-43 was identified on August 29 when it was postulated that there was no stack gas monitoring in effect due to leakage in the sanple system.

R.O. 81-44 occurred on August 25 when SBGTS I Fan 1-8 bearings failed.

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OPERATING DATA REPORT y

. .' g OPERATING STATUS UNIT NAME... OYSTER CREEK DOCKET NUMBER.. 50-219 UTILITY DATA PREPARED BY...J.B. SCAR 639-693-6013 .

REPORTING PERIOD... Auoust 1981 LICENSED THERMAL POWER (MWT).. 1930 NAMEPLATE RATINC(GROSS MWE).. 650 DESIGN ELECTRICAL RATING (NET MWE).. 650 MAXIMUM DEPENDABLE CAPACITY (GROSS MWE).. 650 MAXIMUM DEPENDABLE CAPACITY (NET MWE).. 620 IF CHANGES OCCUR IN CAPACITY RATING SINCE LAST REPORT. GIVE REASON...

NONE POWER LEVEL TO WHICH RESTRICTED. IF ANY(NET (1WE)... NO RESTRICTION RhSON FOR RESTRICTION. IF ANY... '

NO RESTRICTION MONTH YEAR CUMULATIVE HOURS IN PERIOD 744.0 5831.0 102479.0 HOURS RX CRITICAL 341.6 4308.7 76739.3 RX RESERVE SHUTDOWN HRS. 0.0 0.0 46G.2 HRS. GEN ON LINE 337.7 4088.6 75057.5 UT RESERVE SHUTDOWN HRS 0.0 0.0 0.0 GROSS THERMAL ENERGY 414700.0 6411140.0 126557620.5 GROSS ELEC ENERGY 119610.0 2058140.0 4298e385.0 NEI ELEC ENERGY 111030.0 1962070.0 41400728.0 UT SERVICE FACTOR 45.4 70.1 73.2 UT AVAILABILITY FACTOR 45.4 70.1 73.2 UT CAPACITY FACTOR MDC 24.1 54.3 '6.6 UT CAFACITY FACTOR DER 23.0 51.8 62.2-FORCED OUTAGE FACTOR 54.6 i5.3 7.1 THE NEXT SCHEDULED OUTAGE IS TO BEGIN ON FEBRUARY 12. 1982

AVERAGE DAILY POWER LEVEL 4 DOCKET O...... 50-219 UNIT.......... O. C. ?1 REPORT DATE. . . Septe:aber 16. 1981

' COMPILED BY... J.B. SKLAR TELEPHONE..... 609-693-6013 i

MONTH August 1981 DAY NW DAY NW

i. 349. 17. O.
2. '30. 18. O.
3. 320. 19. O.
4. 311. 20. O. , ,,
i. 5. 313. 21. O.
6. 324. 22. O.
7. 328. 23. O.
8. 322. 24. O.
9. 325. 25. O.
10. 344. 26. O.
11. 342. 27. O.

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12. 349. 28. O.
13. 382. 29. O.

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14. 362. 30. O.

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15. 4. 31. O.
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DOCKET NO.

50-219 UNITSilUTDOWNS AND POWER REDUC 110NS UNIT NAME Oyster Creek i

DATE Septenter 16. 1981 August 1981 COMP 1.ETED BY J.B. Sklar REl'OllT hl0N'111 TEl.EP110NE 609-693-6013 4

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, .$ E g Licensee 5% Cause & Corrective No- Date g 3g 7 .E

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$E 5 jgg Repor # Av v Psevent Recurrence S

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, 18 8-15-81 P 406.5 B 1 N/A ZZ ZZZZZ Shutcbwn to correct an increasing l Drydell Unidentified Ieak Rate and Condenser Vacutun problens.

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4 i 2 3 4 F: Forced Reainn: Meilsod: Ealiible G. Insitucilon S: Scheduled A Equipmens Failure (Explain) . Manual for Pseparation of Data ll4taintenance or Tesi 2-e anual Scram. Entry Sheets for Licensee l C Itefueling 3 Automatic Sciam. Event Report (1.ER) File (NUR1:G-D Itegulaiosy Resielclion . 4 Other (Explain) 0161)

. E Opesalor Training & Ucense Exaininallon

, F Administrailve 5

. . _ . _ . G-Oncrallunal Ensur IFuntaint . . _ . . . 8:

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AUGUST SURRRY OF QASL MBCilANICAIo MAIN'IENANCE

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EQUIPMENP MAIRJNCTIm CORRDCTIVE ACTIM Outside Ibactor Building Operating linkage bent Linkage was repaired for Airlock Door satisfactory door operation Fire liose Station Valve Valve leaking through Ibnoved valve, disasscmbled V-9-102 and cleaned valve seat.

Position indicator for Indicator does not show Adjusted indicator to show Fire Valve V-9-150 valve open or closed proper position Pcnd Ptup Water leaking fran Tightened packing gland to stop packing gland leak CRD 26-19 Nitrogen leak around Installed new cap.

Acctmulator charging connection cap Fire protection system Deluge System 40-Gasket on Replaced Gasket.

downstream side of V-9-158 leaking Watnrtight ccmpartnent One dog frozen on watertight Disassenbled dogs, cleaned, door S.E. -19 el. door lubricated, and reassenbled.

1-2 diesel generator lube Ptmp running noisy Ibadjusted cotpling oil recire ptmp "C" Shutdown Cooling Pipe plcq in ptmp casir.g Replao3d pipe plug.

Ptmp leaking Ibfueling Bridge Air Line Take-Up reel Inspected reel and adjusted tension (CAB nounted) needs as necessary adjustment Torus vent valve Valve operator diaphragm Ibplaced with new diaphragm V-28-18 leaking Exhaust fan - Belts slipping on sheaves Replaced belts and adjusted augnented off gas tension.

building

5 AUGJST SUl4%RY OF QASL WCliANICAL MitIN'ID1ANG (cont'd)

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Ecumerr mLancr1m coRmcT1vE AcrION "B" emergency servi Discharge flange leaking Tightened flange bolts water-ptmp CBD Accumulator 46-35 Leakage around acctmulator ' epla l d all o-rings on piston and cylinder ends.

West RDOW lieat Exchanger Tubes leaking 'IWelve tubes plugged and reinspected.

Ibpla d anodes.

East 10CN Ileat Exchanger Tubes leaking 'Nelve tubes plugged and reinspected.

Replamd anodas.

"B" Stack Gas Sanple Ptmp . Drawing excessive anps Disassembled, cleaned and lubricated internals. Ibassenbled and returned to servim.

CRD Accumulator 14-23 V-lll valve body turns in Tightened valve body back into valve block valve block Isolation' condenser Packing leaks Added two rings of packing, drain valve V-14-37 1-2 RBCCW lleat Exchanger 3/4" drain nipple on Replaced nipple service water side is broken off CRD Acctrnulator 46-31 V-106 valve leaking past seat Disassenbled, lapped seat, replaced when valve is closed ball and packing. Reassenbled valve.

Shutdown cooling Icaking from packing gland Replaced 9 rings of packing.

isolation valve V-17-19

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AUGUST 51tNARY OF OMIo INSTFp6T MLMHWJCE .,

EQUIPFETP MMENCPIG1 CDRIECPIVE ACPIO1 Traversing in core #3 Prtte Defectim #3 Detector Maintenan ' and Calibration Calibration System (replaced detector)

Steam Flow Ibcortbr Ibd pen sticks freqmntly Maintenance and Calibraticn (on recorchr)

Internediate range nonitor Frcnt panel discrepancy ibintenan and Calibration channel #17 (burnished relay contacts) _

Area Radiation nonitor Pailed Downscale Maintenance and Calibration (environs nonitor #1) (replamd sensor)

Ilydrogen ibnitor "B" Unit No flcn indication thintenan and Calibration Auxi'lary off gas building (noisture in flow element)

Main Steam Line Radiation Front panel discrepancy Maintenanm and Calibraticn obnitor 01annel #1 (recorder calibration)

Traversing in Core Probe #1 Defectiw #1 detector Maintenan and Calibration (ruolamd cbtector)

Source Range Fbnitor Olannel Upscale Period Meter J1 Maintenance and Calibration

  1. 23 Internediate Range Fbnitor Frtr.t panel. discrepancy Calibration of recorder 01annel #16 on recorchr IIN surveillanm discrepancy No rod block dwn. scale Exact set point adj. per vendors 01 11 and 16 , lite manual and procedures. Tested satis factory.

A.O.G. 112 chator reading Repl. sensor and calibrated.

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. AUGUST SUFf4ARY OF OASL INSTIGHTP MAIrnHWEE (cont'd) '

_EQUIPFD7f MAIJUFCPIM CDRRECTIVE ACfION Drywell/forus 02 Analymr Sticking Cleaned bushings and brush assenbly Iboorchr performed calibration A.O.G. 01 art Ibcorder Not taking up Chart paper installed incorrectly Ibplaced ink cartridges 1-2 Fire Diesel Fire Ptmp Cycling Switch is set properly at 85 psi System is opemting at/or around this pressuw.

Process Rad Monitoring Surveillanm discrepancies Alarm set-points found to be within FEL 01.1 and 2 on alarm set-points toleranm per procedure I.R.M. 14 Ibd Block malfunctica Cleaned relay contacts. Performed bench calibration. Detector scheduled for repla trent.

Control rod drive pcsition Defective probe on scram Replace position probe indication 10-23 position I.R.M. nonitoring diannels Not indicating properly Replaced pre-anp on ch.17 performed 15 and 17 bench calibration on both 15 and 17 Control rod drive position Defective probe on Ibplaced position probe indication 34-11 position 18 MSL break sensor RE22F Dirty snubber Replaced smacr during routine surveillance of RS22F.

Condensate transfer ptmp Broken G.uge Ibplaced broken gauge 1-2 Drywell Ilumidity Ibcorder Does not rotate at proper Replace <*. diart drive notor speed

AUGUST SUMAIN OF OASL INSTRUMENT MAINIENANCE (mnt' d) '

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EQUIP!01T MALM11CTION 00RRECI'IVE ACI'IO1 Event Ibcordar Chart paper not taking up Paper janned. Iblmded chart and tested satisfactory ll Drywell Air Tenp 01 art paper will not drive Ib-installed drive chain and Recortbr adjusted idler wheel Fuel pool AIN Spiking Replaced d3fective sensor and IO-15C-10 '

converter I .R.M. 01. 15 Inoperable: produces half- Peplaced defective dual trip unit scram when taken out of by-pass I.R.M. 01. 16 Spiking causing half-scram Pepaired broken wire on J4-3 I.R.M. 01. 15 Inoperable: defective Beplaced detector, drive tube, detector o-ring and retainer S.R.M. 01. 22 Trip being brought in Replaced defective pre-anp with early: reads 1 d3cade calibrated operational spare higher than other three channels S.R.M. OI. 23 Trip being brought in Replaced drawer with celibrated early: erratic. SRM operational spare inoperable S.R.M. 01. 24 Surveillance discrepancies. Adjustncnts made accordincj to procedure 721.3.001 to correct discrepancies I.R.M. 01. 16 Spiking causing half- Cleaned connector at detector scram. Trip being brought connection in drywell. 01ecked in early. all other connectors.

AUGUST StBNAIN OF QASL ELECTRICAL MAINIU1ANCE '

. i r RXIIPMENT MALEUTCTION (DRRECTIVE AC'I' ION Energency Diesel Generator 82 Outer Insulation Covering Repaired taped cable with 3M Conpany on cable leading frarn #33 electrical tape and #70 silcone Governor was degrad3d tape as final wrap A.O.G. Building Water Ibnoval 'Ihernostat not functioning Rewired liigh Tenperature 'Ihermostat System properly on refrigeration to operate properly.

unit A.O.G. Building Ibocnbiner Wire !!arness Shorted Ibplaced hermetically sealed unit and Motor "B" Electrically wire harness.

RX Building Air Iock Doors Interlock solenoids Double nutted all solenoid nounting misaligned bolts to secure realignment.

RX Building N/W Air lodt Inproper alignment of Retighten all mounting bolts so solenoid Door interlocking mechanism would line up properly to interlocking nochanism.

RX Building Ibfueling Crane lloist loaded lih did not go Found grapple binding. M3dlanics lepaired out when hoist was unloaded grapple. Light was readjusted with test load ard put back inservice.

Diesel Fire Punp liouse DC-30 bbdule not working Installed new BC-30 nodule in control Fire System panel at fire pond house.

4160 Bocm-Fire Protection Degraded fusible links on Installed new fusible links on C&D Boss System ventilation danpers Ventilation System - Fire System.

Oyster Crack Station il Occket No. 50-219 REFUELING INFORMATION -

Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: February 12, 1982 Scheduled date for restart follcwing refueling: August 13, 1982 Vill refueling or resumption of operation thereafter recuire a Technical Specification change or other license amendment?

A Tech Spec Change Pequest to incorporate G.E. fuel assenblies will be subnitted by Octccer 1,1981.

Scheduled'date(s) for submitting proposed licensing action and supporting in fo rma t ion :

Marcit 9,1981 - Ccnplete NEDO docu ent #24195 (G.E. Reload Fuel Applicaticn for Oyster Creek) was subnittwi.

Important licensing consider-'-ions associated with refueling, e.g. , new or

.different fuel design or su:3 'er, unreviewed design or performance analysis

' methods, significant changes in fuel design, new operating procedures:

1. General Electric fuel asserblies - fuel design & performan analysis methods have been approved by the NFC. New operating procedures, if necessary, will be subnitted at a later date.
2. Exxon Fuel Assenblies - No major enanges have been made nor are there any anticipated.

- 560 The number of fuel assemblles (a) in the core (b) in the spent fuel storage pool.. 781 The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

Present: 1,800 Flanned: 2,600

'The projected date of the last refueling that can be discharged to the spent fuel peal assuming the present licensed capacity:

me Spring 1987 Outage.*

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  • NOIE : his is for a normal refueling. Full core off-load, however can cnly be l accanodated through about 1983 or L984 with 1800 licensed locations. l l

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