ML19207B124

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LER 79-059/03L-0 on 790718:discovered Low Fluid Level on Snubber 2E51-40SS87,RCIC Pump Suction.Caused by Leaking Seals.Snubber Replaced
ML19207B124
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/15/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19207B121 List:
References
LER-79-059-03L, LER-79-59-3L, NUDOCS 7908230404
Download: ML19207B124 (1)


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7 8 60 61 DOCKET NUMBER 68 69 EVE'JT D ATE 14 75 REPORT D ATE 80 EVENT GESCRIPTION AND PROBABLE CONSEQUENCES h o 2 bitriw normal plant operation, snubber 2E51-40SS87, RCIC Pump Suction, was noticed to I o a have a low fluid level by plant personnel. Tha snubber was functionally tested, and itl o 4 Ifailed the test. l 0 sj gechnical Specfication 3.7.5, 6.9.1.9b l Lo ' 6 1 I 7 I O.' I O 8 l  !

7 8 9 80 SYSTE\1 CAUSE CAUSE COYP. VA LV E CODE CODE SUBCODE COVPON ENT CODE SUSCODE SUSCODE 7

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_ 21 22 23 24 26 27 28 29 Ju 31 32 T K ACT ON O PLANT 4 HOURS S B IT FOR 8. SUPPLIE MANUFACTURER

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43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l The low fluid level was due to leaking seals. The snubber was replaced with one from l

, 3 l stock. This snubber will be counted as inoperable on the next visual inspection of  ;

, ,,  ; accessible snubbers per Technical Specifications. ,

t 1 l l 1 4 l t 7 3 9 80 ST S ". POWER OTHER STATUS IS OV RY DISCOVERY OE%RIPTION 1 5 [Ej @ l0l9 5 l@l NA l l A l@l NA l A TIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RE' EASE RM d[_Zj 7

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@ l Z l@l NA l NA l 10 11 44 45 80 PERSON %E L E kPOSURES NUMBER TYPF OESCRIPTION d d l 0l 0l 0l@ lZ l@l NA l PERSONNEL INJURIES NUV8ER DESCRIPTION I a 0l 0 l 0 l@l NA y.

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