ML19208D484

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LER 79-080/03L-0:on 790830,primary Containment Ambient Temp Exceeded Tech Spec Limits,Causing Small Steam Leak.Caused by Leakage & Steam Cut of King Pin Cover on Feedwater Check Valve B21-F010B.Leak Repaired & Leakage Decreased
ML19208D484
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 09/25/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19208D481 List:
References
LER-79-080-03L, LER-79-80-3L, NUDOCS 7909280475
Download: ML19208D484 (2)


Text

NRC FORM 366 U. S. NUCLE AR REGULATOR) COMMISSION l.lCENSEE EVENT REPORT CONTROL BLOCK: l

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(PLEASE PRINT OR TYPE AL. REQUIRED INFORMATION) l0l1lly lC B E p 12 l@l0l0 l010 0l0j 01- Ol01@l d 1LICLNSE1l1l1 LICENS" NUWr H 25 /t> T)PE JU l@lSt CAT l

$8 1 8 9 CICENSEE CODE 14 1S CON'T lolIl 3[g" , ' L @l 610l 5 l 0DOCKE l - l T0NUVBEH l 3 l 2 l 4 68l@l630 8l3 0l7l9l@l 0g9l2 5l7l9 g EVENT DATE I4 75 HEPORT D ATE Su

  1. 8 bo EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 IDurinn normal plant operation, the primary containment ambient temperature exceeded j o 3 l135 F (135.176 F). The temperatures over the previous several days had been 133-134 F l 1014 l lwith all available dryvell coolers > operating. Drvwell leakage had increased to approx-l 0 s limately 2 epm and airborne particulate activit:. wac higher than normal, indicating a l 0 6 lsnall steam leak. The heat load on the RBCCW system was high due ~; high service l o 7 Iwater iniection temperature. RWC U.reiectinn to the hotwell, and supplying the 20 gpm l O 8 Iconcentrator in radwaste. Technical Specification 3.6.1.6, 6.9.1.9b 90 l

7 8 9 SYSTEM CAUSE C AUSE C O'? P. VALVE CODE CODE SU8 CODE COMPONENT CODE SU6 CODE SUBCODE O 9 IS 9

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_ SE QUENTI AL OCCUR R E NCE HEFOHT REVISION LE k HO EVENT YE AH HEPOHT NO. CODE TYPE NO.

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l-l l0l8l01 y l 01 3l Ll l- 0l 31 21 23 24 26 2/ 28 2') 30 31 ACTION FUTUHE EFFECT SHUTDOWN ATT ACHYE NT NPHD 4 PHIVE cnvP. COMPONENT TAKEN ACTION ON PL ANT METHOD HOJHS SU8VITTED FORY dUlt SUPP LI F H MANUFAC'UHER lx l@l z l@ lzl@ Izl@ 01010101 LY,j g 41

[Nj @ lA g lAl3l9 3]g 33 34 35 Ju 3/ 40 42 43 44 4; CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 1 o lRWCU reject to the hotwell was decreased from 130 gpm to 100 rpm and service water flow 1 Ii Ii l lto the RBCCW heat exchangers was increased. This lowered the RBCCW outlet temperature l lil2l [from 99 F to 89 F and drvvell ambient temperature was lowered from 135.176 F to 1340F,l lil3l During the recent outage, it was discovered that the King pin cover en the feedwater l g [ check valve B21-F010B was leaking and had a steam cut. This leak was repaired and l 7 8 9 (CON '1)so ST S N POW E H OTHER ST ATUS b V FY DISCOVE HY DESCHiPTION li ls j lE l@ l 0l 9 l 4l@ NA l l A l@l Operator Surveillance l 7 8 9 to 12 11 44 4 ', 46 80 AC TIVI T Y CONTENT J d)

RELEASED OF HELE AGF AVOUN T OF ACTIVITV LOC ATION OF HELE ASE i o Iz I @ l zj@l NA l l NA l

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L OSS OF OR DAYAGE TO F ACILITY TYPE DESCHIPTION 'l i a Lz_J@l u^ 790928o 4 i F 8 9 10 3 80 iss l

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A. C. To111soa, Jr. 919-457-9521 o N AME OF PnFPAF10 Ft PHONE S,

LER CONTINUATIOff -- RO# 2-79-080 Facility: BSEP Unit No. 2 Event Date: 8-30-79 during subsequent power operation, drywell leakage had decreased to agprox-imately 0.2 gpa and the containment temperature was averaging 120-125 F.

The surveillance that detected this event is a daily computer check of dry-well temperatures. This surveillance has been increased to a frequency of once per shift to better detect rising temperatures, and to provide for an earlier initiation of methods for temperature reduction before c::ceeding any limits. This is considered an isolated event and no further action is required.

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