ML19257B397

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LER 79-105/03L-0:on 791219,during Normal Testing,Rip Valves X82B & X58B,E & F Found Not Operating Properly.Caused by Limit Switch on X82B,E & F Not Fully Opening,Restricting Valve Operation.Valve Adjusted
ML19257B397
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/07/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257B387 List:
References
LER-79-105-03L-01, LER-79-105-3L-1, NUDOCS 8001150659
Download: ML19257B397 (2)


Text

(1 498 LICENSEE EVENT REPORT -

CONTROL BLOCK: l 1

l l l l l lh 6

(PLEASE PRINT OR TYPE ALL REQUtRED INFORMATION) l 1JOl@l61 CA T 68l@

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% lN 7 8 9 lC lBLICENSEE lE lP CODE l1 l@l0 l0 l- l0 l0 l0 14 16 l0 l0 "l -l .0l n l@l LICENSE NuM8EH 25 4 26 l 1 lLICENSE 1 l 1TYPE CON'T O 1 Ev'n"c, dl 01 5 l Ol -l Ol 3l 2 l 5 @l1EVENT 68 69 l211'lol71o@l0111ol7lAlnl@

OATE 74 75 REPORT DATE 80 7 8 60 61 DOCKET NUM8E R EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l During normal testing prior to startuo. the conerni nne*,ene nne4 coa ch,* I o a l RIP valves X82B and X58B, E, & F were not operatine oroneriv.

I ITTT11 o s l I

1016 I l I

10171 I Technical Specification 3.6.3, 6.9.1.9b ,

80 E CODE S SC E COMPONENT CODE SUSC O'E SU E ULL9_I 8 9 LsLnJ @ Ir J@ LxJ@ I TIJ l" I s i m i n l n l8 L.SJ@ I z i @

10 11 12 18 19 20 7

OCCUR AENCE REPORT REVISION SEQUENTI AL R EPORT NO. CODE TYPE NO.

tg p EVENT YE AR

@ ,ag,go 17l9l l-l 'l110l5l l/l 1013 l l30 Ll l-l 31 10 l 32 21* 22 23 24 26 27 28 29 HOURS S8 iT FO 1 8. 5 PPLIE MANUP ACTL RER KN AC ON ONP NT ME l3JX l@lJ4X l@ l35Z l@ lZl@

36 lCl0l0l0l JI 40 lY l@

43 lY 42 l@ lNh 43 44 A 15 l 5 l 247l@

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS The limit switch was I i O l The limit switch on X82B was found to be out of adiustment.

i i correctly adjusted, the valve stroked successfully and returned to service. The I i

2 l manual air isolation valve to X58B, E & F was found nc,t fully open, restrictine i 3 l valve operation. The valve was fully opened and the valves tested satisfactorily, ml The reason for the valve beine partially closed could not be determined. (Continitedil80 7 8 9

% POWER CTHER STATUS dis RY OISCOVERY OESCRIPTION 1 s lClh l0l0l0l@l NA l l Alhl Operator Surveillance l ACTIVITY C$ TENT RELE ASEo OF RELE ASE AMOUNT OF ACTivlTY LOCATION OF RELE ASE l

(l.J 6_j d h l_Z.jhl NA NA PERSONNEL EXPOS ES NUM8ER TYPE DE SCRIPTION l

I 7 l 0 l 0 l0 l@l' Z lhl NA

' PEnSONNEt iN;UliES NUYSER DESCRIPTION 1/4/ 025 l

2 4 8 9 In lo lo l@l 11 12 NA 80 LOSS OF OR OAuAGE TO FACILITY TYPE DESCRIPTION L'_lojlt.J@l si 80 I

7 8 9 10 2 o ISSUED

[3 J @) DESCRIPTION u l llllllltill!l]

68 69 80. ;

7 8 9 to NAME OF PREPARER A. C. Tollison. Jr. PHONE: 919-457-9521 $

30011 l

LER CONTINUATION - RO# l-79-105 FACILITY: BSEP Unit # 1 EVENT DATE: 12-19-79 -

All I&C technicians will review this LER as a reminder to insure that all instru-ment air supply isolation valves are completely restored to their normal position after testing or maintenance on the associated equipment.

1747 026 O

9