ML19341A228

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LER 80-115/03L-0:on 801222,reactor Vessel Conductivity, Exceeded 2 umho/cm2 for 27.3-h W/Highest Measured Value at 3.35 umho/cm2.Caused by High Conductivity Condensate in Heater Drains Sys Being Concentrated in Vessel
ML19341A228
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/15/1981
From: Poulk R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341A225 List:
References
LER-80-115-03L, LER-80-115-3L, NUDOCS 8101220409
Download: ML19341A228 (1)


Text

NRc FORM 366 o,,,...,,,,5..,,,,,,,,,,,,,,,,,,,,,,..........

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  • LICENSEE EVENT REPORT CONTROL BLOCK: l 1

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75 l i i sDATE i a l i 80l@

EVENT DESCRIPTION AND PROS A8LE CONSEQUENCES h 2 O 2 l Durine normal oneration reactor vessei conductivity ovceeded 2 emhn/cm for 27.3 I O 3 l hours with the highest measured value at 3.35 umho/Cm2 This event did not affect  !

l the health or safety of the public. l O 4

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[o.12 ] I I O 18 I 1 Technical Specification 3.4.4.2, 6.9.1.9b l 80 SYSTEM CAUSE CAUSE COMP. VALVE COOE COOE SU8 CODE COMPONENT CODE SUSCODE SU8 CODE LI B 7 8 I clo I@ LxJ@ l z l@ Iz Iz Iz Iz Iz I zl@ O@ LZJ @

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OCCURRENCE REPORT REVIS'ON

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EVENT YE AR REPORT NO. CODE TYPE NO.

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a O17 RE,PjE l8l0l l-l l1 1l5l y l 0l3 l {30 g31 l 0l 32

,21 22 23 24 26 27 28 29 T KE AC N L T ME O HOURS SS IT POR 8. St.P Lt MAN AC RER lXlgl4 gg lSZlg W@

33 4 J 36 l 0l 0l 0l 0l 33 40 lhlg el g g g g 42 43 lZl9l9l9[g 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h .

1 gl High vessel conductivity was caused by high conductivity condensate in the heater l i i l drains system being concentrated in the vessel. Forward pumping to the vessel of  ;

heater drains condensate was reduced until its conductivity was lowered, and Nn'CU g i ., l 2

gl was used to reduce vessel conductivity to less than 2 umhos/cm . This is considered; i 4 l to be an isolated event and no further action is required. l 30 7 8 9

% POWER OTHER ST'ATUS dis O Y DISC ER DESCRIPTION ST U RoutineC$emI,strySamp ITTil l E l@ l 0l5 l 0l@l NA l lA lgl 80 l

3 11 4 4 46 t TavtTY C3 TENT KELEASE AMOUNT OP ACTivtTY LOCATION OP RELEASE NA

[,1,,j_s_j W @D OP RELEASEM@l NA l l 30 l

F 8 9 10 11 44 45 PERSONNEL EXPOSURES NuYBE R TYPE DESCRIPTION i 7 l0l0l0l@[Z_j@l NA so l

' ' ' PERSOwE ' 53 L is;UR'iES Nuvet a DESCRIPTION l

7 1 H a 3 l 010 l 0 l@l NA 11 12 80 LOSS OF On OAMAGE TO FACittTY Q i TYPE CE SCRIPTION  %,,/

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LzJ@l NRC USE ONLY ,

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80 3 NAME OF PREPARER R. M. Poulk, Jr. PHONE: 910-457-09')1 E

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