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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141A5021997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Oyster Creek Nuclear Generating Station ML20141H7441997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Oyster Creek Nuclear Generating Station ML20137X8231997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Oyster Creek Nuclear Generating Station ML20137C3771997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Ocnpp ML20134P6151997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Oyster Creek Nuclear Generating Station ML20133M1751996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Oyster Creek Nuclear Generating Station ML20132D1011996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Oyster Creek Nuclear Generating Station ML20134M9761996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Oyster Creek Nuclear Generating Station ML20129B1631996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Oyster Creek Nuclear Generating Station ML20117M7561996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Oyster Creek Nuclear Generating Station ML20116M6761996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for Oyster Creek Nuclear Generating Station ML20115F8561996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Oyster Creek Nuclear Generating Station ML20112J7431996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Oyster Creek Nuclear Generating Station ML20112A6891996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Oyster Creek Nuclear Generating Station ML20101R0401996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for Oyster Creek Station ML20101D7701996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Ocnpp ML20100G5101996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Oyster Creek Nuclear Generating Station ML20096E8071995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Oyster Creek Nuclear Generating Station ML20099L7571995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Oyster Creek Nuclear Generating Station ML20094P8431995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Oyster Creek Nuclear Generating Station ML20093H3571995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Oyster Creek Nuclear Generating Station ML20092H7741995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Oyster Creek Nuclear Generating Station 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
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'O AVEPAGE DAILY P20ER LEUEL j
DCCEET 4..... 50-219 4 UNIT. ...... O. C. ?1 REPORT DATE... June 4, i980 CGMPILED BY... C.M. MCCLAIN 3 TztEpsesE. . . 204-455-e74e i
MONTH May i'?80 i
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- 9. O. 25. O.
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?f'a' AT', 'REPARED DY...C.M. HCCLAIN 291-455-2740 g
'EPOP'INC 2ERIOD... May
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1980 I t! CENSE" TuERMAL POWEP: H 'P '- .. 19M
%, epi _ : re R ATING <. GRGSS MWE ) . . 6'SO DESIGN ELECTPICAL RATING (NET MWE).. 650 i
rm.t Ir1UM DEPENDABLE CAPACITY (GROSS MWE) . 650
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MAXIMUN DEPENDABLE CAPACITY (NET MWE).. 620 IF CHANGES OCCUR IM CAPACITY RATING CINCE LAST REPORT, GIVE REASON...
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NONE POWER LEVEL TO WHICH RESTRICTED, IF ANY(NET MWE)... NO RESTRICTION I REASON FOR RESTRICTION, IF ANY...
NO RESTRICTION I MONTH YEAR CUMULATIVE HOURS IM PERIOD 744.0 3647.0 9151i.0 4
MCU'S RX CRITICAL 0.0 101.5 68740.8 1 RX RESERVE SHUTDOWN HRS. 0.0 0.0 463.2 HPS, GEN ON LINE 0.0 98.4 67403.9 UT RESERVE SHUTDOWN HRS 0.0 3.0 0.9 I GRCSS THERMAL EMERG'r 3 . T ~' - .. -1026769.9 GROSS ELEC EHERGY 0.0 $3670.0 39935985.0 t
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POCKET NO. 50-219 __,
UNIT SHUTDOWNS AND FOWER REDUCDONS UNIT NAME Oc #1 DATE I"n a 11: 14An
- COMPLETED BY C. M. McClain REPORT MONTH Mav - 1980 TELEPHONE 455-8748 "t.o c w
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No. Date
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Licensee Event E,,
mg Cause & Correceive Action to H
bE 5 jif5g R: port # j Prevent Recurrence d
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1 800105 S 744.0 C 1 NA ZZ ZZZZ Refueling / Maintenance Outage l
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i 2 3 4 I F: Forced Reason: Method: Exhibit G-Instructions A-Equipment Failure (Explain) 1-Manual for Preparation of Data S: Scheduled B-Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee
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C-Refueling 3 Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & Ucense Examination
- F-Administrative 5 G4)perational Error (Explain)
- Exhibit I-Sanw Source (9/77) Il-Other (Explain) i
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Oystcr Cr ck Stetten #I
Dock 3t No. 50-219
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OPERATION
SUMMARY
MAY 1980 The plant was shutdown for the entire reporting period for an extended refueling outage. Major activities during the month included installation of the core spray sparger clamps, Installation of the reactor Internals and reactor head, '
and performance of the 10 year code hydrostatic test on the reactor vessel and
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coolant piping.
Four Reportable Occurrences were identified during the reporting period:
R.O. #80-17 was identified on May 16, 1980 when the one rod Free rod withdrawal block was found to be defeated for three control rod drives by two jumpers and a defective position Indicating probe.
R.O. #80-18 was identified on May 7,1980 when the "as found" setpoint for Reactor High Pressure Scram sensor RE030 was found to be greater than the allowable limit driving performance of routine surveillance test.
R.O. #80-19 was identified on May 17, 1980 when core spray relief ,
valves were discovered to be leaking through during testing as part of 1 j the leak reduction program.
I R.0. #80-21 was identified on May 20, 1980 when it was determined the surveillance required by Technical Specification 4.9.D was not being perfo rmed.
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Oystsr Crc k Strtion #1 Docket No. 50-219 .
CORRECTIVE ELECTRICAL MAINTENANCE ON QASL ITEMS FOR THE MONTH OF May 1980 item # Equipment Malfunction Corrective Action 1 Diesel Generator Batteries Degraded battery condition Replaced unacceptable batteries 2 CRD Notch Override Switch Switch stop broken Replaced front plate on switch 3 Scram Relays Checked operation per SIL #308 Relays inspected & tested, all found to be satisfactory.
4 Vital MG Set 1-1 Defective control power trans- Replaced transformer former 5 Vital HG Set 1-1 Defective control power trans- Replaced transformer former 6 Clean-up Demineralizer Inlet Position Indication lights Installed rebuilt gear box Isolation Valve erratic 7 Cleanup Demineralizer Discharge Circuit breaker malfunction Replaced breaker to Condenser Valve during testing 8 Shutdown Cooling Minimum Flow Viv Valve wouldn't open
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- Pcge I cf 2 Oystcr Creek Stction #1
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Docket No. 50-219 ,
CORRECTIVE INSTRUMENT MAINTENANCE - QASL May 1980 item # Equipment Malfunction Corrective Action I CRD Pressure Transmitter RD04 Defective Unit Replaced obsolete transmitter with compatible unit.
2 SRM Channel 24 Instruments out of calibration Channel 24 LCR recorder span adjusted.
3 SRM Channels 22, 23, 24 Instruments out of calibration Channel 23 s 24 LCR recorder's span adjusted.
.4 lRM 15, detector & drive tube Defective Replaced
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IRM 16, detector S #4 TIP Machine in shield light Indicated early inspected 5 adjusted to indicate correctly 6 CRD 06-19 Position Indicating Constant fully in signal Replaced P.I.P.
Probe 7 CRD 06-15 Indication Position 12 didn't indicate Connection in drywell tightened.
8 CRD Drive Flow Indicator Constant Indication was less Resoldered potentiometer connections j than 0 flow ,
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9 lsolation Amplifiers - plant Defective amplifiers Replaced amplifiers (OP-AMP hodule) monitoring system l
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10 Off Gas. Radiation Monitor Continuous downscale alarm Span adjusted to indicate correctly Channel 1 ,
I 11 Torus Level Instruments Redundant Indicators were not Calibrated one transmitter In agreement
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12 Shutdown Cooling System Needle on' indicator fell off Replaced needle. Calibrated gage.
Pressure Indicator PS-438
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13 "D" Recirc Pump Cooling Water Readings were high & erratic Thermocouple connections reconnected.
Temp. Detector 14 CRD 10-11 Insert Solenoid Valve Loose electrical connection Tightened connector 123 15 Core Spray Sys I, PI 25 Pressure Needle off stem Replaced needle & calibrated gage.
Gage 16 Control Room Event Recorder Not tracing Jumpered across rheostat until new rheostat received 17 Reactor Head Flange Area Remove, inspect, reinstall None required '
Thermocouples(9) as needed a
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Prg3 I of_2 Oystcr Creek Stctido #1
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Docket No. 50-219 CORRECTIVE HECHANICAL MAINTENANCE ON QASL ITEMS FOR THE MONTH OF MAY 1979 Item # Equipment Malfunction Corrective Action 1 CRD 18-31 V-Ill valve leaking through Replaced Valve 2 V-20-26 (Core Spray) Packing leak Tightened packing bolts
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3 Biological Shield Failed local leak rate test Installed new o-rings post test -
Stabilizer Hanway #1 passed leak rate test.
4 V-27-364 (Drywell Purge Failed Leak rate test Adjusted linkage and stroke post test -
Isolation Valve) passed leak rate test.
5 V-14-6 "A" Isolation Packing Leak Adjusted packing 6 V-14-30 Emergency Condenser Valves need to be repacked Repacked valves and inspected glands V-14-31 V-14-32 V-14-33
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V-14-34 7 CRD System - NC16A Replace broken air piping Replaced all damaged piping with new back-up scram valve stainless steel fittings 8 CRD 38-19 V-107 valve stem damaged Replaced valve stem and handwheel 4
9 CRD 38-39 & 30-19 V-107 valves have damaged Replaced stem and handwheel stem and handwheel 10 CRD 38-19 V-107 valve has damaged stem Replaced stem and handwheel and handwheel 11 "B" CRD Filter High A -needs cleaning Changed filters with clean ones 12 "A" CRD Filter High AP - needs cleaning Installed new filters
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13 "A" CRD Filter High AP - needs cleaning Installed new filters 14 "A" CRD Filter High AP - needs cleaning Changed filters with clean ones
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15 V-20-26; V-20-27 Core Valves leaking through Disassembled valve, lapped seat and disc Spray System reassembled; tested OK 16 V-26-18 Failed leak test Adjusted stoke; valve then passed leak test 17 l-3 Emergency Service Water Pump Low discharge pressure Removed pump Low amperage readings Cleaneo suction bell & impellers post testing OK
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18 "A" CRD Filter High AP - needs cleaning Changed with clean filters 19 "B" CRD Filter High AP - needs cleaning Changed with clean filters 20 "A" CR0 Filter High AP - needs cleaning Changed with clean filters
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21 "B" CRD Filter High AP - needs cleaning Changed with new filters
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22 V-26-16 Not operating properly Disassembled valve, cleaned shaft, replaced o-rings; reassembled; tested OK 23 "A" CRD Filter High AP - needs cleaning Changed with clean filters 24 "B" CRD Filter High AP - needs cleaning Changed with clean filters 25 I-4 Emergency Service Water Discharge check valve stuck open Freed up hinge pin eyes & cleaned disc Pump face; post-test operates OK 26 V-6-1000 instrument air s Valve leaking Tightened body bolts - leaking stopped nitrogen system to drywell i 27 1-2 Fire Diesel Cooling water leak Tightened all fittings - leak stopped 28 V-9-4 Packing leak Adjusted packing to stop leak 29 Fire Protection System - Rx Packing leak Adjusted packing to stop leak' Bldg - 119' El. Sprinkler System isolation Valve 30 1-2 Service Water Pump Excessive vibration Rebuilt pump post-test operate
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Oystar Crock Section #1 Docket No. 50-219 REFUELING INFORMATION - MAY 1980 Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: January 5, 1980 Scheduled date for restart following refueling: June 11, 1980 Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
No Technical Specification change relative to the refueling is anticipated.
Scheduled date(s) for submitting proposed licensing action and supporting information:
No submittals are scheduled.
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important licensing considerations associated with refue1Ing, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
- 1. General Electric Fuel Assemblies - Fuel design and performance analysis methods have been approved by NRC. .New operating procedures, if necessary, will be submitted at a later date.
- 2. Exxon Fuel Assemblles - No major changes have been made, nor are there any anticipated.
i The number of fuel assemblies (a) in the core - 560 (b) in the spent fuel storage pool - 780 :
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The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
Present: 1,800 Planned: 2,600 The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
The Spring 1987 Outage.
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