ML19141A149

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NEI 99-02, FAQ 19-02-Brunswick RCS Leakage
ML19141A149
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 05/21/2019
From: Galen Smith
NRC/NRR/DIRS/IRGB, Division Reactor Projects II
To: Zimmerman T
Progress Energy Carolinas
Govan T, 415-6197, NRR/DIRS
References
Download: ML19141A149 (10)


Text

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Plant: Brunswick Nuclear Power Plant Unit 1 Date of Event: March 28, 2019 Submittal Date: May 22, 2019 Licensee

Contact:

Tony Zimmerman Licensee Tel/email: 980-373-2520/Tony.Zimmerman@Duke-Energy.com NRC

Contact:

Galen Smith, Brunswick NRC Senior Resident Inspector Tel/email: (910) 832-2831, Galen.Smith@nrc.gov Performance Indicator: BI02 - Reactor Coolant System Leakage Site-Specific FAQ (see Appendix D)? (X)Yes or ( ) No FAQ requested to become effective (X) when approved or (other date) ____________

Question Section Nuclear Energy Institute (NEI) 99-02 Guidance needing interpretation (include page and line citation):

NEI 99-02, Revision 7, Page 42, lines 3 - 6. NEI 99-02 defines the purpose of the performance indicator for Reactor Coolant System (RCS) Leakage as:

3 This indicator monitors the integrity of the RCS pressure boundary, the second of the three 4 barriers to prevent the release of fission products. It measures RCS Identified Leakage as a 5 percentage of the technical specification allowable Identified Leakage to provide an indication of 6 RCS integrity.

Event or circumstances requiring guidance interpretation:

This FAQ is being submitted to request an exemption from the NEI 99-02 guidance to report elevated Reactor Coolant System (RCS) Leakage due to plant-specific circumstances or unique conditions. Specifically, Brunswick Unit 1 is requesting an exemption related to the March 2019 RCS Leakage Performance Indicator (PI) data, which crossed the Green/White threshold due to the unique circumstances surrounding failure of a 1-inch instrument line coupling that occurred on March 28, 2019. Brunswick does not have a Technical Specification limit on Identified Leakage and reports RCS Total Leakage for this PI, as discussed on NEI 99-02, page 42, lines 33 and 34. The following describes the basis for this exemption request:

1. The RCS Leakage Performance Indicator is intended to monitor RCS leakage below the Technical Specification limit to ensure that licensees identify and trend leakage early and take timely corrective actions well before the technical specification limit is reached.

RCS pressure boundary material is ductile by design and typically exhibits a leak-before-break failure mechanism in which cracks begin small and leakage progresses over time.

The RCS Leakage Performance Indicator is intended to monitor licensee behaviors in taking prompt action to address RCS leakage before it reaches the limit in the Technical Page 1 of 10 Revised 20180520

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Specifications.

Contrary to this, the March 28, 2019, Brunswick event resulted from the immediate circumferential separation of a 1-inch coupling on the steam side sensing line for reactor vessel level indication, as shown in Figures 1 and 2. Based on the material of construction and environmental conditions (i.e., temperature, hydrogen), the post-event metallurgical report determined the coupling showed no evidence of localized plastic deformation. The coupling experienced hydrogen embrittlement and did not exhibit a leak-before-break failure mechanism. There were no precursors to this event and the resulting leakage from the break exceeded the Technical Specification (TS) limit. RCS leakage was stable and well below the TS limit before the event. The steam leak could not be isolated from the reactor vessel. Operations took prompt action to reduce power, commence a plant shutdown, and depressurized the reactor to stop the leak. The leakage resulted in the declaration of an Unusual Event (UE). Operations completed an uncomplicated reactor shutdown. It was the last reading taken before entering Mode 4 (i.e., the Mode in which the SR is no longer applicable) that caused the PI to transition from Green to White. RCS leakage was stable and was being appropriately managed before the event. Based on these unique circumstances, Brunswick requests an exemption to exclude reporting the leakage from the event in the RCS Leakage PI. This would result in the PI returning to Green for March 2019.

2. As a result of the event, the NRC initiated their event follow-up process (IMC 0309, Reactive Inspection Decision Basis for Reactors, and IP 71153, Follow-Up on Events and Notices of Enforcement Discretion) to determine if it was appropriate to enter Management Directive 8.3, Incident Investigation Program to initiate a follow-up inspection (Special Inspection). In performing the plant response and event follow-up checklist the NRC evaluates control room conduct, the circumstances of the leak, plant conditions, and the associated risk of the event. NRC determined that a Special Inspection was not needed. Since the RCS leakage was low prior to the event with no precursors, the supplemental inspection initiated for a White PI would be redundant, in part, to that which has already been inspected. Based on the fact that Brunswick has already replaced all the susceptible couplings in both Units and given the unique characteristics of this failure, plant-specific circumstances should be considered to exempt recording the leakage from the event as part of the indicator and evaluate under other NRC processes.

Problem Statement: The RCS leakage Performance Indicator (PI) monitors leakage that is below the Technical Specification (TS) limit to ensure licensees take prompt actions to monitor, diagnose, mitigate, and correct RCS leakage to prevent it from progressing into a more significant condition.

At Brunswick Nuclear Plant, Unit 1, RCS leakage was stable, monitored and managed well below the TS Limit with the PI low in the Green performance band prior to this event. On March 28, 2019, a 1-inch instrument line failed without any prior indications, resulting in exceeding the TS limit for RCS total leakage, as shown in Figure 3. A deliberate, controlled shutdown of Unit 1 was undertaken that was commensurate with the risk associated with the Page 2 of 10 Revised 20180520

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage leakage. The location of the leak prevented it from being isolated, requiring the depressurization of the RCS to stop the steam leak. There were no precursors for the failure of this instrument line. The last data point taken in Mode 3 was 13.93 gpm as shown in Figure 4. This was the only data point in March 2019 that exceeded the 50% of the TS Total Leakage Green/White threshold of >12.5 gpm.

NRC Region II implemented their event follow-up procedure and did not raise any concerns with the performance of the Operations crew responding to the leak. Duke Energys position is that the absence of any precursor to the leakage and the prompt action of the Operations crew in responding to the leak provides special circumstances not addressed in the PI guidance. Duke Energy requests an exemption to exclude reporting leakage from the event in the RCS leakage PI calculation, which would return the indicator to Green for March 2019. While this FAQ is being resolved, the Brunswick Unit 1 first quarter 2019 RCS Leakage PI was reported as White on April 22, 2019, for the PI exceedance on March 28, 2019.

Brunswick, Unit 2 was shut down for a refueling outage during this event.

Event

Description:

At 1419 on March 28, 2019, while operating at 100% reactor power, the Brunswick Nuclear Plant Unit 1 N004B narrow range reactor water level instrument (1-C32-LI-R606B) failed high.

N004B is an instrument tap off the steam space of the reactor vessel. Drywell pressure and drywell floor drain leakage increased. Operators controlled drywell pressure and reduced reactor power per the immediate power reduction instructions. An Unusual Event was declared at 1450 based on elevated drywell leakage and reported to the NRC via Event Notification 53961. A controlled shutdown of Unit 1 was undertaken that was commensurate with the risk associated with the leakage. This timely action by the operators mitigated the leakage while preventing an unnecessary transient on the plant by performing a scram from a high power level. Timeline of event:

March 28, 2019 - Unit 1 operating at full power 1419 - N004B narrow range Reactor Pressure Vessel level instrument failed high Drywell pressure and floor drain leakage increased Entered TS 3.4.4 RCS Leakage for unidentified floor drain leakage Operators reduced reactor power per the immediate power reduction instructions 1429 - Drywell pressure slowly lowering in response to operator action 1438 - Drywell Floor Drain sump alarm increased above setpoint, automatic actions in progress (sump pump started) 1440 - Drywell Floor Drain sump level lowered below reset point and alarm cleared 1450 - Declared Unusual Event due to elevated drywell leakage Operators continued reducing power in accordance with procedures 1600 - RCS leakage data recorded at 8.3 gpm as shown on Fig. 4 1603 - Operators completed a manual reactor shutdown in accordance with procedures Reactor Pressure Vessel level maintained in established level band Page 3 of 10 Revised 20180520

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Scram recovery and cooldown - no significant problems 2000 - RCS leakage data recorded at 11.51 gpm as shown on Fig. 4 March 29, 2019 - Unit 1 shutdown 0000 - RCS leakage data recorded at 13.93 gpm as shown on Fig. 4 0238 - Entered Mode 4 Investigation inside containment determined that a 1-inch coupling on line 1-B21-774 located on the steam side of a reactor level condensing chamber experienced a 360° circumferential separation at the approximate center of the coupling as shown in Figures 1 and 2 below. This opened a path for steam from the reactor to leak into the drywell. Reactor water level was maintained in the established level band, below the level of the sensing line nozzle, throughout the event. The impact from the coupling failure has been analyzed by the Duke Probabilistic Risk Assessment staff and determined to be very low safety significance.

Approximately 1.5 days before the event, the Brunswick, Unit-1 measured an increase in drywell pumping and implementing procedure 0OI-02.3, Drywell Leakage Control. Investigations determined that the cause of the higher measured leakage was a failed vacuum breaker which allowed water to flow back into the sump after it had been pumped out, causing it to be counted twice by the integrator for the RCS Leakage calculation. The integrator was observed to be clicking or counting leakage when the pump was not running. This measured leakage was not related to the coupling failure and did not represent an increase in actual RCS leakage. In addition, there was no indication of increased activity on any of the Radiation Monitors, which provides additional assurance that this was unrelated to the coupling failure. The vacuum breaker was repaired during the outage and leakage rates returned to historical normal values.

Basis for Exemption from guidance:

Appendix E of NEI 99-02, Revision 7, allows an exemption to be submitted via the FAQ process for plant-specific circumstances such as unique conditions. Duke Energy is requesting this based on the unique conditions of this RCS leak in that it was not a leak-before-break and not indicative of chronic unresolved elevated RCS leakage. The RCS Leakage Performance Indicator is intended to monitor how licensees manage RCS leakage below the TS limit to ensure that timely corrective actions are taken in advance of reaching the TS limit. As stated in Appendix C of SECY 1999-007, Barrier Integrity Key Attributes and Means to Measure:

Research has determined the RCS pressure boundary has a high probability of experiencing a leak prior to a rupture (i.e. "leak-before-break"). Therefore, the extent of such leaks offers an objective perspective on the probability of a more catastrophic failure.

A foundational assumption of this Performance Indicator is that the RCS pressure boundary has a high probability of leak-before-break and that the PI is intended to monitor these precursor events. Additionally, in NRC Staff White Paper titled, Objective of the RCS Leakage Performance Indicator, from the June 26, 2013, ROP Working Group Public Meeting (ML13203A258), the NRC Staff made the following statement on page 20 of 60 regarding an Observation from the Davis-Besse Lessons Learned Task Force (LLTF):

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NEI 99-02 FAQ 19-02 Brunswick RCS Leakage As documented in LLTF recommendation 3.3.3(3), the intent of the current RCS Leakage PI is to call attention to those plants that have identified primary systems leaks but have not corrected them in a timely manner.

The PI is intended to monitor leak-before-break situations that are viewed as precursors of a more catastrophic failure. In the Brunswick event, RCS Total leakage had been steady for the month of March as shown below in Figure 3. There was no advanced indications of degradation or leakage from the coupling and no trend that worsened over time due to operator inaction.

As shown in Figure 3, RCS Leakage trends were stable and low in the Green performance band for the month leading up to the coupling failure. The coupling failure occurred without warning.

Drywell leakage and temperature in the vicinity of the coupling did not increase prior to the failure. There was no opportunity for Operations staff to identify this condition in advance of failure. As no precursors were present, no mitigating actions could have been taken in advance of the leak and the actions taken following the leak indicate prompt and conservative response on the part of the licensee. In addition, the location of the leak prevented it from being isolated until the plant was depressurized, which added to the volume of the leakage calculated in the PI.

Despite timely operator actions to accomplish this, the volume of leakage calculated in the PI resulted in one calculation data point exceeding the threshold for White. The degradation mechanism of the coupling will be evaluated under other NRC processes.

The leakage measured during the event should not be counted in the RCS Leakage PI because the operators exhibited the behaviors consistent with the intent of the performance indicator.

Operations took prompt action to conduct a safe and stable shutdown, minimizing the transient to the plant, in the interest of safety. Including this leakage in the performance indicator and taking the actions associated with a White PI could have the unintended consequence of providing an incentive to licensees to depressurize the plant in a less controlled manner without a commensurate benefit to public health and safety.

A Root Cause Evaluation was initiated following the March 28, 2019. The coupling that failed was a 1 Cryofit (cryogenic) coupling. Cryofit couplings are devices used to connect small bore piping (1-inch nominal pipe size and less) without welding. They are fabricated from a shape memory alloy (SMA) material composed primarily of Nickel-Titanium-Iron (Tinel) which experiences a phase change at cryogenic (extremely low) temperatures. To prepare for installation, the Cryofit coupling is cooled below the transformation temperature. The ends of the coupling are then expanded and the coupling is stored in the cold, expanded state. The pipe ends are inserted into the coupling while it is cold. The phase change causes the coupling to shrink as its temperature rises from its installation temperature of less than -200° F to ambient temperature and above. This results in an interference fit that does not require welding. This unique effect is produced by a phase transformation, i.e., an instantaneous shear transformation between the alloys body-centered cubic austenite phase and its highly twinned martensite phase.

These couplings had been installed at Brunswick for approximately 30 years.

Examination of the failed coupling was conducted at the McGuire Island Metallurgical lab.

Microhardness testing, visual microscopy and scanning electron microscopy were used to characterize the failed material. Using metallurgical analysis and investigation of the process Page 5 of 10 Revised 20180520

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage conditions at the coupling location, the Root Cause Evaluation team determined that the failure was due to hydrogen embrittlement of the Tinel material. This resulted from many years of exposure to high temperature and high levels of hydrogen. This conclusion is supported by the transgranular cleavage, high hardness values in the region exposed to the process fluid, and a hydrogen rich environment, which are all consistent with hydrogen embrittlement.

An evaluation was performed to address the couplings installed in both units. All couplings exposed to reactor steam (i.e., potentially susceptible) were removed and replaced with welded fittings prior to startup of Units 1 and 2. In addition, the installation procedure for the couplings was placed on hold pending revision, to prevent any further installation of Cryofit couplings.

RCS Leakage Data Collection:

The BNP Technical Specifications defines the frequency of Surveillance Requirement (SR) 3.4.4.1, RCS Operational Leakage, in accordance with the Surveillance Frequency Control Program (SFCP). The Brunswick SFCP has an 8-hour frequency for this SR. This is consistent with NUREG-1433, Revision 4, General Electric BWR/4 Standard Technical Specifications, which lists an RCS Operational Leakage Surveillance Requirement frequency of 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, or in accordance with the SFCP. As a normal practice, Brunswick performs this surveillance every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> in Modes 1 through 3 as a conservative approach to ensure the completeness of the required surveillance. It was the last data point collected before entering Mode 4 that caused the PI to transition from Green to White.

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NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Figure 1, RCS Leak location Page 7 of 10 Revised 20180520

NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Figure 2, Picture of failed 1-inch coupling:

Figure 3, March 2019 Reported RCS Leakage (4-hour periodicity)

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NEI 99-02 FAQ 19-02 Brunswick RCS Leakage Figure 4, Brunswick Unit 1 total RCS Leakage CDE data reported:

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NEI 99-02 FAQ 19-02 Brunswick RCS Leakage If licensee and NRC resident/region do not agree on the facts and circumstances, explain:

The Brunswick Senior Resident Inspector reviewed this FAQ, said it appears to be factually correct and had no comments.

Potentially relevant FAQs:

N/A Response Section Proposed Resolution of FAQ:

This FAQ is proposed as a plant-specific exemption for the subject event and the RCS leakage data immediately following the transient initiated by the instrument line coupling failure. The RCS leakage associated with this event should not be counted, due to the unique circumstances of the event. RCS Leakage was stable and well below Technical Specification limits before the event, the identified couplings were replaced prior to plant startup and there would be negligible benefit in transitioning the plant to Column 2 of the Action Matrix and performing IP 95001.

PRA update required to implement this FAQ?

No MSPI Basis Document update required to implement this FAQ?

No NRC Response:

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