ML19294B459

From kanterella
Revision as of 10:57, 8 November 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 80-002/03L-0:on 800103,operator Found Valve Stem on HPCI Stop Valve Broken Separating Valve from Operator.Caused by Valve Stem Being Overstressed During Process of Freeing Stop Valve Piston on 790912.Valve Reassembled
ML19294B459
Person / Time
Site: Cooper Entergy icon.png
Issue date: 01/21/1980
From: Phillips D
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19294B458 List:
References
LER-80-002-03L, LER-80-2-3L, NUDOCS 8002280430
Download: ML19294B459 (1)


Text

NRC FORM 366 U S. NUCLE AR REGULATOR' COMMISSloN sm -

UCENSEE EVENT REPORT l  ! l 1 I (PLE ASE PRINT oR T'rPE ALL RECUIRED INFORMATIC"o coNTRotstocx( ]@

7 o l1, l, Nl EIL.CClE.P! . m a RI 11@.l 4 01 OI - I O lxEsu

s 0 ! NO !.m 01 -l 0 01 0 @l'. !1.a~t

-

.e .

I il il 1a@lv i

-_ - l@

cCvT oI' M '; I L @l0 510l0101219I3w@l0111O!3l Aln@l0l1 gl ti al n @

4 w e ;Om e . m Ea 6; o eNT 0 ATE '4 :s sePCHT C ATE w EVENT DESCRiPT*CN i.NC PCCB ABLE CC'. SEQUENCES (h

, T. puring normal operation, an operator found the valve stem on the HPCI stop valve l

., ,, broken separating the valve from the operator. The redundant sy. stem, ADS, was oper-t , i .; able as were all low pressure injection systems. Since the valve is pushed open bv 1 i , the operator, the HPCI would have cerformed its intended safety function if recuired!.

' i-- There were no adverse affects to &blic % ,1

  • 5 ,-d Wa" ,e , -o c n 1 * # We o"c I

. I! l l ) !d l l 80 g y S v 0 T E *.1 CALSE CALSE COYP VALVE CCE JCCE CLSCCOE JYPC'NENT CODE SLBCODE SUBCODE

'

l9 l S l F l @ l A l@ ([,]@ U

!AlI lV r l Vl@ @ N

@

4 i

1.3 t, i; IJ nt 19 aE JL EN TI AL Ut a b46'.Cf HEPoHT W V l5'ON

_:vFNTfEAR REPCRT NO COCE TYPE NO.

@ $ ;;;al 18101 l-l loinI,I l/l Inl 7 :")I Lt_J I-I Laj

'

_:' 22 23 24

"

.b  :* :S 30 31 3:

ACTION SUTLnE ESFECT SHuTDOAN ATT ACwY E N T N PR O-4 PR3VE COMP COYPONENT TAKEN AC TION QN PL ANT YETHOD HOURS 2 SUBYlTTED 50HM w8 SLFPUER MANLFACTUAER lAl@lZ @ l Z l@

JJ 34 35 y@

36 l0l0l0l01 3/ 40 I Nl@

41 l

42

@ lNl@ IS l0 17 15 l @

43 44 47 CAUSE CESCRIPTION AND CCARECTIVE ACTIONS

'

o The stem for a 10" inverted n41 n n n'-n e na c en, , 1-o m ,,c,c*nvoA u S A ,,

  • t , my

_

I

,

, jKoerting Con:pany was overstressed while freeing the stuck valve piston. A new stem I

, , yas installed and the valve internals were cleaned and inspected. The valve was l

, 3 l reassembled and HPCI operability was verified (S.P. 6. 3.3.!4) . I I 4j l l 7 8 i 90 F ACILITy , UE T**00 0F STAfus .POWE9 OTHER ST ATUS DiSCOV E R Y DISCOk ERY CESCR'PTION I '" [f_j@ l0l9l6l@ 10 NA 44 I lAl@l Observed by Ooerator on Tour 80 l

r 8 1 12 11 4's 46 AC TIVI T Y CON TEN T

  • RE L,E ASED OF RELE ASE AMOUNT OF ACTivlTY LOC ATION OF RELE ASE i a l Zl @ LZj@l NA l l 45 NA 80 l
  • 4 1 10 11 44 PERW%EL F MPOSUR[5 5 8.'H E R TYPE DESCRIPTION '

i 7 l010l0l@(Zj@lNA 1 8 i t1 1: 13 60 PE NSONNE L 'NJL A'E 5 NLYHE H DESCR PTION a

lo lo lo l@l s l' 11 u

60 I

t uw r af ist D AM AyE TO F ACils rv tvPE i;E sGttPTION s A d @l i to NA ga I

" "

hj@l

, ,u t i u nP f luN OO2280 @0 -

. o u I I l l l l i l l l l l_LJ80:.1

< << ) to 68 69 NAVE CF PREPARER " i %4114po PHONE- '02-Q'5-Mll